Tiwest Joint Venture

Transcription

Tiwest Joint Venture
Tiwest Pigment Plant
Kwinana
Using Downtime & Uptime Metrics to
drive plant improvement
Tiwest Joint Venture
Presentation
• Tiwest
• Why we needed the system to collect
Downtime & Uptime data
• What is the system
• How do we use for improvement
Lessons learnt
Tiwest Joint Venture
Tiwest Joint Venture
Tiwest Sites
Location Map
Tiwest Joint Venture
Tiwest Joint Venture
• Mine at Cooljarloo (Heavy mineral concentrates)
• Heavy Minerals Separation and Synthetic Rutile plant
at Chandala
• TiO2 Pigment Plant at Kwinana
Uses technology licensed by Kerr McGee to
make ultra white TiO2 pigment.
97,000 tonnes pa.
260 employees
Used in coatings, plastics, high gloss paints, ceramics, paper,
cosmetics, sunscreen, smarties ……………….
The Kwinana Pigment Plant
Tiwest Joint Venture
Maintenance status - 2002
Tiwest Joint Venture
• Lack of planning and detailed measurement
• Four building blocks to establish
–
–
–
–
Planning & Scheduling
Maintenance KPIs
Plant performance measurement
Robust improvement cycle
Tiwest Joint Venture
What is the system?
What is this system ?
Tiwest Joint Venture
Downtime
– Automatically record all instances of plant downtime
and allow for Operator entry of plant information
Uptime
– Automatically record all instances of plant production
rate reduction below a specified threshhold and allow
for Operator entry of plant information
Emmission Alarms
– Automatically capture all small scale fugitive
emissions and allow for Operator entry of plant
information
Other
Plant
Tiwest Joint Venture
A
A
Services
B
B
C
C
D
Chlorination
Oxidation
Finishing
Tiwest Joint Venture
Tiwest Joint Venture
Tiwest Joint Venture
Lessons:
Lessons:
Guidelines around coding Categories
Operator training
Create the need !
Start with the bottleneck Predict how you want to analyse the data
Design the database
Downtime first, others after
Be prepared to change
Prototype on a spreadsheet
Make easy for manual input
Tiwest Joint Venture
Rate
hurdle
Average
rate for 4 hr
period
Manual
entries
Tiwest Joint Venture
Lessons:
Update rate target
Plan for how you want to report data
Manual data needs vetting
Ensure can extract to Excel
Tiwest Joint Venture
Manually
entered
System Architecture
DCS
SCADA
Rosemount
Wonderware
Lessons:
Affect from virus attack
No licences but no backup
Technology flexible and cheap
Tiwest Joint Venture
Data
Historian
INSQL
SQL Server
Microsoft
Control
room
PC
Engineers
PC
Managers
PC
Tiwest Joint Venture
How do we use it for improvement
Improvement process
Weekly
– KPI review
– Action plan progress review.
– Future action plan commitment
Monthly
–
–
–
–
–
Weekly review
Are we getting the results?
Are we targeting the right things ?
Readjust priorities
Improvement targets for month
Tiwest Joint Venture
1 Month Pareto – Lost
Tonnes
Lessons:
Convert Downtime and Uptime to tonnes lost
Make sure don’t react to short term one of issues
Tiwest Joint Venture
3 Month Pareto – Lost
Tonnes
Lessons:
Show operators & trades the data
Use Excel for graphing to prototype
Tiwest Joint Venture
Lost Tonnes Monthly
Comparison
Tiwest Joint Venture
1
2
3
4
5
1000
0
6
7
8
9
10
So
ut
as h o
f
h
/ T Ca
ra l co
ns n
N Ya
E
Sa
o rd
n d Ra f U
Sa Se c k 300
n d p L Bo
e ile
So Se ve rs
ut p L l 3
h
ev SW
o
Li f G el 3
m
3
N
0
e
Sc 1 B W
ru l ...
H bb
2S er
O
E
U 4 C as t
4
D 00 ool
20
N e
1C W rs
C Do
C hlo or
G ontr rin
55 o
a
2 l R to r
R
ac Sna oom
k
O ke S 2
U ff C ou
40
ol
th
D 0 S l ect
20 o
i
o
1A uth n
C Do
hl
or or
in
at
or
Month
5000
4000
3000
2000
Chlorine Alarms by Month
29
27
25
23
21
19
17
15
13
11
C
Chlorine Alarms by Area
9
7
5
3
1
on
tro
l
Se
la
s
C
ok
e
Bo
un
dr
y
A1
Sn
ak
e
A4
00
Pi
pe
ra
ck
hl
or
in
at
io
n
1600
1400
1200
1000
800
600
400
200
0
N
ec
ov
er
om
y
pr
es
sio
n
C
C
R
Gas Alarms
Tiwest Joint Venture
Chlorine Alarms by date
500
400
300
200
100
0
Chlorine Alarms by Tag
800
700
600
500
400
300
200
100
0
Summary – Lost Tonnes – For
Discussion
Tiwest Joint Venture
Lost Tonnes
Event
Current Trends / Comments
What Do We Think Is Working?
Further Ideas / Actions?
• Scheduled
Maintenance
• Dec03 saw improved consistency in
frequency and duration
• Shut co-ordinator (75%)
• Shut planning / scheduling /
execution
• Shut co-ordinator (other 25%)
• Tighten durations / CP
• Strategy for reducing frequency at higher
line rates
• Full Sand
Separator
• 85% drop from OctNov03 to Dec03
• N2 purge system
• Dump valve timing
• Increased dump leg size
•?
• Chlorinator
Recycle Header
Pressure
• 75% drop from OctNov03 to Dec03 –
mainly during Chlorinator rebricks in
OctNov03
• Ceramic venturi crossover
• Install cerramic venturi crossover on other
lines
• Clean out header on plant shut
• Chlorinator PM routines and quality of work
• U200 Problems
(chlor offline)
• 90% drop from OctNov03 to Dec03 –
mainly during Chlorinator rebricks in
OctNov03
• Alignment of D Chlor shuts with Line
Shuts
• Align all Chlor shuts with Line Shuts
• Chlorinator PM routines and quality of work
• TIC/HIC
Blockages
• Highest loss in Dec03 – a result of DCS
failure on Boxing Day
• G222 Repack
• No issue in Dec03 – need to be 100%
sure that further ideas will fully address
problems
• B309B Oxidiser
Water Leak
• One off event at end of Oct 03 – need to
be 100% sure that problem fully
addressed
• Data Not
Recorded
• Data entry improving each month
• Increased focus on data entry
• K Jarvie work on Reporting System
• DCS Failure /
Lost control file
• One off electrical hit on Boxing Day
(second highest loss in Dec03)
• N/A
• N Bell action plan
• Sand Blast
• Gradually increasing through Dec03.
Sympton of oxidiser / shotgun issues
• N/A
• TOP PRIORITY – Production Team
• Clean out / replace pipework on plant shut
• “Excess XOver Temp Strategy” idea from
MT?
• Online repacking
• Install harder packing ring and collar
• Replace during Puri upgrade
• Actions from original root cause
investigation?
Drilldown – Paretos – High Level Summary
Loss
P/M?
Comment
Current Initiatives
Whom
Scheduled
Maintenance
Maint/
Prodn
A Line Ceramic oxi
installation (27%)
Additional Line Shuts
(14%)
Scheduled Line Shuts
incl. overruns (59%)
Lock in Shut Co-ordinator role
Execute Line shuts to agreed schedule
Close loop on Shut performance (esp. startup
issues) to eliminate overruns
Review Dec performance and capture ideas to
reduce duration
Two major events plus
multiple events on A
and B Lines
Agree and approve idea form for improving N2
purge monitoring and control
Workshop to determine frequency of scheduled and
event based cleaning of sand separators
Implement idea for increasing K+ to 1000 ppm on B
line for Grade 834
Implement idea for optimising dump leg valve timing
Sand Separator
Levels
Prodn
Tiwest Joint Venture
When
Pot. Redn.
T Young
A Temp.
T Young
8 Jan
In prog
15 Jan
60%
A Temp,
15 Jan
J Cullen
5 Dec
D Anderton
12 Dec
N Kon-Yu
8 Dec
G Theunissen
12 Dec
50%
G222 Repack
Maint
Four events in Oct/Nov
Agree direction following purification review
Agree go / no go decision on improved pump
Commission N2 regulation
G Hewson
T Munro
K Matthias
12 Dec
12 Dec
20 Jan
50%?
Chlor Recycle
Header Pressure
(during re-bricks)
Prodn
Low rates due to A/B/D
Chlor rebircks. Wet air
caused blocked tuyeres
See separate action for Chlor Recycle Header
Pressure (excl. re-bricks)
N/A
N/A
100%
G301 Gearbox /
Coupling
Maint
Majority of problems on
G301B
Short term corrective actions completed
Capture further actions in idea 3011
Execute action plan
K Matthias
J Smith
K Matthias
Done
10 Dec
31 Jan
75%
Tube Bundle
Failure
Maint/
Prodn
Single event
Confirm all resulting actions completed / locked in
L Hughes
12 Dec
100%
Plant Shut –
E210A Reboiler
valves
Maint
Single event
5 Dec
12 Dec
19 Dec
100%
A Templeman
Submit AFE for replacement valves
Approve AFE
Confirm estimated installation date
J Smith
T Martin
J Smith
Lost Tonnes Charts Comments
Tiwest Joint Venture
Tracking Down…
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•
•
•
Line (Scheduled) Maintenance – due to high focus on shut execution and benefit of regular,
scheduled shuts
Recycle Header Pressure / Standby U200 – record chlorinator OSE, rebricks back in Nov03
Sand Separator Level – larger dump legs installed, cleaning regime, increased reliability of
dump valves
G222 Packing Failure – online repacking procedure
Tracking Up…
•
•
•
Node Failures / TIC/HIC blockages / Crossover Temps – mainly due to one event on Dec 26th
Shotgun Changeout / Sand Blast – TOP PRIORITY
Fouled vapourisers – ongoing issue and D213 solids carryover
Next Steps…
•
•
•
Progress ideas to Cash Flowing status
Review existing ideas for “Tracking Up” areas to ascertain what’s working / not working
Generate new ideas to address “Tracking Up” areas
Tiwest Joint Venture
Further extensions to the system
Shift supervisor handover
Morning meeting data
Tiwest Joint Venture
Shift supervisor handover
Morning meeting data
Tiwest Joint Venture
Control Room
Operator Log
Every 4 hours the
most important
points are logged
Tiwest Joint Venture
Parameter
outside
limit
Tiwest Joint Venture
Control Room
Operator Shift Log
for shift supervisor
Conclusion
Tiwest Joint Venture
• A formal plant improvement process requires
recording of plant information. It is a building
block of good maintenance.
• Tiwest has delivered significant improvement
using targeted improvement strategies
Tiwest Joint Venture
Thankyou
Implementation & Lessons
learnt
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Prototyped on spreadsheet
Started on Downtime
Never right the first time/ technology can make quick changes
Predict how you want to analyse the data
Construct database to reflect
Make easy for manual input
Rules around coding
Operator training
Need a need form line personnel
Show analysis to personnel
Ensure can extract to EXCEL
No licences/ no backup
Start on bottleneck
Update rate target
Technology is flexible and cheap
Allow for expansion
Plan for what you want to get out of it
Manual data input needs vetting
Design for Operator entry and reporting output
Tiwest Joint Venture