CNRL Extraction Water Treatment Plant Pilot Study
Transcription
CNRL Extraction Water Treatment Plant Pilot Study
CNRL Extraction Water Treatment Plant Pilot Study Basal Water Phase Final Report 2012 May 29, 2013 Prepared for: Canadian Natural Resources Ltd. Calgary, Alberta Attn. Kavithaa Loganathan Manager, Water Treatment Pilot Projects Prepared by: EPCOR Suite 1210, 401-9 Avenue SW Calgary, AB T2P3C5 epcorwatersolutions.com phone: 403-717-4600 STATEMENT OF QUALIFICATIONS AND LIMITATIONS EPCOR and all persons involved in the preparation of these materials disclaim any warranty as to accuracy or currency of the contents. These materials are provided for informational purposes only and on the basis that none of EPCOR or other persons involved in the creation of these materials will be responsible for the accuracy or currency of the contents or for the results of any action taken on the basis of the information contained in these materials or for errors or omissions contained herein. None of EPCOR or other persons involved in the creation of these materials is attempting to render business, scientific, legal, accounting or other professional advice. The materials contained herein should in no way be construed as being either official or unofficial policy of any governmental body. Version 1.1 Date (DD/MM/YY) 05/12/12 2.0 20/02/13 2.0 29/05/13 Revision Notes Originator(s) DRAFT for comments from Technical Team DRAFT accounting for comments from technical team review Finalized version of report B Leinan S Molla B Leinan S Molla B Leinan S Molla CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 2 of 80 ACKNOWLEDGEMENTS Kavithaa Loganathan Joy Romero Ashok Babu Charles Williams Mike Rogers Steve Stanley Audrey Cudrak Jamie Gingrich Lee Ward Rob Brown Don Macuch David Rector Vicki Campbell Ryan Litwinow Brent Leinan Saif Molla Andrew Rose Ryan Thomas Zach Pruden Lyle Deines Stan Epp Leonardo Paternina Stephen Peters Brian Mottershead Glen Sinclair Garry Germscheid David Parker Steve Kroll John Korpiel Jean-Francois Beaudet Ryan Colley Jeremy Jones Martin Gendron CNRL CNRL CNRL CNRL ATSI EPCOR EPCOR EPCOR EPCOR EPCOR EPCOR EPCOR EPCOR EPCOR EPCOR EPCOR EPCOR EPCOR EPCOR EPCOR EPCOR EPCOR EPCOR EPCOR LSI LSI Veolia Veolia Veolia Veolia Veolia Veolia Veolia Project Manager VP Technology Development Lead Technology Development Project Coordinator Technical Advisor SVP Water Services Director, Project and Technical Services Senior Manager, Operational and Technical Senior Manager, Project Development Manager, Water Project Development Project Controls Director, Oil Sands, Industrial Water Manager, Northern AB W & WW Project Manager Project Manager Piloting Engineer Lead Hand Operator Crew A Lead Hand Operator Crew B Operator Operator Operator Operator Operator Operator Director, Water Projects Project/Construction Manager Project Manager VP Business Development Senior Process Engineer Manager - Technical Services Pilot Project Engineer Applications Engineer Field Engineer CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 Overall Project Management Project Executive Project Support Project Support Project Support Project Executive Executive Sponsor Senior Pilot Engineering Advisor Program Manager Project Oversight Project Support Project Support Project Support Project Manager – Construction Phase Project Manager – Piloting Phase Pilot Design and Analysis On-site Liaison and Operations Lead On-site Liaison and Operations Lead Operations and Process Optimization Operations and Process Optimization Operations and Process Optimization Operations and Process Optimization Operations and Process Optimization Operations and Process Optimization Project Support Construction Support Project Manager – Vendor Project Support Project Support Project Support Operations Support Operations Support Operations Support May 29, 2013 3 of 80 EXECUTIVE SUMMARY Canadian Natural Resources Ltd. initiated an Extraction Waters Pilot Study to determine the lowest cost option for an Integrated Water Management Plan. Source water for treatment included Basal Water and Recycled Water (RCW) from the Tailings Pond. The pilot study is divided into two phases based on source water type. Phase 1 involved the treatment of basal water. Phase 2 involved the treatment of tailings pond recycle water. This report is focused on the basal water treatment piloting phase of the project, which took place between June 7th and October 8th, 2012. A separate report will address Phase 2 pilot testing subsequent to completion of the pilot in early 2013. The experimental phase of the pilot was started in April 2012 and is scheduled for completion in early 2013. EPCOR has been contracted to execute the pilot in concert with a CNRL project team, with support from equipment vendors. Lockerbie Stanley Inc. (LSI) was contracted to carry out the construction and maintenance of the pilot facility. All process equipment used in the Basal treatment phase was supplied by Veolia. EPCOR led the reporting and analysis of pilot scale data, with input from both CNRL and Veolia personnel. Veolia has prepared a document (included as an Appendix in this report) with input from both CNRL and EPCOR, that details scaling up the piloted equipment to a full scale treatment facility. The pilot facility was located on CNRL Horizon site adjacent to 99A plant, which is on the north side of the site, adjacent to the tailings pond. Basal water was trucked directly from the basal water wellheads to the pilot influent water storage tank. Basal water is typified by neutral pH, low to moderate TSS and high TDS (Table E1). TDS is primarily composed of sodium, chloride, bicarbonate and hardness-causing compounds. Organic compounds were at low concentrations, with the ability to measure low levels compromised by high detection limits resulting from the high salinity of the water. TOC was less than the detection limit (13 mg/L) for 88% of samples taken. Oil and Grease (O&G) was consistently low. Table E1. Primary water quality characteristics of untreated basal water Parameter Units Average Std. Deviation pH SU 7.0 0.1 TSS mg/L 23.4 81.5 TDS mg/L 21,300 3,456 Chloride mg/L 12,456 509 Bicarbonatemg/L as CaCO3 3,638 193 Total Hardness mg/L as CaCO3 1,450 102 Total Organic Carbon mg/L <13 mg/L 2.8 Oil & Grease mg/L 1.1 0.3 CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 4 of 80 Potassium Permanganate Sulphuric Acid (option) Metabisulphite & Anti-Scalant Ferric Chloride & Caustic (option) Basal Tank Reaction Tank Polymeric Ultra-Filtration (PUF) Reverse Osmosis (RO) Figure E1. Basal water treatment process train The treated water quality goals for the basal water treatment phase included effluent Total Dissolved Solids (TDS) < 1000 mg/L, Sodium < 500 mg/L and the maximum possible recovery for reuse. An overview of the treatment train is provided in Figure E1. The goal of each treatment step and optimal operating conditions determined by the pilot are described below. Oxidation/Precipitation/Coagulation The goal of including an oxidation treatment step in the treatment train was to precipitate out sulfides, iron, and manganese, which had the potential to negatively impact fouling rates on the UF and RO membrane systems. Based on pilot observations on downstream membrane fouling, optimal operation was identified as maintaining a neutral pH in the oxidation/precipitation stage, adding permanganate at a fixed dose in order to precipitate iron and sulphides, but keeping manganese in dissolved form. Bench scale experimentation using sodium hypochlorite was carried out as an alternative oxidant to potassium permanganate, but not examined at the pilot scale. Use of sodium hypochlorite instead of potassium permanganate would reduce the dissolved manganese concentration in RO feed water. Optimal chemical dosages for this unit process identified in the pilot are presented in Table E2. Table E2. Optimal process settings for Oxidation/precipitation/coagulation Parameter Optimal Setting Potassium permanganate = 1 to 1.5 mg/L Ferric chloride = 0 to 2 mg/L as Fe Sodium Hydroxide = 0 mg/L CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 5 of 80 Ultrafiltration (UF) System The primary goal of the ultrafiltration step was solids removal. The UF system used during the pilot was a polyvinylidene fluoride (PVDF) hollow fiber outside - in type (DOW SFD 2860 module) membrane. The strategy for managing fouling of the membranes was primarily through a combination of frequent physical backwashes combined with the use of Chemically Enhanced Backwashes (CEBs) at regular intervals. Clean-In-Place (CIP) procedures were also utilized when a more significant membrane clean was required. Backwashes (non-chemically enhanced) were less effective at restoring performance than anticipated. Solids removal was consistently good, with UF filtrate turbidity averaging 2.0 NTU and Silt Density Index (SDI) averaging 0.9 over the course of the pilot (well water source). RO feed requires an SDI of less than 5 at a minimum and ideally less than 3. UF filtrate concentrations of iron and sulphides were consistently low enough to achieve targets based on the perceived ability of anti-scalant chemicals to manage fouling on the downstream RO membranes. Pilot data and the results of the membrane autopsy indicate iron was the primary foulant on the UF membrane, with a notable concentration of sodium present as well. Two pH ranges were trialed during the pilot: elevated (pH 7.5 – 8.0) and neutral (pH 6.9 – 7.2). The impact of iron fouling is more significant at the neutral pH than the elevated pH initially used in July and early August. Minimizing the ferric chloride dose would also likely assist in reducing overall UF fouling rate and maximization of UF system recovery. Other compounds identified as present on the membrane surface in much smaller quantities include calcium, manganese and sulfur. Visible inspection of the UF module noted the presence of an oily subsance and a petrochemical smell was detected. However, the membrane deposits were noted to be primarily inorganic in the membrane autopsy. The basal water was trucked directly from the basal wellheads for most of the pilot. Basal pond water use was explored in the pilot due to the presumed benefits of water equalization and water aging (introduction of oxygen into the water from the atmosphere). However, the presence of significant algae in the pond water was a dominant factor which ultimately resulted in an immediate negative impact on UF performance. Optimal operational settings for this unit process identified in the pilot are presented in Table E3. The typical cleaning pH levels recommended by DOW for the modules are 2 and 12 for inorganic and organic cleaning phases respectively. Exposing the membranes to extreme high and low pH levels over time contribute to membrane degradation and therefore should be minimized. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 6 of 80 Table E3. Optimal process settings for Ultrafiltration Parameter Optimal Setting Flux (normalized to 20˚C) = 53 lmh Recovery range = 70 to 80% based on pilot waste streams observed (improved recovery may be possible at full scale due to waste stream scalability) Operational flow mode = Cross-flow operation CEB sequence = Acid CEB – Caustic CEB – Acid CEB Acid CEB approximately 2.5 pH 5000 mg/L citric acid 200 mg/L sodium metabisulphite 30 min soak time Caustic CEB approximately 12 pH using caustic 600 mg/L NaOH 600 mg/L NaOCl 30 min soak time CEB frequency = Once every 24 hours at optimum operating conditions CIP sequence = Caustic CIP – Acid CIP - Caustic CIP Acid CIP ≤2.3 pH using citric acid, 200 mg/L sodium metabisulphite 38°C solution 10 hr soak/ recirculation period intermittent air scour Caustic CIP approximately 12 pH using caustic 2000 mg/L NaOCl 32°C solution 10 hr soak/ recirculation period intermittent air scour CIP frequency = Every 2 to 4 weeks Reverse Osmosis (RO) System The primary goal of the RO system was to reduce total dissolved solids (TDS), with a specific target for sodium. The pilot RO system consisted of a three stage design with fiberglass pressure vessels containing Polyamide Thin-Film Composite elements (DOW Filmtec SW30-4040). The anticipated challenge was running the RO system at a high recovery while at the same time managing fouling with standard cleaning methodologies and frequencies. Recoveries of 50% (pilot target) and 60% were examined during the study. At all times, the RO permeate was below the 1000 mg/L target for TDS and 500 mg/L target for sodium. At 50% recovery, permeate conductivity was reduced to 593 µS/cm, a 98.4% reduction relative to UF filtrate and untreated basal water. TDS was reduced to 304 mg/L on average with a standard deviation (SD) of 90 mg/L. Total sodium was reduced to an average of 123 mg/L with a standard deviation of 25 mg/L. Operation at CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 7 of 80 60% recovery was for a brief period, but saw similar rejections as was observed at 50% operation. Pilot data does not indicate irreversible fouling is occurring as full permeability recovery was achieved from the CIP and operational pressures remained relatively stable during regular operation. Iron was a significant foulant for the RO membranes and of all parameters examined in the CIP, had the highest levels relative to RO influent concentrations. The membrane autopsy identified iron and barium as the primary scalants present. Sulfur, phosphorous, and strontium were all present in the CIP solution at elevated concentrations as well, indicating some level of scaling on the RO membranes. Total Organic Carbon (TOC) deposit on the membrane accounted for 4.4% of the total fouling material by weight on the front RO element (where organic fouling tends to be most significant). Evidence of biological fouling was not observed in this pilot. Calcium carbonate was a significant scale-causing compound for the RO system due to the high calcium hardness and alkalinity in basal water. However, use of pH adjustment, and anti-scalant dosing during the pilot appeared to effectively manage the impact of hardness causing ions on the membrane. Optimal operational settings for this unit process identified in the pilot are presented in Table E4. Table E4. Optimal process settings for Reverse Osmosis Parameter Optimal Setting Sulphuric acid dose = 700 to 800 mg/L as H2SO4 (to achieve 6.5 pH in RO feed) Sodium metabisulphite dose = 160 to 200 mg/L (Dose was based on maintaining an RO feed ORP value of 100 to 150 mV as recommended by the equipment vendor. -Maintaining manganese in a reduced dissolved form was a key consideration in dosing metabisulphite as manganese in a dissolved and reduced state did not act as a significant RO foulant. Higher than industry standard Mn levels were often present in the RO feed so this was a significant consideration. Lower doses of metabisulphite may be possible. Anti-scalant dose (50% recovery) = 6.6 mg/L Anti-scalant dose (60% recovery) = 6.6 mg/L Biocide dose = 200 mg/L for 30 min, once per week (Nalco Permaclean PC-11) Time between CIPs = 1 to 2 months Flux rate (normalized to 25°C) = 23 lmh at 50% recovery CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 8 of 80 TABLE OF CONTENTS 1 Background _______________________________________________ 14 1.1. Project Overview _________________________________________________ 14 1.2 Project Objectives ________________________________________________ 15 1.3 Roles and Responsibilities _________________________________________ 15 2. Pilot Plant Design __________________________________________ 17 2.1 Design Basis Basal Water Quality ___________________________________ 17 2.2 Treatment Train Overview _________________________________________ 17 3 Experimental Plan __________________________________________ 21 3.1 Analytical Sampling Plan Overview __________________________________ 21 3.2 Analytical Methods and Considerations ______________________________ 24 4 Untreated Basal Water Quality ________________________________ 26 5. Treatment Performance _____________________________________ 28 5.1 Oxidation _______________________________________________________ 28 Bench Scale Testing ______________________________________________________29 Pilot Scale ______________________________________________________________34 5.2 Polymeric Ultrafiltration (PUF) ______________________________________ 35 Treatment Performance____________________________________________________40 Comparison of Pond and Well Water on UF Fouling _____________________________59 5.3 Reverse Osmosis (RO) ____________________________________________ 61 Operating Conditions ______________________________________________________61 Treatment Performance____________________________________________________67 Fouling Rate and Cleaning Effectiveness ______________________________________72 CIP Analysis ____________________________________________________________72 6. Summary and Conclusions __________________________________ 77 6.1 Treated Water Quality _____________________________________________ 77 6.2 Operational Experiences and Lessons Learned _______________________ 77 6.3 Optimal Operational Settings Observed in Pilot (by Unit Process) ________ 77 6.4 Primary Factors Impacting Process Performance ______________________ 79 6.5 Stability of Operation _____________________________________________ 79 6.6 Comparison of Operation with Pond and Wellhead Basal Water Sources ________________________________________________________ 80 6.7 Impact of Not Softening ___________________________________________ 80 CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 9 of 80 LIST OF APPENDICES APPENDIX A: APPENDIX B: APPENDIX C: APPENDIX D: APPENDIX E: APPENDIX F: APPENDIX G: APPENDIX H: Summary of Untreated Basal Water Quality Summary of Unit Process Effluent Water Quality Operational Settings Overview UF and RO CIP Procedures UF and RO Membrane Autopsy (Veolia) RO Concentrate Evaporator Testing (Veolia) Full Scale Equipment Sizing and Considerations (Veolia) Photos CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 10 of 80 LIST OF ACRONYMS BW CEB CIP CNRL CUF DBE DOC gfd gpm kPa lmh LSI MDL NAWS ND NDP NPF NSP NSR NTU ORP psi PUF PVDF RCW RO ROSA SCADA scfm SD SDI SDSI SP SU TDS TMP TOC TSS RO UF UPVC ZLD Backwash Chemically Enhanced Backwash Clean-In-Place Canadian Natural Resources Limited Ceramic Ultra-Filtration David Bromley Engineering Dissolved Organic Carbon gallons (US) per square foot per day gallons (US) per minute kilo pascal litres per square meter per hour Langelier Saturation Index Method Detection Limit North American Water Systems Non-Detectable Net Driving Pressure Normalized Permeate Flow Normalized Salt Passage Normalized Salt Rejection Nephelometric Turbidity Unit Oxidation-Reduction Potential pounds per square inch Polymeric Ultra-Filtration Polyvinylidene Fluoride Recycled Water Reverse Osmosis Reverse Osmosis System Analysis Supervisory Control and Data Acquisition standard cubic feet per minute Standard Deviation Silt Density Index Stiff & Davis Stability Index Sample Point Standard Units (pH) Total Dissolved Solids Trans-membrane Pressure Total Organic Carbon Total Suspended Solids Reverse Osmosis Ultra-Filtration Unplasticized Polyvinyl Chloride Zero Liquid Discharge CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 11 of 80 LIST OF FIGURES Figure 1. Photo of basal water treatment pilot facility on CNRL Horizon Site. _______ 14 Figure 2. Basal water treatment process train ________________________________ 17 Figure 3. Overview of the pilot timeline _____________________________________ 20 Figure 4. Manganese Solubility at various pH values and ORP (Pourbaix Diagram) ___ 29 Figure 5. Change in basal water pH and Oxidation-Reduction Potential (ORP) with aeration (fully aerated) and mixing observed in bench scale testing ______ 31 Figure 6. Overview of the impact of a high potassium permanganate dose on ORP with time for basal water taken from the wellhead _______________________ 32 Figure 7. Overview of dissolved manganese in basal water at various permanganate dosages observed in bench scale testing ____________________________ 33 Figure 8. Overview of UF recovery, flux and TMP increase rate during the pilot. _____ 42 Figure 9. Overview of UF recovery relative to water usage for membrane cleaning cycles during the pilot. _______________________________________________ 44 Figure 10. Overview of fouling rate development for the UF. ____________________ 46 Figure 11. Comparison of backwash effectiveness using UF filtrate, UF filtrate with 100 mg/L of sodium metabisulphite and RO permeate as source water _______ 51 Figure 12. Plot of TMP and normalized permeability at various influent pH settings __ 52 Figure 13. Solubility plot for ferric iron relative to pH __________________________ 53 Figure 14. Solubility plot for CaCO3 at various calcium and dissolved carbonic acid concentrations relative to pH_____________________________________ 54 Figure 15. Comparison of residual iron in untreated and UF filtrate water at various coagulant doses and pH ranges in the oxidation/precipitation stage ______ 55 Figure 16. TMP development rates for individual UF runs at different coagulant and permanganate doses ___________________________________________ 56 Figure 17. Plot of TMP and permeability for dead-end and cross-flow UF operation __ 58 Figure 18. Comparison overview of flux, run length, baseline TMP and TMP increase rate for piloting periods when pond water versus wellhead water were used as feed water for the pilot _________________________________________ 60 Figure 19. Simplified view of RO system configurations at 50% and 60% recovery. ___ 63 Figure 20. Overview of RO flux rate and normalized (to 25°C) flux rate over the course of the pilot _____________________________________________________ 64 Figure 21. Overview of normalized (to 25°C) RO flux rate broken down by stage over the course of the pilot _____________________________________________ 65 Figure 22. Overview of Normalized Salt Rejection (NSR) and Normalized Salt Passage (NSP) over the course of the pilot _________________________________ 68 Figure 23. NPF of the RO membrane overall and for each stage __________________ 75 CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 12 of 80 LIST OF TABLES Table 1. Overview of basal well water quality data used as the pilot design basis ____ 18 Table 2. Overview of operating targets for key process equipment _______________ 19 Table 3. Overview of sample point locations _________________________________ 21 Table 4. Overview of online instrumentation used in the pilot ___________________ 22 Table 5. Overview of initial on-site and external laboratory analytical sampling frequency ____________________________________________________________ 23 Table 6. Summary of analytical methods and detection limits (external laboratory) __ 25 Table 7. Summary of select water quality parameters for untreated basal water ____ 27 Table 8. Summary of UF system specifications and operating conditions ___________ 35 Table 9. Overview of a typical UF backwash sequence _________________________ 36 Table 10. Overview of a typical UF CEB _____________________________________ 36 Table 11. Overview of UF system related chemical usage and operational settings at optimal conditions _____________________________________________ 38 Table 12. Summary of select water quality parameters for UF permeate ___________ 41 Table 13. High level overview of chemical dosing zones during the pilot ___________ 42 Table 14. Overview of UF CIP cleaning solution analysis for key fouling compounds __ 48 Table 15. Overview of RO membrane specifications ___________________________ 61 Table 16. Overview of RO system operating conditions_________________________ 62 Table 17. Overview of RO system related chemical usage and operational settings at optimal conditions _____________________________________________ 66 Table 18. Summary of RO treatment performance (permeate water quality) at 50% recovery _____________________________________________________ 69 Table 19. Summary of RO treatment performance (permeate water quality) at 60% recovery _____________________________________________________ 70 Table 20. Summary of RO reject water quality characteristics at 50% recovery ______ 71 Table 21. Summary of RO reject water quality characteristics at 60% recovery ______ 71 Table 22. Overview of RO CIP cleaning solution analysis for key scaling compounds __ 73 CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 13 of 80 1 Background Canadian Natural Resources Ltd. initiated an Extraction Waters Pilot Study to determine the lowest cost option for an Integrated Water Management Plan. Source water for treatment included Basal Water and Recycled Water (RCW) from the Tailings Pond. The experimental phase of the pilot was started in April 2012 and is scheduled for completion in early 2013. EPCOR has been contracted to execute the pilot in concert with a CNRL project team, with support from equipment vendors. Lockerbie Stanley Inc. was contracted to carry out the construction and maintenance of the pilot facility. 1.1. Project Overview The Basal Water Treatment Pilot Facility was located on CNRL Horizon site, adjacent to 99a Pump House which is on the north side of the site, next to the tailings pond. Basal water was trucked directly from the wellhead main header into a 60 m 3 storage tank used as the plant influent water source. Figure 1. Photo of basal water treatment pilot facility on CNRL Horizon Site. The pilot study is divided into two phases based on source water type. Phase 1 involved the treatment of basal water. Phase 2 will involve the treatment of tailings pond recycle water. The following is a list of the major equipment: Phase 1 (Basal Water Treatment): Polymeric Ultrafiltration (UF) and Reverse Osmosis (RO) from North American Water Systems (NAWS - Veolia) Phase 2 (Tailings Water Treatment): Nanoflotation from David Bromley Engineering (DBE) Degasification, Multiflo Softening, Ceramic Ultrafiltration (CUF), Ion Exchange, Reverse Osmosis from Veolia Water Solutions (Veolia) This report is focused on the basal water treatment piloting phase of the project, which was carried out from June to October 8th, 2012. The main body of the report is focused on analysis of pilot scale process performance analysis and identification of optimal CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 14 of 80 operating conditions. Appendices in this report include summaries of water quality data and operational settings, details on membrane cleaning procedures, results of membrane autopsy (Veolia) and zero liquid discharge testing (Veolia) and details on scaling up the piloted treatment processes as identified by the equipment supplier (Veolia). Reports analyzing the piloting of tailings water treatment processes (as identified in Phase 2 above), will be prepared independently of this report, and will be available in early 2013. 1.2 Project Objectives The project treated water quality goal for the basal water treatment phase included effluent TDS < 1000 mg/L, Sodium < 500 mg/L and the maximum possible recovery for reuse. The project treated water quality goal for the tailings pond water treatment phase includes effluent TDS < 50 mg/L and Sodium < 30 mg/L. Piloting data was collected in order to permit scaling up of the pilot system to a commercial water treatment plant with a capacity to treat 3000 m3/hr of basal and tailings water. 1.3 CNRL Roles and Responsibilities Project initiator and primary stakeholder Overall project management and oversight Provision of power supply and basal water to pilot site Chair the Basal Water Treatment Technical Group which made all critical process related decisions during pilot experimentation EPCOR Lead and oversee all aspects of pilot facility operation Provide construction oversight and coordination Manage chemical procurement, inventory and storage for all processes Provide environmental and safety management for the project and all personnel on site Provision of certified operations staff for 24 hrs per day, 7 days per week pilot facility operation Plan and execute bench and pilot scale experimentation to optimize treatment processes Troubleshoot equipment and processes Setup and operation of an onsite analytical laboratory to provide rapid results to support operational setting changes and optimization Provide detailed logs of operations activity and equipment settings CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 15 of 80 Provide detailed data summary and analysis to present to the project technical group (CNRL, EPCOR & Veolia personnel) throughout the piloting phase Provide a basal water testing phase summary report detailing process performance at pilot and bench scale, summary of operational activities and recommended optimal process settings for use in full scale facility design LSI Design and construction of pilot infrastructure excluding process treatment trailers provided directly from equipment vendor (Veolia), office facilities and power supply Receive and install pilot treatment process trailers/skids and design/construct mechanical and electrical interconnections between equipment Provide electrical and mechanical support during commissioning and pilot operation Veolia Provision of primary process equipment for basal treatment pilot phase (oxidation reaction tanks, chemical dosing systems, polymeric ultrafiltration system and reverse osmosis system) Provide recommendations on chemical types and initial operational setting targets for the supplied process equipment Assist in process optimization Provision of remote and field technical support for Veolia supplied equipment Conduct autopsy on the used membranes at the end of pilot operation and provide results Conduct a zero liquid discharge (ZLD) study on RO reject from the pilot and report results Provision of a report detailing scaling up of pilot results to a full scale facility design CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 16 of 80 2. Pilot Plant Design 2.1 Design Basis Basal Water Quality The basal water treatment pilot system was designed according to historical basal water quality parameters provided by CNRL and are given in Table 1. In general, water quality observed during the pilot was similar to the design basis water quality data. However, notable variations that potentially impacted treatment system performance include suspended solids (TSS and turbidity) as well as pH. TSS was observed to average 23 mg/L, and reached as high as 430 mg/L which is significantly higher than the design basis number of 23 mg/L. The pH observed in the pilot averaged 7.0 which is notably different than the design basis value of 7.9. Observed basal water quality before treatment and at key locations throughout the treatment train are examined in depth in later sections of this report. 2.2 Treatment Train Overview Due to high TDS values in basal well water (Average TDS = 21,300 mg/L), low fouling potentials due to low organic carbon present and minimal silica present, a combination of polymeric UF, and Reverse Osmosis technologies was selected for this application. An oxidation step was included up front to precipitate out substances (iron, manganese and sulphides) that could foul the membranes. Water was trucked to site, directly from wellheads, and stored in a 60 m3 tank which was used to feed the pilot facility. Figure 2 illustrates the treatment train. Potassium Permanganate Sulphuric Acid (option) Metabisulphite & Anti-Scalant Ferric Chloride & Caustic (option) Basal Tank Reaction Tank Polymeric Ultra-Filtration (PUF) Reverse Osmosis (RO) Figure 2. Basal water treatment process train In the initial planning stages of system design, the treatment train included processes for degasification (alkalinity reduction) and softening (divalent metal ion reduction) upstream of the UF system. Significant consideration was given to the hardness levels in basal water and the advantages and disadvantages of softening the water before treatment by UF and RO membranes. It was decided to pilot basal water treatment without softening based on the projected high chemical usage requirements for removing hardness causing ions, and modeling results that suggested negative impacts on the RO could be managed using anti-scalant chemicals. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 17 of 80 Table 1. Overview of basal well water quality data used as the pilot design basis Compound Cations Calcium, mg/L Magnesium, mg/L Sodium, mg/L Potassium, mg/L Aluminum, mg/L Barium, mg/L Strontium, mg/L Ammonium, mg/L (cal.) Ferrous Iron, mg/L Ferric Iron, mg/L Manganese, mg/L Arsenic, mg/L Antimony, mg/L Beryllium, mg/L Cadmium, mg/L Chromium, mg/L Cobalt, mg/L Copper, mg/L Lead, mg/L Lithium, mg/L Mercury, mg/L Molybdenum, mg/L Nickel, mg/L Selenium, mg/L Silver, mg/L Thallium, mg/L Tin, mg/L Titanium, mg/L Vanadium, mg/L Uranium, mg/L Radium, mg/L Thorium, mg/L Zinc, mg/L Organics TOC, mg/L CBOD, mg/L COD, mg/L VOC, mg/L Semi-VOC, mg/L Naphthenic Acids, mg/L Conc. 222 303 10,000 78.4 < 0.15 0.32 19.2 Compound Anions Bicarbonates, mg/L Carbonates, mg/L Sulfates, mg/L Bisulfide, mg/L (cal) Bromide, mg/L Chloride, mg/L Phosphate, mg/L Nitrate, mg/L Fluoride, mg/L Other Constituents pH, standard units Temperature Range, °C Silica, mg/L Boron, mg/L Total Dissolved Solids, mg/L Conductivity, μS (est.) Total Alkalinity, mg/L as CaCO3 Carbon-dioxide, mg/L (cal.) Total Ammonia, mg/L as N Free Ammonia, mg/L a N (cal.) Total Sulfides, mg/L as S Hydrogen Sulfide, mg/L (cal) TSS, mg/L Total Residual Chlorine, mg/L Total Inorganic Nitrogen, mg/L Total Oil & Grease, mg/L Soluble Oil, mg/L (< 1μ) Emulsified Oil, mg/L (1 ~ 20μ) Free Oil, mg/L (> 20μ) Diesel Range Organics, mg/L Gasoline Range Organics, mg/L Total Hardness, mg/L as CaCO3 Benzene, mg/L Toluene, mg/L Ethyl Benzene, mg/L Xylenes, mg/L Methanol, mg/L n-Hexane, mg/L CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 Conc. 3,480 <5 20 14,000 <1 <1 7.9 5 (constant) 26,300 40,200 2,850 26 1,800 - May 29, 2013 18 of 80 The basal water was dosed with potassium permanganate to oxidize iron, sulphides and manganese. The water was then processed through the polymeric ultra-filtration membrane system operated in dead-end mode for the removal of solids to lower concentrations. Cross flow operation was tried briefly at the end of the piloting period to address limitations of dead-end UF operation. At the beginning of the study, when manganese was being targeted for removal, the feed to the Ultrafiltration (UF) system was pH adjusted from near neutral to approximately 7.6 using caustic soda. For the second half of the study, when manganese was being maintained in a reduced soluble state, the UF filtrate was pH adjusted from near neutral to approximately 6.5 using sulphuric acid and fed to the RO system. Anti-scalant was also added upstream of the RO system to address mineral scaling. The RO system was operated in a three stage, single pass configuration with a target recovery of 50%. Reverse Osmosis (RO) reject water from this study was shipped to Veolia laboratory in Plainfield, IL for an evaporation/crystallization study using Veolia technology. This will simulate ZLD conditions. Details of this testing are located in Appendix F. Table 2. Overview of operating targets for key process equipment System Target Polymeric Ultra-Filtration Filtrate Flow, m3/hr Filtrate Flux, lmh 4.1 ~ 51 to 85 Recovery, % 90 Single Pass, RO Feed Flow, m3/hr 3.5 3 Permeate Flow, m /hr 3 ~ 1.8 Reject Flow, m /hr ~ 1.8 Permeate Flux, lmh 13.5 Recovery, % 50 CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 19 of 80 Overall Basal Water Treatment Pilot Timeline 26-Jun: Start of 24/7 Pilot Operations 7-Jun: Power supplied to the Pilot 8-Oct: End of Basal water treatment Pilot Operation 15-Jun: Commissioning with Basal water 5 Jun, 2012 12 Jun, 2012 19 Jun, 2012 26 Jun, 2012 3 Jul, 2012 10 Jul, 2012 17 Jul, 2012 24 Jul, 2012 31 Jul, 2012 26 Jun - 12 Jul: Attempt to optimize pH adjustment and KMnO 4 dosing strategy based on ORP UF Operation Timeline 19 Jun, 2012 26 Jun, 2012 3 Jul, 2012 10 Jul, 2012 12-17 Jul: Pond Water Trials; Process units flushed at the end of trial 17 Jul, 2012 24 Jul, 2012 14 Aug, 2012 21 Aug, 2012 Change in Dosing Strategy: Operate at neutral pH to prevent CaCO 3 scaling, not targeting Mn removal 12-Jul: Mixing introduced in the influent water tank 17-Jun: UF system start-up 7 Aug, 2012 31 Jul, 2012 7 Aug, 2012 14 Aug, 2012 28 Aug, 2012 4 Sep, 2012 11 Sep, 2012 24-30 Sep: UF Feed pH 7.6-8.0 (with Caustic) KMnO 4 Dosage ~5 mg/L FeCl 3 Dosage ~3 mg/L 21 Aug, 2012 28 Aug, 2012 4 Sep, 2012 18 Sep, 2012 25 Sep, 2012 2 Oct, 2012 9 Oct, 2012 1-8 Oct: UF Feed pH ~7.0 (no Caustic) KMnO 4 Dosage ~1.5 mg/L FeCl 3 Dosage 0 mg/L 11 Sep, 2012 18 Sep, 2012 25 Sep, 2012 2 Oct, 2012 13-14 Sep: UF CIP 23 Jul - 13 Aug: UF Feed pH ~7.5 (with Caustic) KMnO4 Dosage 5 - 7 mg/L FeCl 3 Dosage ~7 mg/L 16 Aug - 24 Sep: UF Feed pH ~7.0 (no Caustic) KMnO 4 Dosage 1 - 1.5 mg/L FeCl 3 Dosage 1.5 - 7 mg/L 1-8 Oct: Cross-flow UF operation 2-8 Oct: New UF modules RO Operation Timeline 24 Jul, 2012 31 Jul, 2012 24-Jul: RO operation started at 16.5 gpm feed and ~20% recovery in 3×2×1 array 7 Aug, 2012 14 Aug, 2012 15-17 Aug: RO CIP 21 Aug, 2012 28 Aug, 2012 4 Sep, 2012 11 Sep, 2012 18 Aug - 8 Oct: RO Feed pH adjusted to ~6.5to prevent CaCO 3 scaling, also adding Na 2 S2 O 5 to keep Mn in reduced state 7 Aug: RO recovery increased to 50% 18 Sep, 2012 25 Sep, 2012 2 Oct, 2012 3-8 Oct: RO recovery increased to 60% in 2×1×1 array Figure 3. Overview of the pilot timeline CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 20 of 80 3 Experimental Plan 3.1 Analytical Sampling Plan Overview Consistent and representative sampling was one of the most important tasks performed by operations personnel during the pilot project at the Extraction Water Treatment Pilot Plant. Daily operator tasks included collecting and analyzing samples in the onsite lab, and entering data in the log sheets and electronic records. Sample point locations used in the study are outlined in Table 3. Table 3. Overview of sample point locations Sample Point 1. Untreated basal water 2. Reaction tank influent 3. UF influent 4. 5. UF filtrate RO influent 6. RO permeate 7. 8. RO reject UF backwash Description From the outlet of the influent storage tank After potassium permanganate and caustic soda (not always dosed) addition After ferric chloride addition Immediately after the membrane UF filtrate after passage through cartridge filters and addition of sulphuric acid and anti-scalant From the combined RO permeate line from all 3 RO stages From the RO reject waste stream Intermittent flow only during cleaning cycles A key aspect of this pilot study was the collection of a continuous data set of key process parameters through the use of online instrumentation. The online instruments were linked to the pilot plant SCADA (Supervisory Control and Data Acquisition) system which permitted instantaneous feedback to operations personnel. This data was also historized to assist in troubleshooting and data analysis. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 21 of 80 Table 4. Overview of online instrumentation used in the pilot Parameter pH Turbidity ORP Flow Water temperature Air temperature UF TMP Pressure Location Untreated basal water UF influent UF filtrate RO influent Untreated basal water UF influent UF filtrate Oxidation reaction tank (location varied during pilot based on operational requirements) – data not historized RO influent – data not historized Untreated basal water UF influent UF filtrate RO influent RO permeate RO reject o (Stages 1, 2 & 3) Untreated basal water All process buildings Surrounding the UF membrane RO influent RO permeate RO reject o (Stages 1, 2 & 3) The baseline analytical sampling plan used in the pilot study is summarized in Table 5. In addition to the baseline testing plan, analytical testing was carried out as the pilot progressed and experimental data requirements arose. Complete testing results are located in Appendix A and B. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 22 of 80 Table 5. Overview of initial on-site and external laboratory analytical sampling frequency Parameter Suspended Solids Total Suspended Solids Turbidity SDI Dissolved Solids Conductivity TDS General pH Alkalinity Calcium Hardness ORP Temperature Anions Sulfate Chloride Fluoride Phosphate Silica Total Sulfide Dissolved Sulfide Organics TOC DOC Total Oil & Grease Naphthenic Acids Cations Dissolved Iron Dissolved Manganese Total Aluminum Total Barium Total Boron Total Calcium Total Iron Total Magnesium Total Manganese Total Potassium Total Sodium Total Strontium Untreated Reaction Tank Infl. UF Infl. UF Filtrate UF Backwash RO Infl. RO Permeate RO Reject Ons i te Offs i te Ons i te Offs i te Ons i te Offs i te Ons i te Offs i te Ons i te Offs i te Ons i te Offs i te Ons i te Offs i te Ons i te Offs i te Frequency Frequency Frequency Frequency Frequency Frequency Frequency Frequency Frequency Frequency Frequency Frequency Frequency Frequency Frequency Frequency Daily Daily Weekly Weekly Daily Daily Weekly Weekly Daily Daily Weekly Weekly Daily Bi-daily Daily Weekly Daily Weekly Weekly Daily Weekly Weekly Weekly Daily Daily Daily Daily Daily Weekly Weekly Weekly Weekly Weekly Daily Weekly Daily Weekly Weekly Weekly Daily Weekly Weekly Bi-daily Weekly Weekly Weekly Daily Weekly Weekly Weekly Daily Weekly Weekly Daily Weekly Weekly Weekly Daily Weekly Weekly Weekly Daily Daily Daily Weekly Weekly Weekly Daily Daily Weekly Weekly Daily Weekly Daily Weekly Daily Weekly Weekly Weekly Daily Weekly Weekly Weekly Weekly Weekly Weekly Weekly Weekly Weekly Weekly Weekly 5 time /wk 6 time /wk Weekly Weekly Weekly Weekly Weekly Weekly Weekly Weekly Weekly Weekly Weekly Weekly Weekly Weekly Weekly 4 time /wk 4 time /wk 3 time /wk Weekly Weekly 3 time /wk Weekly Weekly Weekly Daily 3 time /wk 3 time /wk Weekly Weekly Weekly Weekly Weekly Weekly Weekly Weekly Weekly CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 23 of 80 3.2 Analytical Methods and Considerations Onsite testing included pH, temperature, Oxidation-Reduction Potential (ORP), Silt Density Index (SDI), turbidity, TSS, alkalinity, and conductivity. This testing was primarily intended to provide rapid feedback on process conditions in order to guide operational settings and adjustment. External lab results are primarily used in this report due to the higher level of accuracy possible from a full scale commercial lab. However, key on-site parameters are more relevant than external lab results due to the tendency for change/instability during sample transportation to and preparation at the external lab facility. For this reason, onsite test results for parameters such as pH, temperature, SDI and ORP were used as the primary data source. Detailed water quality results are provided in Appendix A, where onsite and external analytical results are clearly distinguished. External analytical testing was carried out by Maxxam Analytics in Calgary, Alberta. A summary of analytical methods and detection limits are provided in Table 6. In this report non-detectable analytical results are considered to equal 50% of the detection limit in order to carry out statistical analysis of results. Also of note, Method Detection Limits (MDL) occasionally varied based on dilutions carried out for a given sample. Typically MDLs were the same for all water types with the exception of RO permeate. The high salinity of basal water resulted in high MDLs for tests such as TOC. In low salinity water such as RO permeate, MDLs were at more typical levels. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 24 of 80 Table 6. Summary of analytical methods and detection limits (external laboratory) Analysis Alkalinity @25C (pp, total), CO3,HCO3,OH Biochemical Oxygen Demand BTEX/F1 in Water by HS GC/MS Cadmium - low level CCME – Dissolved Chlorine (Free) Chloramines, Residual Chlorine (Total) Chloride by Automated Colourimetry Chemical Oxygen Demand Total Coliforms and E.Coli Oxygen (Dissolved, winkler) Carbon (DOC) Conductivity @25C Fluoride CCME Hydrocarbons (F2-F4 in water) Hardness Mercury - Low Level (Total) Elements by ICP – Dissolved Elements by ICPMS – Dissolved Ion Balance Sum of cations, anions Nitrogen (total), Calc. TKN, NO3, NO2 Naphthenic Acids by IR Ammonia-N (Total) Nitrate and Nitrite Nitrate + Nitrite-N (calculated) Nitrogen, (Nitrite, Nitrate) by IC Oil and Grease by IR Polycyclic Aromatic Hydrocarbons pH @25°C (Alkalinity titrator) Orthophosphate by Konelab Sodium Adsorption Ratio Sulphate by Automated Colourimetry Cyanide (Total) Low level Total Dissolved Solids (Filt. Residue) Total Dissolved Solids (Calculated) Total Trihalomethanes Calculation Total Kjeldahl Nitrogen Carbon (Total Organic) Total Suspended Solids (NFR) Turbidity VOCs in Water by HS GC/MS (Std List) Lab SOP AB SOP-00005 AB SOP-00017 AB SOP-00039 AB SOP-00043 AB SOP-00032 CAL SOP 00045 AB SOP-00032 AB SOP-00020 CAL SOP-00042 CAL SOP-00013 CAL SOP-00053 CAL SOP-00077 AB SOP-00005 AB SOP-00005 CAL SOP-00086 AB WI-00065 CAL SOP-00007 AB SOP-00042 AB SOP-00043 AB WI-00065 AB WI-00065 AB WI-00065 CAL SOP-00085 AB SOP-00007 AB SOP-00023 AB SOP-00023 AB SOP-00023 CAL SOP-00096 AB SOP-00003 AB SOP-00005 AB SOP-00025 AB WI-00065 AB SOP-00018 CAL SOP-00073 CAL SOP-00074 AB WI-00065 CAL SOP-00104 AB SOP-00008 CAL SOP-00077 CAL SOP-00075 CAL SOP-00081 CAL SOP-00227 CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 Analytical Method SM 2320-B SM 5210 B CCME, EPA 8260C EPA 200.8 SM Method 4500-Cl G HACH 8167 SM Method 4500-Cl G EPA 325.2 SM5220D SM 9223 A,B SM 4500-O C MMCW 119 SM 2510-B SM 4500-F C EPA3510C/CCME PHCCWS SM 2340B EPA 1631 EPA 200.7 EPA 200.8 SM 1030E SM 1030E SM 4500-N A EPA 3510C/IR EPA 350.1 SM 4 1 1 0 B SM 4110-B SM 4110-B SM 5520C EPA 3510C/8270D SM 4500-H+B SM 4500-P SSMA 15.4.4 EPA 375.4 EPA 335.2 SM 2540-C SM 1030E EPA 8260 C EPA 351.1, 351.2 MMCW 119 SM 2540-D SM 2130B EPA 8260 C May 29, 2013 25 of 80 4 Untreated Basal Water Quality Basal water is typified by neutral pH (average 7.0; SD 0.1), low to moderate TSS (average 23.4 mg/L; SD 81.5mg/L) and high TDS (average 21,300; SD 3,457 mg/L).TDS is primarily composed of sodium (average 8,086 mg/L), chloride (average 12,458 mg/L), bicarbonate (average 3,638 mg/L as CaCO3) and hardness causing compounds (average 1,450 mg/L as CaCO3). Table 7 contains a summary of key water quality parameters for untreated basal water delivered to the pilot facility from the basal water wellheads. A more comprehensive summary of water quality parameters is provided in Appendix A. Organic compounds were at low concentration, with ability to measure low levels compromised by high detection limits resulting from the high salinity of the water. TOC was less than 13 mg/L for 88% of samples taken (average 6.9 mg/L; SD 2.8 mg/L). Oil and Grease (O&G) was consistently low (average 1.1 mg/L; SD 0.3 mg/L). However, these levels of organic compounds can theoretically contribute to RO membrane fouling. The compounds of most significance to this pilot had the potential to form scale on UF and RO membranes and subsequently reduce process performance. Of particular note were calcium, magnesium, manganese, iron, barium, strontium, boron, and silica. Prior to initiating the pilot study, untreated influent water quality and the RO system configuration were input into the modeling software ROSA (Reverse Osmosis System Analysis) in order to identify scaling compounds of most significant concern. The software predicts the concentration of common RO membrane scaling compounds in the RO reject for a given operational setting. If a given compound is near or in excess of its solubility limit in the RO reject (which is the feed water for the end of the final membrane element in the last stage), significant scaling is expected unless mitigative measures are taken. The most common mitigative measures include choosing an appropriate antiscalant chemical and dose as well as adjusting feed pH in order to increase compound solubility. Prior to piloting operation, compounds with the highest likelihood of causing scaling issues (without mitigation) identified were barium sulphate (BaSO4) and calcium fluoride (CaF2). Due to the high alkalinity and hardness present in untreated basal water, calcium carbonate (CaCO3) was also a concern. Compounds in a reduced state coming out of the well were unstable over the short term, but displayed relatively consistent results in aged samples. These included iron, manganese, and sulphides including hydrogen sulphide. These compounds have a tendency to precipitate out of solution as they are exposed to oxidizing compounds. It was important to control this reaction in order to ensure it was not occurring on the membrane surfaces. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 26 of 80 Table 7. Summary of select water quality parameters for untreated basal water Parameter Units pH (on-site lab) SU Total Suspended Solids mg/L Turbidity NTU Conductivity µS/cm Total Dissolved Solids mg/L Dissolved Chloride (Cl) mg/L Total Sulphide mg/L Dissolved Sulphate mg/L Alkalinity mg/L (Total as CaCO3) Bicarbonate (HCO3) mg/L Total Reactive Silica mg/L Hardness (CaCO3) mg/L Total Ammonia mg/L Total Organic Carbon mg/L Dissolved Organic Carbon mg/L Naphthenic Acids mg/L Oil and grease mg/L F1 (C6-C10) µg/L Hydrocarbons Total Aluminum (Al) mg/L Total Barium (Ba) mg/L Total Boron (B) mg/L Total Calcium (Ca) mg/L Total Iron (Fe) mg/L Total Magnesium (Mg) mg/L Total Manganese (Mn) mg/L Total Strontium (Sr) mg/L Dissolved Aluminum (Al) mg/L Dissolved Barium (Ba) mg/L Dissolved Boron (B) mg/L Dissolved Calcium (Ca) mg/L Dissolved Iron (Fe) mg/L Dissolved Magnesium (Mg) mg/L Dissolved Manganese (Mn) mg/L Dissolved Strontium (Sr) mg/L SD = ND = Average (ND= 50% MDL) 7.0 23 23 36,167 21,300 12,458 0.22 10.4 Min Max SD # of Obs. %ND MDL 6.6 1 8 34,000 11,503 12,000 <0.002 <1 7.4 430 110 37,000 23,000 13,000 4.6 34.0 0.1 81 20 637 3457 509 0.72 10.3 79 27 27 24 10 24 41 12 0 0% 0% 0% 0% 0% 20% 33% 0 2.5 0.1 1 10 100 0.002 1 2975 2,800 3,200 157 24 0% 5 3638 5.10 1,450 11.8 6.9 6.1 3.5 2.1 3,400 4.60 1,100 11.0 <13 <13 1.6 <2 3,900 7.78 1600 13.0 17.0 <13 5.1 5.3 193 0.64 102 0.8 2.8 1.2 1.2 1.4 24 24 24 10 16 11 11 12 0% 0% 0% 0% 88% 100% 0% 50% 5 0.05 0.5 0.5 13 13 1 2 316 <100 730 203 9 11% 100 0.2 2.3 5.0 188 2.0 233 0.27 13.3 0.045 2.3 4.9 189 1.2 235 0.27 13.1 0.039 2.2 4.8 160 1.1 210 0.16 12.0 <0.025 2.1 4.6 150 <0.6 210 0.21 12.0 0.380 2.5 5.3 210 3.3 260 0.70 14.0 0.110 2.6 5.3 210 3.1 260 0.37 14.0 0.167 0.2 0.2 16 0.5 22 0.07 1.0 0.040 0.2 0.2 12 0.7 14 0.03 0.8 4 4 4 16 42 4 52 4 14 14 14 26 41 16 42 14 0% 0% 0% 0% 0% 0% 0% 0% 36% 0% 0% 0% 22% 0% 0% 0% 0.025 0.1 0.2 3 0.6 2 0.04 0.2 0.025 0.1 0.2 3 0.6 2 0.04 0.2 standard deviation; analytical result below the MDL result; MDL = CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 method detection limit; May 29, 2013 27 of 80 5. Treatment Performance The primary water quality objectives for this treatment train were to reduce TDS to less than 1000 mg/L and sodium levels to less than 500 mg/L. Based on the use of RO membrane technology it was expected that these objectives would be met. However, another primary objective in piloting was to identify the maximum sustainable recovery rates and fouling characteristics for the UF and RO membranes as this impacts the sizing of the membrane systems and expected membrane module service life. Key considerations in evaluating this treatment train relate to the fouling rate characteristics and cleaning requirements for both the UF and RO membranes. Significant consideration was given to the hardness levels in basal water and the advantages and disadvantages of softening the water before treatment by UF and RO membranes. It was decided to pilot basal water treatment without softening based on the projected high chemical usage requirements for removing hardness causing ions, and modeling results that suggested negative impacts on the RO could be managed using anti-scalant chemicals. However, hardness related scaling on pilot equipment was determined to be an issue at the original treatment target pH of >7.5, but was manageable at the revised neutral pH used from August 16th to the end of the study in October. 5.1 Oxidation Basal water comes out of the ground in a reduced oxidative state due to the lack of oxygen underground. When the basal water is exposed to atmospheric oxygen, compounds such as dissolved iron, manganese and sulphides have a tendency to oxidize and potentially precipitate out of solution as a solid. It is important to control this precipitation in a membrane based treatment process, so that the solids do not precipitate out on the surface or inside of the membrane structure. If fouling of the membrane is excessive it can reduce the sustainable recovery rate of the system (due to additional backwashes and chemical cleanings) as well as reduce the membrane service life (if frequent high strength chemical cleanings are required). The goal of including an oxidation treatment step in the treatment train was to precipitate out sulfides, iron and manganese which had the potential to negatively impact fouling rates on the UF and RO membrane systems. Iron and sulphide compounds will tend to be oxidized before manganese compounds. Oxidation of manganese by dissolved oxygen at ambient conditions is a slow reaction that requires significant timespans. As can be clearly seen in Figure 4, for the Oxidation-Reduction Potential (ORP) values observed for untreated basal water (-0.5 v to -0.1 v) Mn tends to remain soluble as Mn2+ below a pH of 7.5, but theoretically will precipitate out of solution at pH values above this level. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 28 of 80 2.2 MnO4- (purple) pH range observed in pilot Figure 4. Manganese Solubility at various pH values and ORP (Pourbaix Diagram) Bench Scale A number of bench scale experiments were carried out over the course of the pilot by both EPCOR and Veolia technical staff, in order to optimize oxidation related chemical dosing. However, bench scale results did not always prove scalable to the pilot. Factors such as short circuiting, tank hydraulics, reaction times and potential complexation reactions have all been identified as possibly playing a role in variations between bench and pilot treatment results. Bench scale testing has identified several key requirements in designing a basal water treatment plant. Basal water taken from the well head is in a reduced state and as it is exposed to atmospheric oxygen, oxidation reactions slowly take place over several hours which result in increases in pH, reduction in sulphides (and H2S) and to some degree iron. Large rapid changes tend to occur over the first few hours after being taken CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 29 of 80 from the well head, afterwards changes are much more gradual but can continue over the course of the next one or two days. Several methodologies were examined in order to stabilize water quality changes in order to facilitate optimal dosing of oxidation chemicals (Figure 5). In this set of bench scale trials, basal water was subjected to three different oxidizing conditions and changes in pH and ORP were monitored with time. Replicates were carried out for all three conditions. As a control, one set of samples was stored in a covered container with no mixing (indicative of minimal oxidation due to exposure to atmospheric oxygen). The second condition was an open container with some mixing provided (indicative of exposure to atmospheric oxygen such as may be encountered in an open equalization pond or tank). The third condition was full aeration of the basal well water using air (indicative of maximum possible aeration achievable). Natural aging of the water does result in stability, but requires significant time-spans, and therefore also potentially requires large equalization storage volumes upstream of the treatment facility (see the “No Mixing, Covered 1 and 2” curves in Figure 5). Aeration of the water tends to speed up the natural aging process, but due to the slow kinetics involved in oxidizing some species in the water, some gradual changes in water quality still tend to occur over the long term (see Aerated curves in Figure 5). This bench scale testing occurred over a six hour timeframe, but slow gradual changes can be expected over the course of several days. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 30 of 80 9.5 9 No Mixing, Covered 1 pH 8.5 No Mixing, Covered 2 8 Aerated, Open 1 7.5 Aerated, Open 2 Mixing, Open 1 7 Mixing, Open 2 6.5 0 1 2 3 4 5 6 Time (hr) 300 250 200 ORP (mV) 150 No Mixing, Covered 1 100 No Mixing, Covered 2 50 Aerated, Open 1 0 -50 Aerated, Open 2 -100 Mixing, Open 1 -150 Mixing, Open 2 -200 0 1 2 3 4 5 6 Time (hr) Figure 5. Change in basal water pH and Oxidation-Reduction Potential (ORP) with aeration (fully aerated) and mixing observed in bench scale testing Chemical oxidation of the water using potassium permanganate was shown to have a rapid stabilization effect on basal water quality in the bench scale, but this result did not scale up at the pilot scale and therefore was not pursued (Figure 6). Addition of mixing in the feed tank was the primary mechanism used to stabilize influent ORP and pH at the pilot scale as opposed to relying on the effects of permanganate dosing. Potassium permanganate was dosed at the pilot scale to provide oxidation, but stabilization of ORP and pH was not an objective due to the limitations stated above. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 31 of 80 500 400 300 ORP (mV) 200 16 mg/L KMnO4 100 0 -100 -200 0 2 4 6 8 10 12 14 16 18 20 22 24 26 28 30 Time (minutes) Figure 6. Overview of the impact of a high potassium permanganate dose on ORP with time for basal water taken from the wellhead Based on pilot results, provision of aeration and some equalization of fresh basal water provide sufficient stability to dose the required treatment chemicals upstream of the UF treatment process. However, optimal chemical dosing is important in order to manage fouling rates of the UF membranes. Equalization time of basal water varied significantly throughout the pilot due to the feed water being trucked from the mine and stored in a 60 m3 feed tank at the pilot site. Trucking fill/unload times, delivery times and consumption rates at the pilot all impacted the equalization time for the water entering the treatment plant. Appendix G contains a report detailing full scale equipment sizing that addresses recommended equalization time for a full scale facility. Permanganate dose was optimized through a combination of bench scale and pilot scale experimentation. Figure 7 displays the impact of pH and permanganate dose on dissolved manganese concentration in the oxidized basal water. As predicted using the Pourbaix diagram (Figure 4), elevated pH provides the lowest residual concentration, while lower pH results in the highest residual. Use of an alternative oxidizing chemical such as sodium hypochlorite could resolve the potential for elevated dissolved manganese subsequent to oxidation/precipitation due to non-optimal permanganate dosing and complexation issues. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 32 of 80 pH 7.2 pH 7.6 pH 8.0 Raw 0.25 Total Mn (mg/L) 0.20 0.15 0.10 0.05 0.00 0 1 2 3 4 5 6 Permanganate Dosage (mg/L) Figure 7. Overview of dissolved manganese in basal water at various permanganate dosages observed in bench scale testing CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 33 of 80 7 Pilot Scale Manganese removal did not scale up well from bench scale testing, as dissolved manganese levels in UF filtrate were frequently higher than what was observed at bench scale. It is likely that other compounds were complexing with manganese, keeping it in dissolved form, despite being in the zone of the Pourbaix diagram (Figure 4) where precipitation should have occurred. Bench scale work identified a strong relationship between ORP and permanganate dosing required for precipitating out iron, sulphides and manganese. However, ORP proved to be an impractical parameter to base chemical dosing on due to the tendency for compounds in the water to rapidly foul ORP probes (often within an hour), such that reliable online readings were not possible. The rapid change and stabilization of ORP subsequent to permanganate addition did not scale up from bench to pilot scale as detailed in the previous section. The chemical dosing strategy was changed on August 16th, after extensive attempts to achieve reliable manganese removal were unsuccessful. This involved stopping pH adjustment upstream of the UF and adding permanganate at a fixed dose in order to precipitate iron and sulphides, while attempting to keep manganese in dissolved form. The fixed permanganate dose was notably lower as only sufficient oxidation was required to address iron and sulphide precipitation. The dosing strategy was modified for several additional reasons. Firstly, the elevated manganese levels observed in the UF filtrate did not show measureable negative impact on downstream RO operation. Secondly, operation at the high pH, theoretically required for manganese precipitation, resulted in excessive calcium carbonate scaling on pilot plant equipment and potentially the UF and RO membranes. Operation at neutral pH also resulted in a significant reduction in volume of caustic required for upstream pH adjustment and therefore significant savings for ongoing chemical operating costs. The optimal operational settings for the Oxidation treatment step are as follows: Potassium permanganate = 1 to 1.5 mg/L Ferric chloride = 0 to 2 mg/L as Fe Sodium Hydroxide = 0 mg/L Equalization (with mixing and exposure to the atmosphere) of water upstream of the oxidation system in order to stabilize ORP and pH CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 34 of 80 5.2 Polymeric Ultrafiltration (PUF) Hollow fibre PVDF membranes (DOW SFD 2860) were used as the sole solids removal mechanism in the treatment train. As expected, suspended solids (gauged by turbidity and TSS) were consistently low in UF filtrate, regardless of influent solids or chemical dosing upstream. A significant portion of the pilot was used to identify optimal operating conditions and upstream chemical dosing in order to maximize water production while attempting to maintain fouling rates at practically manageable levels. Operating Conditions The UF system used during the pilot consisted of a single membrane module. Detailed specifications and operational settings for the system are provided in Table 8. Flux rates are normalized to 20°C as recommended by the manufacturer in order to permit comparison of operational results as water temperature varied. Table 8. Summary of UF system specifications and operating conditions Parameter Membrane type Membrane model Membrane surface area per module Number of modules operated Rated filtration flux at 25°C Rated filtration flux at 20°C Chemical resistance - Operating pH range - NaOCl maximum concentration Temperature range (UPVC limited) Maximum feed pressure at 20°C Maximum operating TMP Nominal pore diameter External fiber diameter Internal fiber diameter Module diameter Module length Operating flow in pilot Feed flux rate in pilot Feed flux rate in pilot (normalized to 20°C) CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 Details PVDF Hollow Fiber Outside - In DOW SFD 2860 module 51 m2 1 40 to 120 lmh 35 to 105 lmh pH: 2 – 11 2000 mg/L 1 to 40°C 625 kPa (93.75 psi) 210 kPa (30 psi) 0.03 µm 1.3 mm 0.7 mm 225 mm 1500 mm 1.5 to 4.2 m3/hr 28 to 80 lmh 28 to 105 lmh May 29, 2013 35 of 80 The strategy for managing fouling of the membrane was primarily through a combination of frequent physical backwashes combined with the use of Chemically Enhanced Backwashes (CEBs) at regular intervals. Triggers for initiating a CEB included a Trans Membrane Pressure (TMP) increase to maximums of approximately 97 to 159 kPa (14 to 23 psi) (target varied as the pilot progressed), a permeability drop of more than 15% or time between CEBs. The fouling management philosophy used during the pilot was to carry out frequent small duration CEBs before excessive fouling occurred and became difficult to restore performance to baseline levels. CEBs were initiated based on a maximum time interval of 24 hrs (though fouling rates and not time interval generally governed CEB frequency during the pilot) if neither TMP nor permeability thresholds were reached. A summary of a typical UF backwash sequence and UF CEB sequence are provided in Table 9 and Table 10 respectively. Table 9. Overview of a typical UF backwash sequence Step 1 Time (s) Flux (lmh) 5 --- Stand by 3 2 Air Scour #1 – 5 m /hr (3 scfm) 10 --- 3 4 5 Standby 3 Air Scour #2 – 5 m /hr (3 scfm) Drain 5 10 60 ----150 6 BW top + air 45 60 7 BW bottom 45 150 8 BW rinse 0 0 Time (s) Flux (lmh) Table 10. Overview of a typical UF CEB Step 1 Stand by 30 --- 2 Air Scour #1 – 5 m /hr (3 scfm) 0 --- 3 Standby 0 --- 3 3 4 Air Scour #2 – 5 m /hr (3 scfm) 0 --- 5 Drain 5 100 6 BW Bottom 15 100 7 Dosage Bottom 90 100 8 Dosage Top 90 100 Soak BW rinse 900 180 0 100 9 10 CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 36 of 80 Chemically Enhanced Backwashes (CEBs) were experimented with significantly during the course of the pilot in order to optimize the fouling rate control of the system. Parameters experimented with in order to optimize CEB sequences include the following: # of acid and caustic CEBs executed in a sequence # of physical backwashes (BW) in a CEB sequence Order of executing CEB types and BWs Use of RO permeate instead of UF filtrate (to gauge negative impact of dissolved metals in UF permeate) Addition of hypochlorite to BW water (enhanced organics removal) Addition of sodium metabisulphite to BW water (enhanced manganese removal) Production cycle length Maximum permissible TMP Chemical Usage and Operational Settings at Optimal Conditions Table 11 provides a summary of the chemical dosing and operational settings recommended for UF system operation at optimal settings. A brief summary of the reasoning for each setting is also provided, with the detailed analysis contained in the following sections of this report. It should be noted when interpreting these recommendations, that the standard cleaning methodology identified by the membrane manufacturer is use of acid CEBs at a pH of 2 (using HCl, H2SO4, citric or oxalic acid), and caustic CEBs at a pH of 12 (using NaOH). Membrane exposure to extreme high or low pH levels should be minimized as these conditions contribute to gradual degradation of the membrane surface which ultimately impacts the service life of the membrane module. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 37 of 80 Table 11. Overview of UF system related chemical usage and operational settings at optimal conditions Parameter Potassium permanganate Ferric chloride Optimal Setting = 1 to 1.5 mg/L Reasoning -Targets iron and sulfide precipitation, but not Mn = 0 to 2 mg/L as Fe Sodium Hydroxide = 0 mg/L Flux (normalized to 20˚C) Recovery range = 53 lmh Operational flow mode = Cross-flow operation -Low dose if/as required to potentially increase particle size and rejection by the UF, but not too high in order to avoid contributing to UF scaling -Operation at neutral pH significantly reduces chemical consumption due to pH adjustment. -The primary goal of operating at elevated pH was Mn precipitation, which is not an objective at the optimum conditions identified in this pilot. Mn in a dissolved reduced state was shown to not be a significant RO scalant. -Operation at elevated pH resulted in severe CaCO3 scaling throughout the pilot facility. Impact of full scale equalization on pH must be considered in full scale design -Based on TMP development rate and observed time required between CEBs -Based on pilot waste streams observed (improved recovery may be possible at full scale due to waste stream scalability) -Based on TSS levels observed -Provides physical scouring of the membrane surface which reduces membrane fouling and a mechanism to deal with elevated TSS levels occasionally experienced. = 70 to 80% CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 38 of 80 Table 11 (con’t) Parameter CEB sequence - Acid CEB - Caustic CEB CEB frequency CIP sequence - Acid CIP - Caustic CIP CIP frequency Optimal Setting = Acid CEB – Caustic CEB – Acid CEB approximately 2.5 pH 5000 mg/L citric acid 200 mg/L sodium metabisulphite 30 min soak time approximately 12 pH 600 mg/L NaOH 600 mg/L NaOCl 30 min soak time = once every 24 hours at optimum operating conditions = Caustic CIP – Acid CIP - Caustic CIP ≤2.3 pH using citric acid, 200 mg/L sodium metabisulphite 38°C solution 10 hr soak/ recirculation period intermittent air scour approximately 12 pH using caustic 2000 mg/L NaOCl 32°C solution 10 hr soak/ recirculation period intermittent air scour = every 2 to 4 weeks CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 Reasoning -Based on observed performance in pilot -Based on observed performance in pilot -Based on observed performance in pilot -Based on observed performance in pilot May 29, 2013 39 of 80 Treatment Performance A summary of select water quality parameters for UF permeate is provided in Table 12. A complete listing of water quality parameters examined is located in Appendix B, while detailed plots of online instrumentation data is locate in Appendix C. As shown in Table 12, solids removal was consistently good, with effluent turbidity averaging 2.0 NTU and Silt Density Index (SDI) averaging 0.9 over the course of the pilot (well water source). RO feed requires an SDI of less than 5 at a minimum and ideally less than 3. UF filtrate concentrations of iron and sulphides were consistently low enough to achieve targets based on the perceived ability of anti-scalant chemicals to manage fouling on the downstream RO membranes. Subsequent analysis of RO fouling compounds did indicate iron was a major foulant for the RO system. The RO system is discussed in detail in a later section of this report. Iron residual concentration in the UF filtrate appeared to be lowest during the initial chemical dosing regimen with high pH (≥7.4) in the oxidation/precipitation phase. Manganese removal did not scale up from bench to pilot scale testing. Typical manganese water quality targets upstream of an RO system are a maximum of 0.1 mg/L and preferably less than 0.05 mg/L. These levels were not consistently met with the UF system as a number of factors resulted in high concentrations of manganese remaining in dissolved form and passing through the UF membrane. These factors included oxidation chamber influent water quality fluctuations in ORP and pH over short timeframes, complexation with compounds in the water resulting in elevated dissolved manganese levels, potential short circuiting of tanks, and other flow related effects. High levels of organics can be a significant factor in UF and RO membrane fouling, but this did not appear to be a factor in this pilot. Organic compounds in untreated basal water were consistently at low levels. Due to the high salinity of the water the method detection limit for TOC and DOC ranged from 10 to 13 mg/L, and the majority of tests on both untreated basal and UF filtrate were below detection. Oil and grease was also typically of low concentration in basal water (average 2.1 mg/L), with an average reduction of 48.9% after treatment by the UF. Naphthenic acids averaged 3.5 mg/L in untreated basal water and displayed no reduction due to treatment by the UF unit. The membrane autopsy indicated membrane deposits were primarily inorganic. Overview of Dosing Strategy The chemical dosing strategy was primarily governed by and modified based on UF filtrate quality and desired RO influent water quality (and to a lesser extent UF operational performance). The piloting period can be broken down into nine operational zones as presented in Figure 8. The primary operational and chemical dosing aspects of each zone and accompanied advantages and disadvantages are provided at a high level in Table 13. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 40 of 80 Table 12. Summary of select water quality parameters for UF permeate Parameter Average Units (ND= 50% MDL) SU pH (on-site) NTU Turbidity (on-site) SDI (on-site) Total Suspended Solids mg/L NTU Turbidity µS/cm Conductivity mg/L Dissolved Chloride (Cl) Total Sulphide mg/L Dissolved Sulphate (SO4) mg/L Alkalinity (Total as mg/L CaCO3) mg/L Bicarbonate (HCO3) Total Organic Carbon mg/L (C) mg/L Oil and grease mg/L Total Aluminum (Al) mg/L Total Barium (Ba) mg/L Total Boron (B) mg/L Total Calcium (Ca) mg/L Total Iron (Fe) mg/L Total Magnesium (Mg) mg/L Total Manganese (Mn) mg/L Total Strontium (Sr) Dissolved Aluminum (Al) mg/L mg/L Dissolved Barium (Ba) mg/L Dissolved Boron (B) mg/L Dissolved Calcium (Ca) mg/L Dissolved Iron (Fe) Dissolved Magnesium mg/L (Mg) Dissolved Manganese mg/L (Mn) Dissolved Strontium (Sr) mg/L 7.2 2.0 0.9 0.6 1.5 36,500 12,500 0.001 358 Min Max 6.9 8.0 0.1 38.6 0.2 3.2 <1.0 1.0 <0.1 9.0 36,000 37,000 12,000 13,000 <0.002 0.006 <1 5,000 SD Count %ND MDL % Reduction (from Raw) 0.3 4.9 0.8 0.2 2.5 707 707 0.001 1,336 16 80 33 13 27 2 2 42 14 85% 4% 0% 0% 81% 93% 1.0 0.1 1 100 0.002 1 97.5% 93.5% <1% <1% 99.4% <1% 2864 2,800 3,200 122 14 0% 5 <1% 3500 3,400 3,900 162 14 0% 5 <1% 6.7 <13 14.0 1.5 27 96% 13 3.0% 1.1 0.047 2.4 5.1 200 0.4 250 0.44 13.5 0.025 2.5 5.3 205 0.7 <2 <0.025 2.4 5.0 200 <0.6 250 <0.04 13.0 <0.025 2.4 5.3 200 <0.6 2.1 0.081 2.4 5.2 200 1.7 250 1.10 14.0 0.038 2.5 5.3 210 1.7 0.3 0.048 0.0 0.1 0 0.4 0 0.31 0.7 0.018 0.1 0.0 7 0.6 14 2 2 2 2 45 2 55 2 2 2 2 2 5 93% 50% 0% 0% 0% 60% 0% 2% 0% 50% 0% 0% 0% 40% 2 0.025 0.1 0.2 3 0.6 2 0.04 0.2 0.025 0.1 0.2 3 0.6 48.9% 74.9% <1% <1% <1% 77.6% <1% <1% <1% 44.5% <1% <1% <1% 40.1% 255 250 260 7 2 0% 2 <1% 0.41 0.10 0.78 0.33 5 0% 0.04 <1% 14.0 14.0 14.0 0.0 2 0% 0.2 99.8% CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 41 of 80 Table 13. High level overview of chemical dosing zones during the pilot Operational Settings Wellhead water source Pond water source Elevated pH in oxidation zone Neutral pH in oxidation zone Flux range (Low/Moderate/High) Dead end operation Cross flow operation Mn targeted for precipitation New membrane modules (burn in period) Advantages Low chemical usage Stable influent ORP & pH Physical scouring of membrane surface Disadvantages CaCO3 scaling throughout pilot facilities CEBs not sufficient to restore baseline TMP Elevated Mn residuals in UF filtrate Elevated Fe residuals in UF filtrate Not relevant to scaling up UF design A X X B X X C X D X Zone E X X H X X M X X L X L X H X X X X X F X G X X X M X L X X X H X I X X L X M X X X X X X X X X X X X X X X X X X X X X X X X X X X Figure 8. Overview of UF recovery, flux and TMP increase rate during the pilot. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 42 of 80 UF Recovery Water recovery for the UF system was purely a function of the proportion of treated water used for membrane cleaning cycles (backwashes and CEBs). The inverse relationship of UF recovery to total water used for cleaning cycles is visible in Figure 9. During production cycles there is no waste stream, such that 100% of water fed to the system passed through the membrane and becomes UF filtrate. In the UF system the primary operational variables that can be used to impact recovery are: backwash frequency; chemically enhanced backwash (CEB) frequency; clean-in-place (CIP) frequency; Water usage during a single cleaning cycle (BW, CEB, CIP); flux; and optimization of upstream chemistry to target UF membrane fouling reduction. In this pilot the severity of fouling on the UF membrane (as gauged by TMP increase rate) had a major impact on the UF recovery rate, due to the treated water requirements for cleaning cycles. Recovery for the UF varied significantly during the couse of the pilot as is visible in Figure 8. Recovery is calculated as a balance between the water treated by the UF system, minus the treated water used for backwashes and chemically enhanced backwashes (CEBs). Clean in Place (CIP) chemical cleaning events were not considered in the calculations used in this report. From late August onwards there was a significant increase in the volume of water used per day for both backwashes and CEBs in response to increased fouling on the membrane. The increased fouling was due to increased flux rates (and therefore volume of water treated per day) as well as the chemistry of the water contacting the UF membrane. Initially UF recovery was lower (typically in the 60 to 70% range) as upstream chemical process optimization was the focus. Recovery was gradually increased to 80% and to as high as 89% in late August. Significant issues related to scaling on the UF membrane were encountered at the end of August and persisted through much of September. Experimentation with a variety of cleaning methodologies during this period was responsible for the rapid reduction/variation in recovery. It is likely that relative water volumes for cleanings could be reduced in a full scale facility relative to the pilot. Inherent facility design issues unique to the pilot (e.g. length of pipe runs, sizing of pipes and vessel volumes) likely increase the total volume of clean water used during this study relative to a full-scale facility. However, it is clear that frequency and type of cleanings used for the UF have a significant and notable impact on system recovery. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 43 of 80 Figure 9. Overview of UF recovery relative to water usage for membrane cleaning cycles during the pilot. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 44 of 80 Fouling Rate Development and Cleaning Effectiveness Ideally, execution of a CEB sequence would provide complete removal of fouling material and initial membrane TMP would return to baseline levels. At the beginning of the pilot, the CEB sequence and frequency were effective in maintaining TMP within a manageable range. However, in late August, CEBs were not restoring TMP and permeability to baseline values despite significant effort in modifications to CEBs, including sequence order, chemical strength, duration, frequency and use of accompanied backwashes (Figure 10). For reference, plots of UF TMP throughout the entire piloting period are located in Appendix C. The overall fouling characteristic of the UF membrane during the pilot is depicted in Figure 8 and Figure 10. The TMP increase rate indicates the increase in TMP per unit time during a run and the Baseline TMP indicates the TMP level at which a run is started right after a CEB has been completed. A complete run is defined as the period of UF operation in between two CEBs and is referenced in Figure 10 as “Time Between CEBs”. In order to remove foulants not addressed by the CEBs, a CIP was conducted on September 13 to 14, which was effective in restoring membrane TMP and permeability to baseline values. However issues reappeared in less than a week of operation. At this point, rapid TMP development was occurring and CEBs were required on a frequency (approximately every 3 hours) that had negative implications for recovery as well as practical operational factors. In general, CIPs are more effective than CEBs at removing fouling material and restoring permeability. This is due to the use of higher cleaning chemical concentrations in combination with prolonged soaking periods, where the cleaning solution is in contact with the membrane surface. However, CIPs negatively impact the service life of a membrane more than CEBs due to the combination of higher strength chemical solutions and contact time. As previously mentioned, the number of CIPs carried out should be minimized. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 45 of 80 Baseline TMP (psi) Time Between CEBs (Hrs) TMP Increase Rate (psi/day) Flux Corrected to 20°C (lmh) 140 120 Pond Pond Water Water Trial Trial Flushing system of pond organics pH 7.4-7.6 pH 7.6-8.0 100 Crossflow pH 6.8-7.0 pH 6.8-7.0 80 Major change in dosing strategy CIP 60 New modules 40 20 0 20-Jun 30-Jun 10-Jul 20-Jul 30-Jul 09-Aug 19-Aug 29-Aug 08-Sep 18-Sep 28-Sep 08-Oct 18-Oct Figure 10. Overview of fouling rate development for the UF. CIP Solution Analysis and Membrane Autopsy Overview The autopsy conducted on the UF membrane (Appendix E) used during the pilot indicated deposits were mainly inorganic, with iron and chloride being the main elements present. Low levels of sulphur, calcium and manganese were also detected, but at significantly lower levels that iron and sodium. A brown orange deposit on the UF strands was noted to have penetrated deep into the membrane structure, not just on the membrane surface. The cleaning solutions used during the CIP were sampled and sent for analysis in order to isolate key compounds that were present on the membrane surface and contributing to reduced performance (Table 14). The CIP consisted of multiple steps designed to remove typical organic foulants and mineral scalants. High pH cycles are typically effective in removing organic material, while low pH cycles target removal of mineral scalants. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 46 of 80 The detailed procedure used for CIPs is located in Appendix D. An abbreviated summary of the CIP cycle is as follows: 2 hr recirculation (#1) with cleaning solution at 40 lmh o Sample solution 6 hr soak in cleaning solution 2 hr recirculation (#2) at 40 lmh o Sample permeate and concentrate solution Drain cleaning solution Rinse with potable water until neutral pH at 20 lmh o Sample solution Organic compounds were not found in significant concentrations in the high pH CIP solution, which targeted removal of organic foulants on the membrane. Additionally, untreated basal water TOC concentrations were consistently below detection limits (though detection limits were 13 mg/L due to high water salinity). These two factors suggest organic fouling is not the governing issue in UF performance. However, it should be noted that even the low levels of TOC and O&G observed can result in membrane fouling. The maximum O&G concentration specified by the manufacturer for the UF membranes is 2 mg/L. Though 93% of analytical results were reported to be < 2mg/L, several results were marginally above this limit (Table 12). Fouling on the UF membrane was correlated to upstream chemical dosing. Iron was present in the most significant concentration in the low pH CIP solution, which targeted mineral scale removal from the membrane. Subsequent investigation into the impact of lower coagulant dosing suggests that dosing of ferric chloride coagulant immediately upstream of the UF membrane was a significant contributor to rapid membrane fouling rates observed. Coagulant dose across the various chemical dosing strategies is examined in greater depth in a later section of this report. The elevated TOC present in the low pH CIP solution is due to the use of citric acid to lower the pH and does not indicate organics removal from the membrane. Organics tend to precipitate out of solution at low pH. In addition to iron, there was also elevated barium, calcium, strontium, sulfur and zinc in the low pH CIP cleaning solutions. Minimal organic material was observed in the high pH CIP solution. This suggests mineral scaling and not organic fouling is the primary source of reduced performance instigating the CIP. In the membrane autopsy, iron was the dominant metal deposit by a wide margin. Ferric chloride was selected as the coagulant for this application due to its proven use in similar treatment scenarios and effectiveness over a wide pH range. However, iron and chloride were the most significant deposits on the UF membrane, indicating the coagulant significantly contributed to membrane fouling. This is backed up by both the CIP solution analysis and membrane autopsy data. It is likely possible to reduce the impact of iron fouling by the ferric chloride dose used in the application in combination with the use of CIP chemicals specifically targeting the iron deposits. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 47 of 80 Table 14. Overview of UF CIP cleaning solution analysis for key fouling compounds Parameter pH Acid CIP Recirc#1 Solution Acid CIP Recirc#2 Conc. Units UF Effl. SU 7.2 2.21 9000 b a 2.36 a Acid CIP Recirc#2 Filtrate Acid CIP BW Flush Caustic CIP Conc Caustic CIP Filtrate MDL 2.61 6.15 12.1 12.1 0 7700 a Total Organic Carbon (C) mg/L <13 7700 120 38 30 13 Carbonate (CO3) mg/L <0.5 Dissolved Sulphate (SO4) mg/L 358 <0.5 130 <0.5 120 <0.5 170 <0.5 42 1300 100 1300 <1 0.5 1 Total Aluminum (Al) mg/L 0.046 0.9 6.7 2.7 1.7 4.1 4 0.025 Total Antimony (Sb) mg/L <0.015 <0.015 <0.015 0.002 <0.015 <0.015 <0.015 0.015 Total Arsenic (As) mg/L <0.005 0.0021 0.0045 0.012 0.0048 0.0016 0.0016 0.005 Total Barium (Ba) mg/L 2.4 1.5 1.5 2.3 0.77 0.14 0.16 0.1 Total Beryllium (Be) mg/L <0.025 <0.025 <0.025 <0.025 <0.025 <0.025 <0.025 0.025 Total Boron (B) mg/L 5.1 <0.2 <0.2 <0.2 <0.2 <0.2 <0.2 0.2 Total Cadmium (Cd) ug/L <0.13 1 1.6 2.6 1.1 0.32 0.25 0.13 Total Calcium (Ca) mg/L 200 110 200 220 57 28 27 3 Total Chromium (Cr) mg/L <0.025 0.022 0.063 0.11 0.032 0.013 0.0082 0.025 Total Cobalt (Co) mg/L <0.0075 0.0012 0.0036 0.0088 0.0022 <0.0075 <0.0075 0.0075 Total Copper (Cu) mg/L 0.0025 0.032 0.061 0.3 0.14 0.017 0.015 0.005 Total Iron (Fe) mg/L <0.6 39 80 230 38 3 0.69 0.6 Total Lead (Pb) mg/L <0.005 0.016 0.033 0.091 0.023 0.0021 0.0014 0.005 Total Lithium (Li) mg/L 2.2 <0.2 <0.2 <0.2 <0.2 <0.2 <0.2 0.2 Total Magnesium (Mg) mg/L 250 12 25 17 15 <2 2.3 2 Total Manganese (Mn) mg/L 0.44 0.84 2.6 3.8 2.5 0.054 <0.04 0.04 Total Molybdenum (Mo) mg/L <0.005 0.0012 0.0028 0.0082 0.0026 0.0032 0.0029 0.005 Total Nickel (Ni) mg/L 0.014 0.0069 0.021 0.072 0.016 <0.013 <0.013 0.013 Total Phosphorus (P) mg/L <1 <1 <1 2.4 1.4 <1 <1 1 Total Potassium (K) mg/L 66 <3 <3 <3 <3 7.6 8.6 3 Total Selenium (Se) mg/L <0.005 <0.005 <0.005 <0.005 <0.005 <0.005 <0.005 0.005 Total Silicon (Si) mg/L 2.5 2.4 3 4.1 3.3 1.5 1.7 1 Total Silver (Ag) mg/L <0.0025 <0.0025 <0.0025 0.0013 0.0004 <0.0025 <0.0025 0.0025 Total Sodium (Na) mg/L 7600 100 120 190 170 2000 2300 25 Total Strontium (Sr) mg/L 13.5 3.6 7.9 9.3 1.1 0.36 0.26 0.2 Total Sulphur (S) mg/L 4.4 66 53 58 11 11 10 2 Total Thallium (Tl) mg/L <0.005 <0.005 <0.005 0.0009 <0.005 <0.005 <0.005 0.005 Total Tin (Sn) mg/L <0.025 <0.025 0.0078 0.02 0.0037 <0.025 <0.025 0.025 Total Titanium (Ti) mg/L <0.025 0.011 0.036 0.087 0.04 <0.025 <0.025 0.025 Total Uranium (U) mg/L <0.0025 0.0003 0.0004 0.0005 0.0003 <0.0025 <0.0025 0.0025 Total Vanadium (V) mg/L <0.025 0.0057 0.01 0.02 0.0073 <0.025 <0.025 0.025 Total Zinc (Zn) a mg/L <0.075 2.8 68 450 0.4 0.29 0.14 0.075 TOC elevated in Acid CIP due to use of an organic acid for cleaning (citric acid) b Onsite pH CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 48 of 80 Table 14 (con’t) Acid CIP Recirc#1 Solution Acid CIP Recirc#2 Conc. Acid CIP Recirc#2 Filtrate Acid CIP BW Flush Caustic CIP Conc Caustic CIP Filtrate 7.2 2.21 2.36 2.61 6.15 12.1 12.1 0 mg/L 0.025 0.88 6.7 2.3 0.58 4.6 4.3 0.025 Dissolved Antimony (Sb) mg/L <0.015 <0.015 <0.015 <0.015 <0.015 <0.015 <0.015 0.015 Dissolved Arsenic (As) mg/L <0.005 0.002 0.0037 0.0041 0.00092 0.002 0.0013 0.005 Dissolved Barium (Ba) mg/L 2.45 1.4 1.4 1.9 0.38 0.13 0.15 0.1 Dissolved Beryllium (Be) mg/L <0.025 <0.025 <0.025 <0.025 <0.025 <0.025 <0.025 0.025 Dissolved Boron (B) mg/L 5.3 <0.2 <0.2 <0.2 <0.2 <0.2 <0.2 0.2 Dissolved Cadmium (Cd) µg/L <0.13 1.2 1.6 0.81 0.3 0.39 0.27 0.13 Dissolved Calcium (Ca) mg/L 205 110 210 230 55 28 28 3 Dissolved Chromium (Cr) mg/L <0.025 0.022 0.06 0.091 0.0087 0.015 0.0088 0.025 Dissolved Cobalt (Co) mg /L <0.0075 0.0011 0.0034 0.007 0.00047 <0.0075 <0.0075 0.0075 Dissolved Copper (Cu) mg/L <0.005 0.032 0.031 0.017 0.011 0.019 0.015 0.005 Dissolved Iron (Fe) mg/L 0.7 41 85 230 17 1.5 <0.6 0.6 Dissolved Lead (Pb) mg/L <0.005 0.015 0.027 0.049 0.005 0.0025 0.0014 0.005 Dissolved Lithium (Li) mg/L 2.2 <0.2 <0.2 <0.2 <0.2 <0.2 <0.2 0.2 Dissolved Magnesium (Mg) mg/L 255 12 14 16 14 <2 <2 2 Dissolved Manganese (Mn) mg/L 0.41 0.88 2.8 3.8 0.9 <0.04 <0.04 0.04 Dissolved Molybdenum (Mo) mg/L <0.005 0.0012 0.0024 0.0046 0.00093 0.0037 0.0035 0.005 Dissolved Nickel (Ni) mg/L 0.016 0.0069 0.019 0.05 0.0049 <0.013 <0.013 0.013 Dissolved Phosphorus (P) mg/L <1 <1 <1 <1 <1 <1 <1 1 Dissolved Potassium (K) mg/L 67.0 <3 <3 <3 <3 7 7.7 3 Dissolved Selenium (Se) mg/L 0.0074 <0.005 0.00077 0.00072 <0.005 <0.005 <0.005 0.005 Dissolved Silicon (Si) mg/L 2.5 2.7 3.6 4.1 2.6 1.9 1.9 1 Dissolved Silver (Ag) mg/L <0.0025 <0.0025 <0.0025 <0.0025 <0.0025 <0.0025 <0.0025 0.0025 Dissolved Sodium (Na) mg/L 8,300 100 120 180 180 2200 2200 25 Dissolved Strontium (Sr) mg/L 14 3.8 8.6 9.5 0.98 0.35 0.26 0.2 Dissolved Sulphur (S) mg/L 5.7 1500 760 520 15 13 12 2 Dissolved Thallium (Tl) mg/L <0.005 <0.005 <0.005 0.00058 <0.005 <0.005 <0.005 0.005 Dissolved Tin (Sn) mg/L <0.025 <0.025 0.0071 0.01 0.0013 <0.025 <0.025 0.025 Dissolved Titanium (Ti) mg/L <0.025 0.015 0.035 0.072 0.0048 <0.025 <0.025 0.025 Dissolved Uranium (U) mg/L <0.0025 0.0003 0.00042 0.00045 0.00026 <0.0025 <0.0025 0.0025 Dissolved Vanadium (V) mg/L <0.025 0.0059 0.011 0.017 0.0016 <0.025 <0.025 0.025 Dissolved Zinc (Zn) b mg/L <0.075 2.9 53 480 0.33 0.28 0.15 0.075 Parameter Units UF Effl. SU Dissolved Aluminum (Al) pH b Onsite pH Refer to Appendix D for the detailed CIP procedure CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 49 of 80 MDL Impact of Flux Rate Flux rate of a membrane is a measure of the volume of water passing through a unit area of membrane surface. At high flux rates, more water is being forced through the membrane, so it is expected that fouling rate would also be elevated. UF flux rate was normalized to 20°C in order to permit comparison of membrane performance as the water temperature varied. Normalization was carried out in accordance with the USEPA Membrane Filtration Guidance Manual (EPA 815-R-06-009) as recommended by the membrane manufacturer. The UF system was run at normalized flux rates as high as 105 lmh (Figure 8 and Figure 10) to maximize recovery, but ultimately was reduced to a more optimal level of 53 lmh in order to permit use of standard cleaning methodologies and frequencies. Operation at the lower flux rate permits longer run times between CEBs, but ultimately requires a larger UF system and capital expenditure. UF backwash waste essentially contains basal water with elevated levels of coagulated solids, which should not represent an issue for reintroduction into the basal storage pond, as solids would naturally separate out in the pond. It is anticipated that UF reject can be directed back to the basal water storage pond, such that management of UF waste streams is not a significant issue. If waste stream management is not a significant issue, then the primary impact of system flux and recovery is on equipment sizing. Backwash Effectiveness Backwashing is a physical cleaning of the membrane that should result in a significant, though typically short-lived, improvement in TMP and membrane permeability. The goal of backwashing is to maintain performance and extend the timeframe required between chemical cleaning cycles such as CEBs and CIPs. In this pilot, backwashes were less effective at restoring performance than anticipated. During the initial part of the study, marginal but somewhat visible decrease in UF TMP could be observed with each backwash. However, after sustained operation and potential build-up of scalants on the membrane surface, fouling rate and TMP were not observed to decrease substantially with the backwashes. Nevertheless, backwashes were continued to be used because the backwash cycle was the primary mechanism used to remove accumulated solids in the UF vessel and maintain them at manageable levels. During a production cycle all flow was forced into the UF vessel and the only flow out was from water passing through the UF membrane, such that solids concentration in the membrane vessel continually increased during a production cycle (dead-end operation). Ultimately, when chemical dosing was not optimized during the pilot, backwashing was not an effective mitigative measure to remove fouling from the membranes. UF filtrate was used as the source of backwash water during the pilot. Brief experimentation with sodium metabisulphite (for enhanced manganese removal) added to backwash water was carried out in late September and is presented in Figure 11. No CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 50 of 80 appreciable improvement in backwash effectiveness was observed relative to UF filtrate alone. Low doses of sodium hypochlorite (for enhanced organics removal) in combination with UF filtrate were also examined, with no benefit observed either. Brief experimentation was carried out using RO permeate for backwash water in order to identify if a higher quality of water would improve backwash effectiveness (Figure 11). No improvement in backwash effectiveness was observed using RO permeate relative to UF filtrate. Figure 11. Comparison of backwash effectiveness using UF filtrate, UF filtrate with 100 mg/L of sodium metabisulphite and RO permeate as source water Impact of Manganese Concentration Manganese concentration was targeted primarily due to its anticipated impact on the RO membrane as opposed to the UF membrane. The initial UF filtrate target for Mn was 0.05 mg/L, while a common industry standard maximum for RO influent is 0.1 mg/L of Mn. Due to the complexities of oxidizing and precipitating Mn out of solution as detailed in previous sections, these targets were not consistently met. Precipitated Mn was removed from solution by the UF, while dissolved Mn passed through the membrane. As shown in Table 12, dissolved Mn concentrations in the UF filtrate ranged from 0.1 to 0.78 mg/L. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 51 of 80 Manganese was not significantly elevated in the UF CIP solution relative to iron and other common scalants. This indicates that manganese was not the governing factor in the fouling issues encountered with the UF membrane system. Impact of UF Influent pH Analysis of pH impact on UF fouling is possible due to the dosing strategy change that occurred on August 16th. Elevated pH was attempted at approximately 7.4 to 7.6 in order to minimize manganese solubility, but this was ultimately unsuccessful. High pH increased the impact of the high alkalinity of the water, which impacted the plant and UF membranes through CaCO3 precipitation. Reduction of the pH correlates to a negative impact on UF TMP development, TMP baseline and permeability (Figure 12). However, the pH change occurred at the same time as an increase in UF flux rate and a major change in chemical dosing strategy, which involved a reduction in permanganate dosing and deliberately not attempting to precipitate out all the manganese upstream of the UF. Due to the multiple changes that occurred alongside the pH change in the oxidation/precipitation stage upstream of the UF on August 16th, several key factors must be considered in order to identify the overall impact. Key considerations are manganese, iron, and calcium carbonate solubility and residuals, coagulant dosage and potassium permanganate dosage. The SDSI was positive at elevated pH of 7.5, indicating calcium carbonate scaling potential. At neutral UF effluent pH, the SDSI was slightly negative, indicating scaling was not theoretically expected. Each of the above noted factors contributing to scaling are discussed further below. Baseline TMP (psi) Time Between CEBs (Hrs) TMP Increase Rate (psi/day) Flux Corrected to 20°C (lmh) 40 UF Feed pH ~7.0 KMnO4 Dosage 1-1.5 mg/L FeCl3 Dosage ~7 mg/L UF Feed pH 7.4-7.5 KMnO4 Dosage 5-7 mg/L FeCl3 Dosage ~7 mg/L 110 30 100 25 90 20 80 15 70 10 60 5 50 0 30-Jul 04-Aug 09-Aug 14-Aug 19-Aug 24-Aug 29-Aug 03-Sep Flux TMP & Time Between CEBs 35 120 40 08-Sep Figure 12. Plot of TMP and normalized permeability at various influent pH settings CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 52 of 80 Metal solubility and the ability to prevent metal precipitation on the surface of the UF membrane were critical to achieving acceptable system performance. Manganese solubility was discussed in depth and it was determined that the inability to obtain consistently low Mn residuals in the UF filtrate was due to complexation reactions causing an increase in Mn solubility. CIP solution analysis does not indicate Mn precipitation on the UF was the governing factor in UF performance. Figure 13 shows the point of minimum Fe3+ solubility at pH 8.8, with solubility increasing as pH is reduced from that point. The target of the pilot was to precipitate iron ahead of the UF in order to minimize residual onto the RO system. Operation of the oxidation stage upstream of the UF at the higher range of pH experimented with has a clear benefit in lowering iron residuals in UF effluent. However, the benefits provided from the slightly reduced iron concentration in UF effluent must be weighed against the negative aspects of operating at elevated pH. pH range observed in pilot Figure 13. Solubility plot for ferric iron relative to pH Calcium carbonate solubility is significantly increased as pH decreases from a pH of 11. Scaling tends to increase as pH increases for the operating range experienced in the pilot (Figure 14). Significant CaCO3 scaling was observed throughout the pilot infrastructure and calcium was present in elevated concentrations in the CIP solution. Calcium carbonate scaling was an issue for the UF and the pilot as a whole, but the amount of scaling would be more significant at the high pH operational setting. In this pilot CaCO3 was not targeted for precipitation ahead of the UF system, and was addressed through the use of anti-scalant chemicals ahead of the RO system. Chemical dosing upstream of the UF was not designed to address CaCO3 as CEBs were anticipated to be sufficient to remove deposited material. Softening and degasification CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 53 of 80 were initially contemplated for inclusion in the process train, but were ultimately not included due to the extremely high chemical consumption anticipated. In the CIP solution analysis, iron was found in significantly elevated concentrations, warranting further analysis. While operating with the original dosing strategy, with both elevated pH and high coagulant and permanganate dosages, iron residual in UF filtrate was consistently below the detection limit (0.6 mg/L as Fe) as visible in Figure 15. In contrast, when the revised dosing strategy was employed with neutral pH in the oxidation/precipitation stage, iron residual in the UF filtrate was frequently elevated to near the 1 mg/L range. At the neutral pH, influent iron levels remained similar and coagulant dose range was used at both high and low levels with similar results. Minimum ferric solubility occurs at pH 8.8, which supports the observation of higher dissolved iron levels in UF filtrate at lower pH values. Approximate ranges in pilot : pH: 6.5 to 8.0 log (Ca): -2.28 to -2.40 CT: 0.014 to 0.030 Figure 14. Solubility plot for CaCO3 at various calcium and dissolved carbonic acid concentrations relative to pH CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 54 of 80 Raw Fe (mg/L) UF Effluent Fe (mg/L) Coagulant Dosage (mg/L as Fe) 10 9 Low Fe residual Elevated Fe residual pH approx 7.4 to 7.6 pH approx 6.8 to 7.0 pH 7.4 to 8.0 Coagulant Dose; Total Iron Concentration 8 7 6 5 4 3 2 1 0 01-Jul 08-Jul 15-Jul 22-Jul 29-Jul 05-Aug 12-Aug 19-Aug 26-Aug 02-Sep 09-Sep 16-Sep 23-Sep 30-Sep Figure 15. Comparison of residual iron in untreated and UF filtrate water at various coagulant doses and pH ranges in the oxidation/precipitation stage Analysis of coagulant dosing relative to pH and UF filtrate residuals provides insight into the impact of oxidation/precipitation operating pH on UF performance. Addition of ferric chloride (FeCl3) coagulant upstream of the UF was intended to destabilize colloidal particles and increase the average size of particulate coming in contact with the membrane surface. A secondary objective identified initially was for increased removal of organic material and a concurrent reduction in organic fouling of the UF. However, organic fouling was determined to not be significant as identified in the autopsy report (Appendix E). Several changes to coagulant dosing were made over the course of the pilot (Figure 16). It is clear that high coagulant dose alone is not responsible for elevated fouling rates as dose was maintained in the 6.0 to 7.5 mg/L (as Fe) range from the start of the trial until roughly a week after the operating pH was lowered to the 6.8 to 7.0 range. Fouling rate was stable during this period initially, but started to increase only after the pH change was made. During the period of exponential fouling rate increase in early September, the coagulant dose was increased from low levels (approximately 1.5 mg/L as Fe) in an attempt to counteract the rise, but fouling rate continued to increase. Stopping all coagulant dosing was briefly experimented with, but mostly using new UF membrane modules (initiated in order to provide sufficient flow to operate the downstream RO CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 55 of 80 system due to flow limitations caused by operating the UF system at the optimized UF flux of 40 lmh). Pilot data indicates iron fouling on the membrane is more significant at the neutral pH than the elevated pH initially used in July and early August. Ferric chloride dose is secondary relative to this consideration, but it is logical to conclude that minimizing the ferric chloride dose would assist in reducing iron fouling on the membrane surface and therefore result in the reduction of overall fouling rate and maximization of UF system recovery. However, operation at elevate pH introduces issues with calcium carbonate scaling as discussed previously. Permanganate dosing levels and philosophy changed substantially through the pilot (Figure 16). Initial attempts to dose the oxidant to achieve a target ORP level proved ineffective. When the major change in dosing strategy was carried out on August 16th, permanganate was dosed at a constant low dose typically in the 1.0 to 1.5 range. High and low permanganate doses (regardless of pH) did not reliably produce low Mn levels in the UF filtrate. The reduction in permanganate dosing occurred at the same time pH was reduced, such that their impacts cannot be fully separated. However, fouling rate changes appear to more closely follow pH changes than permanganate dosing changes for periods such as the high pH period between September 27th and 30th (Figure 16). Baseline TMP (psi) TMP Increase Rate (psi/day) Coagulant Dose as Fe (mg/L) Permaganate Dose (mg/L) 80 60 TMP 50 Flushing system of pond organics pH 7.4-7.6 10.5 Major change in dosing strategy pH 6.8-7.0 9.0 pH 7.6-8.0 CIP Crossflow pH 6.8-7.0 40 7.5 6.0 30 New modules 4.5 20 3.0 10 1.5 0 0.0 20-Jun 30-Jun 10-Jul 20-Jul 30-Jul 09-Aug 19-Aug 29-Aug 08-Sep 18-Sep 28-Sep 08-Oct 18-Oct Figure 16. TMP development rates for individual UF runs at different coagulant and permanganate doses CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 56 of 80 Chemical Dose 70 12.0 Pond Water Trial Impact of Not Softening Upstream of the UF Initially, the basal water treatment process train included both a degasification (alkalinity reduction) step as well as a softening process step upstream of the UF system. Prior to initiation of pilot testing, a review of the advantages and disadvantages of including these process steps was carried out and the decision was made by CNRL to exclude them from pilot testing. The primary disadvantage in including these processes is the large volumes of chemicals (sulphuric acid, caustic soda and lime) required. This initial configuration would have required three significant pH adjustments to permit degasification (low pH), softening (high pH) and finally neutral pH going into the RO system. Based on preliminary modeling of the system it was determined that the pretreatment provided by oxidation/ coagulation and the UF in combination with use of appropriate anti-scalant chemicals would be sufficient pre-treatment for piloting the RO system. Not carrying out softening upstream of the UF system results in a trade-off between different negative impacts that occur when operating at elevated (7.6 to 8.0) to neutral (approximately 6.9 to 7.0) pH in the oxidation/precipitation stage. At elevated pH the iron oxidation reaction is more easily controlled such that precipitation occurs ahead of the membrane instead of scaling on the membrane surface. Elevated pH also tended to reduce iron concentrations in the UF filtrate. However, in the pilot when the elevated pH scenario was used, there were widespread issues with CaCO3 precipitation throughout the pilot plant infrastructure (due to the high scaling potential of the water as evidenced by the high SDSI value of 0.56 at a pH of 7.5 and water temperature of 15°C as experienced in the pilot trials). Even if water temperature was at the temperature it comes out of the wellhead (reported to be approximately 5˚C by CNRL) SDSI calculates to be 0.37, which indicates high scaling potential. This resulted in repeated issues with scaling up of equipment such as pumps and the Amiad pre-screening filter (standard equipment used upstream of UF systems to protect UF membranes from damage), though only a minor impact on UF performance. At neutral pH, the calcium carbonate precipitation was reduced such that it was no longer a governing operating factor. At a pH of 6.9 and water temperature of 15°C (as observed in the pilot trials), the SDSI was approximately -0.04, indicating calcium carbonate scaling was not theoretically expected. A new concern relating to iron precipitation (among other compounds) on the UF membrane surface began to be a significant factor which resulted in a dramatic increase in observed fouling rate and reduced intervals between required CEBs. The major benefit of not including softening in the treatment train is the elimination of the need for softening infrastructure as well as significant ongoing chemical dosing costs. Significant reduction in sulphuric acid, caustic soda and lime were achieved, though additional anti-scalant chemical was required. Cross Flow versus Dead End UF Operation The UF pilot system was designed for dead end operation and was operated in this manner for the majority of the basal piloting period. Dead end operation was initially deemed acceptable for this application as the untreated basal water contained CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 57 of 80 consistently low solids concentrations. However, chemistry of the UF influent water resulted in higher than desirable fouling rates, necessitating experimentation with cross flow operation in the final weeks of basal piloting. Cross flow was obtained by recirculation of 25% of influent flow back to the coagulation tank from October 1st to 2nd. Introducing a cross flow stream causes scouring action across the surface of the UF membrane. The scouring acts to physically remove a portion of the fouling material that has deposited on the membrane and theoretically increases the timeframe between CEBs or CIPs. Figure 17 clearly shows improved TMP and normalized permeability after the transition from dead-end to cross-flow UF operation. During this period the flux rate was set at a normalized flux of approximately 53 lmh (with some minor variations due to temperature fluctuations). Cross flow operation is a more optimal operational condition than dead end operation for this treatment application. The membrane used in this pilot is primarily intended for low solids, dead end applications. Alternative membrane types designed for cross flow operation should be considered when scaling up the results from this pilot study. Figure 17. Plot of TMP and permeability for dead-end and cross-flow UF operation CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 58 of 80 Comparison of Pond and Well Water on UF Fouling Pond water use was explored in the pilot due to the presumed benefits of water equalization and water aging (introduction of oxygen into the water from the atmosphere). However, the presence of significant algae in the pond water was a dominant factor which ultimately resulted in an immediate negative impact on UF performance when pond water was fed to the pilot infrastructure (Figure 18). The TMP increase rate and baseline TMP dramatically increased upon introduction of pond water into the system. After extensive flushing of the system and resumption of using wellhead water as feed water, TMP increase rates returned to levels similar to before the pond water was introduced. Key differences between untreated basal water taken from the pond relative to basal water taken from the wellhead are as follows: easily oxidized compounds have been oxidized and in some cases precipitated out of solution reduced dissolved hydrogen sulphide algae in the water was significant and easily observable in both water at the pilot plant and in the source pond organic material (algae) were most probably responsible for the immediate and rapid decrease in UF performance when basal water source was changed from the wellhead common header to directly from the pond. Algae was visibly present in significant quantity in the basal water pond at the time of the trial CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 59 of 80 Figure 18. Comparison overview of flux, run length, baseline TMP and TMP increase rate for piloting periods when pond water versus wellhead water were used as feed water for the pilot CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 60 of 80 5.3 Reverse Osmosis (RO) Reverse Osmosis provides the highest level of treatment of all membrane types. The microscopic pores reject organic compounds salts and minerals. In designing this pilot it was expected that RO would be capable of producing water of sufficient quality to achieve project objectives. However, the level of pre-treatment required is typically high for this technology. The initially proposed pre-treatment train included degasification with sulphuric acid followed by softening upstream of the UF system. Based on a review of the untreated basal water quality and the significant cost savings in chemical usage, the upstream treatment was reduced to chemical oxidation, coagulation and UF treatment followed by pH reduction, anti-scalant dosing and ORP reduction immediately upstream of the RO membranes. With the revised pre-treatment train, the anticipated challenge was running the RO system at a high recovery while at the same time managing fouling with standard cleaning methodologies and frequencies. Operating Conditions The pilot RO system consisted of a three stage design with fiberglass pressure vessels containing three 102 mm (4 inch) diameter, 1016 mm (40 inch) long elements. Detailed specifications on the membranes are provided in Table 15. Provision of adequate flow rates through a pilot sized system resulted use of a three stage design for the pilot study. System configurations and operating ranges used over the course of the pilot are provided in Table 16 and Figure 19. Detailed plots of RO system operating parameters over the entire course of the pilot are located in Appendix C. Table 15. Overview of RO membrane specifications Parameter Membrane Model Membrane Type Maximum Operating Temperature Maximum Operating Pressure Maximum Pressure Drop pH Range, Continuous Operation pH Range, Short Term Maximum Feed Silt Density Index Feed Chlorine Tolerance Membrane Element Active Surface Area Stabilized Salt Rejectiona Max Feed Flow Ratea Details DOW Filmtec SW30-4040 Polyamide Thin-Film Composite 45 °C 6895 kPa (1000 psi) 103 kPa (15 psig) 2 to 11 1 to 13 SDI 5 <0.1 mg/L 7.4 m2 (80 ft2) 99.4% 3.6 m3/hr (16 gpm) a Based on standardized test conditions as follows: 32,000 mg/L NaCl, applied pressure of 800 psig, 25C, and 8% recovery rate CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 61 of 80 Table 16. Overview of RO system operating conditions Parameter Number of Stages Number of elements per pressure vessel Membrane Array (50% recovery) Membrane Array (60% recovery) Recovery Feed Pressure Permeate Pressure Influent Flow Operating flux (normalized to 25°C) Value 3 3 3 (stage 1) X 2 (stage 2) X 1 (stage 3) 2 (stage 1) X 1 (stage 2) X 1 (stage 3) 50% and 60% 3447 to 6895 kPa (500 to 1000 psi) Stage 1: 0 to 414 kPa (0 to 60 psi) Stage 2 & 3: 0kPa (0 psi) 3.6 m3/hr (16 gpm) Overall: 7 to 46 lmh (4 to 27 gfd) Operating pressure (50% recovery) Stage 1: 4 to 50 lmh (2 to 29 gfd) Stage 2: 7 to 56 lmh (4 to 33 gfd) Stage 3: 20 to 40 lmh (12 to 24 gfd) Overall: 3613 to 4737 kPa (524 to 687 psi) Operating pressure (60% recovery) Stage 1: 3565 to 4537 kPa (517 to 658 psi) Stage 2: 3530 to 4537kPa (512 to 658 psi) Stage 3: 3482 to 4433 kPa (505 to 643 psi) Overall: 4633 to 6419 kPa (672 to 931 psi) Time between CIPs Antiscalant chemical Antiscalant dose range Biocide chemical Cleaning Agents Stage 1: 4516 to 6260 kPa (655 to 908 psi) Stage 2: 4454 to 6205 kPa (646 to 900 psi) Stage 3: 4357 to 6129 kPa (632 to 889 psi) Approx. 1 to 2 months Hydrex 4102 - Liquid 2.7 – 7.6 mg/L Nalco Permaclean PC-11 - Liquid Citric Acid, Sodium Hydroxide, Sodium Metabisulphite CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 62 of 80 50% Recovery Configuration Stage 1 Stage 2 Stage 3 RO Influent Permeate Concentrate 60% Recovery Configuration Stage 1 Stage 2 Stage 3 Permeate Concentrate RO Influent Figure 19. Simplified view of RO system configurations at 50% and 60% recovery. Flux and pressures for each stage are provided in Table 16, and detailed plots in Appendix C Flux rate is a key parameter in the design of a RO treatment system. RO system flux rates in this report have been normalized to 25°C in accordance to ASTM standard D4516 - 00 (Standard Practice for Standardizing Reverse Osmosis Performance Data) and the membrane supplier technical manual. Initial flux rate for the system was set at around 14 lmh (8 gfd), with notably high flux rates through the third stage membranes (Figure 21 and Figure 22). During this period, overall recovery was determined to be in the 25 to 30% range due to a malfunctioning reject flow meter. On August 11th, the recovery rate was increased to the target rate of 50%, at an influent flow of roughly 16 gpm and an overall normalized flux of around 20 to 22 lmh (12 to 13 gfd). A recovery rate of 60% was operated from October 4th to 8th using a 3 stage, 2 X 1 X 1 pressure vessel array at an overall normalized flux of approximately 43 lmh (25 gfd). CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 63 of 80 Figure 20. Overview of RO flux rate and normalized (to 25°C) flux rate over the course of the pilot CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 64 of 80 Figure 21. Overview of normalized (to 25°C) RO flux rate broken down by stage over the course of the pilot Chemical Usage and Operational Settings at Optimal Conditions A summary of operational settings and chemical usage for operation of the RO unit at optimal conditions is provided in Table 17. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 65 of 80 Table 17. Overview of RO system related chemical usage and operational settings at optimal conditions Parameter Sulphuric acid dose (to achieve 6.5 pH) Sodium metabisulphite dose Optimal Setting = 700 to 800 mg/L as H2SO4 Reasoning = 160 to 200 mg/L Anti-scalant dose (50% recovery) Anti-scalant dose (60% recovery) Biocide dose (Nalco Permaclean PC-11) = 6.6 mg/L -Dose was based on maintaining an RO feed ORP value of 100 to 150 mV as recommended by the equipment vendor. -Maintaining manganese in a reduced dissolved form was a key consideration in dosing metabisulphite as manganese in a dissolved and reduced state did not act as a significant RO foulant. Higher than industry standard Mn levels were often present in the RO feed so this was a significant consideration. Lower doses of metabisulphite may be possible. -Alternate anti-scalant chemicals could be considered to address the iron scaling issues identified in this study -Alternate anti-scalant chemicals could be considered to address the iron scaling issues identified in this study -Weekly application of biocide was carried out as a preventative measure -Biological growth in the RO system was not observed in this study. -The short duration of the pilot study may not have given biological activity in the system sufficient time to establish Time between CIPs Flux rate normalized to 25°C (50% recovery) = 1 to 2 months = 23 lmh = 6.6 mg/L = 200 mg/L for 30 min, once per week CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 -Based on performance observed during the pilot May 29, 2013 66 of 80 Treatment Performance Treated water quality from an RO unit is highly dependent on parameters such as recovery, temperature and influent water quality. Water temperature was relatively stable throughout the study as is typical with groundwater. Brief temperature excursions were primarily due to limitations of the pilot facility. For example, there was a brief period in August where water temperature increased to above 20˚C, due to an operations shutdown resulting in extended hold times in the untreated water storage tanks combined with high ambient temperatures. Two recovery settings of significance (50% and 60%) were used and are worthy of analysis. However, the vast majority of the study was focused on the 50% recovery as this was originally identified as the primary target for the pilot. The 60% recovery was examined briefly at the end of the study in an attempt to push the operational limits of the technology. Influent water quality was relatively stable throughout the study, but did undergo a reduction in TDS at the latter portion of the study, when the 60% recovery setting was examined. High TDS levels in the basal water and RO feed water result in high osmotic pressures and resulting high feed water pressures. The resulting high osmotic pressure was the primary factor that limited the achievable RO recovery levels to the range of 50 to 60% observed in the pilot. Scaling at pH of 7.6 a higher contributed to scaling during the pilot. However, operation at a pH below 7.0 and maintaining manganese in a reduced state largely mitigated the impact of scaling on achievable RO recovery. Normalized Salt Rejection (NSR) Normalized salt rejection is a standard parameter used in assessing performance of RO membranes. NSR takes into account the effect of changes in temperature, recovery, feed TDS and permeate flow on salt passage. Declines in NSR over time can indicate an issue with membrane integrity or fouling. Ideally the NSR remains relatively stable over the course of operation. The initial two weeks of RO operation displayed a higher normalized salt rejection (NSR) than the remainder of the pilot study (Figure 22). This is typical of the breaking in period for an RO membrane. In mid-August, there were significant deviations in NSR, which were later attributed to improperly set valves in the RO system that were permitting a small portion of RO reject water to pass through to the permeate flow. During this period, elevated TDS was observed in the permeate. Once this issue was resolved, TDS levels dropped and NSR stabilized to between 98% and 99%. Based on the NSR trend, the membrane maintained its treatment integrity throughout the course of the pilot study. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 67 of 80 Figure 22. Overview of Normalized Salt Rejection (NSR) and Normalized Salt Passage (NSP) over the course of the pilot 50% Recovery Table 18 summarizes the RO treatment performance at 50% recovery. Organic material in UF filtrate was below detection limits, but due to the high salinity of the water, the detection limit for TOC was 13 mg/L. In RO permeate, salinity is greatly reduced which eliminated the detection limit issue. In RO permeate the TOC was reduced to 0.3 mg/L on average. Naphthenic acids were reduced to < 1 mg/L from 3.5 mg/L in the untreated basal water. UF treatment did not appreciably reduce naphthenic acid concentration. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 68 of 80 Table 18. Summary of RO treatment performance (permeate water quality) at 50% recovery Average (ND= 50% MDL) Min psi 639 624 858 SU 5.4 4.7 µS/cm 770 SU µS/cm Parameter Feed Pressure (on-line instrumentation) pH (onsite) Conductivity (onsite) pH Conductivity Total Dissolved Solids Total Organic Carbon Naphthenic Acids Total Sodium (Na) % Reduction Relative to Std. Dev # of Obs 6.7 0.4 37 448 1652 273 39 5.90 593 5.47 220 6.44 810 0.35 169 9 9 0% 0% mg/L 304 120 430 90 9 mg/L 0.3 <0.5 <0.5 0.0 mg/L mg/L 0.5 123 <1 87 <1 160 0.0 25 Units Max %ND MDL UF Effl RO Infl Raw 0 1 98.4% 98.4% 0% 10 98.6% 98.6% 9 100% 0.5 95.0% 96.4% 9 9 100% 0% 1 25 95.0% 73.7% 98.4% Dissolved solids were the primary target for reduction by the RO system. Permeate conductivity was reduced to 594 µS/cm, a 98.4% reduction relative to UF filtrate and untreated basal water. TDS was reduced to 304 mg/L on average, with a standard deviation of 90 mg/L. Sodium was also a primary target for reduction. Total sodium was reduced to an average of 123 mg/L (SD = 25 mg/L) in the RO permeate at a recovery of 50%. This represents a 98.4% reduction relative to the dissolved sodium concentration in untreated basal water. At all times, the RO permeate quality stayed well below the maximum targets of 1000 mg/L for TDS and 500 mg/L sodium (Table 18). 60% Recovery The RO was operated at 60% recovery at the beginning of October; during a period where influent temperature was lower than average for the piloting period. Over the 50% recovery period, average RO influent temperature was 16.2°C, while during the 60% recovery period, average temperature was 13.0°C. As temperature decreases, diffusion activity across the membrane also decreases which typically results in an increase in rejection by the membrane. In order to confirm that there are no issues with the membrane and results are accurate, the Normalized Salt Rejection (NSR) trend can be examined for anomalies. The NSR accounts for changes in feed water temperature and recovery changes in addition to salt concentration gradient changes. Comparing the two periods, the NSR was relatively constant in the 97% to 98% range before and after the CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 69 of 80 transition from 50% to 60% rejection (Figure 22). This indicates that the membrane performed as expected in terms of salt rejection, with variations in permeate TDS and conductivity attributable to the changes in temperature and recovery. At all times, the RO permeate quality stayed well below the maximum targets of 1000 mg/L for TDS and 500 mg/L sodium (Table 19). Table 19. Summary of RO treatment performance (permeate water quality) at 60% recovery Parameter Feed Pressure (on-line instrumentation) pH (on-site) Conductivity(onsite) pH Conductivity Total Dissolved Solids Total Organic Carbon Naphthenic Acids Total Sodium (Na) Average (ND= 50% MDL) Min psi 856 672 931 SU 4.8 4.7 µS/cm 471 SU µS/cm % Reduction Relative to Std. Dev. # of Obs. 4.9 0.1 5 374 611 117 5 5.43 5.30 5.53 0.12 3 0% 0 410 360 480 62 3 0% 1 mg/L 207 180 250 38 3 0% 10 mg/L 2.3 <0.5 <0.5 3.6 3 100% 0.5 mg/L mg/L 0.5 <1 <1 0.0 3 100% 1 90 81 95 8 3 0% 25 Units Max %ND MDL UF Effl RO Infl Raw 98.9% 98.9% 98.9% 99.1% 64.1% 64.1% 64.1% 86.1% 87.8% 98.9% 98.8% RO Reject Water Quality RO reject disposal is an important consideration, which was independently investigated by Veolia using reject water produced during this pilot. The quality of the RO reject is critical for designing related treatment processes. The methodology used for the ZLD testing was further treatment of the reject by evaporators and crystallizer. Details of this testing is presented in Appendix F of this report. Table 20 and Table 21 provide a summary of RO reject water quality characteristics for 50% and 60% recovery operation during the course of this pilot. At a 50% recovery, it is expected that the concentration factor for most compounds would be 2.0 times the RO influent water. At a recovery of 60%, concentration factor should theoretically be 2.5. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 70 of 80 Table 20. Summary of RO reject water quality characteristics at 50% recovery Min Max Std. Dev. # of Obs. SU µS/cm SU µS/cm mg/L Average (ND= 50% MDL) 6.9 65,687 7.49 65,222 43,222 6.6 41,600 7.09 64,000 42,000 7.8 68,900 7.97 66,000 44,000 0.3 4,467 0.26 667 667 mg/L 4,944 4,100 5,900 mg/L 3 <5 mg/L mg/L mg/L mg/L 6,033 3 3 2,567 mg/L Parameter Units %ND MDL C.F. pH (on-site) Conductivity (on-site) pH Conductivity Total Dissolved Solids Alkalinity (Total as CaCO3) Alkalinity (PP as CaCO3) Bicarbonate (HCO3) Carbonate (CO3) Hydroxide (OH) Hardness (CaCO3) Total Organic Carbon (C) Naphthenic Acids Total Calcium (Ca) Dissolved Calcium (Ca) Dissolved Magnesium (Mg) 37 39 9 9 9 0% 0% 0% 0 1 10 1.81 1.96 629 9 0% 5 2.35 <5 0.0 9 100% 5 5,000 <5 <5 1,800 7,200 <5 <5 2,800 760 0.0 0.0 308 9 9 9 9 0% 100% 100% 0% 5 5 5 0.5 2.32 7 <13 15 2.9 9 89% 13 1.46 mg/L mg/L 7 337 <1 300 9 370 2.8 23 9 9 11% 0% 1 3 2.24 mg/L 337 260 370 37 9 0% 3 2.10 mg/L 420 420 420 1 0% 2 2.14 C.F = Concentration factor Table 21. Summary of RO reject water quality characteristics at 60% recovery Parameter Units pH (on-site) Conductivity (on-site) pH Conductivity Total Dissolved Solids Alkalinity (Total as CaCO3) Alkalinity (PP as CaCO3) Bicarbonate (HCO3) Carbonate (CO3) Hydroxide (OH) Hardness (CaCO3) Total Organic Carbon (C) Naphthenic Acids Total Calcium (Ca) Total Potassium (K) Dissolved Calcium (Ca) Dissolved Magnesium (Mg) SU µS/cm SU µS/cm mg/L mg/L mg/L mg/L mg/L mg/L mg/L mg/L mg/L mg/L mg/L mg/L mg/L Average (ND= 50% MDL) 6.6 81,120 7.3 78,667 55,333 Min Max Std. Dev. # of Obs. 6.5 79,600 7.0 78,000 55,000 6.7 82,200 7.6 79,000 56,000 0.1 1,028 0.28 577 577 4,033 3,800 4,400 3 4,867 3 3 3,633 <5 4,600 <5 <5 3,600 21.3 12.7 487 160 477 593 %ND MDL C.F. 5 5 3 3 3 0% 0% 0% 0 1 10 2.19 2.52 321 3 0% 5 2.69 <5 5,300 <5 <5 3,700 0.0 379 0.0 0.0 58 3 3 3 3 3 100% 0% 100% 100% 0% 5 5 5 5 0.5 <13 12.0 470 150 470 25.0 13.0 500 170 480 4.7 0.6 15 14 6 3 3 3 2 3 33% 0% 0% 0% 0% 13 1 3 3 3 580 610 15 3 0% 2 CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 2.56 2.42 3.52 2.43 12.31 2.38 May 29, 2013 71 of 80 Fouling Rate and Cleaning Effectiveness Particulate fouling was not considered a major factor for the RO due to the reliable and near complete solids removal by the upstream UF system. SDI values in UF filtrate averaged 0.9 with a standard deviation of 0.8. The RO system requires an SDI of less than 5 at a minimum and ideally less than 3. SDI values underwent a small increase after passage through the cartridge filter, pH adjustment and anti-scalant addition, with a resulting average SDI of 2.8 (standard deviation 1.3). This could be due to post filtration precipitation caused by pH changes or from the chemical additions themselves. Regardless, SDI values for water contacting the RO membrane were consistently low. Mineral scaling on the RO membranes was modelled using DOW software (ROSA) prior to starting the pilot in order to identify priority compounds in the untreated water that needed addressing. Initially, manganese was focused on as requiring reduction due to anticipated negative impact on the RO membrane. However, observation of the RO performance showed that if manganese was maintained in a reduced state (as gauged by an ORP of approximately 100 to 200 mV) with pH reduction and anti-scalant addition, scaling impact was minimal. Biological fouling is always a consideration in RO systems, but no evidence of biological fouling was observed in this pilot when feeding well water. As a preventative measure, biocide was applied to the RO membranes on a weekly basis. CIP Analysis The chemical cleaning methodology used for the RO membrane was an infrequent clean-in-place (CIP), which used a combination of citric acid and sodium metabisulphite to address mineral scaling. The CIP was carried out in 3 stages in order to permit isolation of each of the three RO system stages. All phases of the CIP were carried out at low pH as the focus of the cleaning was removal of mineral scalants. A plot of the RO system stage layout is provided in Figure 19. A sample of the cleaning solution used in each of the three CIP steps was sent to an external lab for analysis of common scalants. Only a single RO CIP was carried out during the pilot study. The pilot strategy for an RO CIP had the following trigger events: Normalized permeate Flow (NPF) decrease by 10 to 15% Trans-membrane Pressure (TMP) drop increase by 15 to 25% Iron was a significant foulant of the RO membranes and of all parameters examined in the CIP cleaning solution, had the highest levels relative to RO influent concentrations (Table 22). For all three stages in the system, iron had notable concentrations in the CIP solution. It is likely that iron fouling could be addressed by modification of the type or dose of anti-scalant. Most significant is that iron was present at extremely high levels in all three RO stages indicating iron scaling had occurred throughout the RO system. All other metals analysed for were only present in high concentration in the final RO stage, which is where mineral scaling is expected to first manifest as an issue. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 72 of 80 Table 22. Overview of RO CIP cleaning solution analysis for key scaling compounds Iron (total) Manganese (total) Aluminum (total) Barium (total) Calcium (total) Magnesium (total) Strontium (total) mg/L 0.66 mg/L 0.56 mg/L 0.22 mg/L 1.7 mg/L 186 mg/L 248 mg/L 12.6 Phase 1 (Stage 3 focused) 26 26 2.5 7.7 1800 89 64 Phase 2 (Stage 2 focused) 95 1.6 2.2 1.7 660 9.1 8.7 0.54 0.27 100 67 6.8 8.4 1.2 2.4 1.4 630 12 9.7 Analyte Units RO Influent Avg CIP Solution Phase 3 (Stage 1 focused) 110 0.7 1.4 Control (unused) 2.4 0.26 0.6 Metabisulphite CIP 23 2 1.3 Ratio of CIP Concentration to RO Influent Concentration Phase 1 (Stage 3 focused) 3,965% 4,631% 1,133% 451% 969% 36% 509% Phase 2 (Stage 2 focused) 14,488% 285% 997% 100% 355% 4% 69% 16,776% 366% 3,508% 125% 46% 356% 634% 272% 589% 32% 16% 82% 54% 36% 339% 3% 3% 5% 10% 19% 77% Phase 3 (Stage 1 focused) Control (unused) Metabisulphite CIP Calcium was present in very high concentrations in the CIP step that focused on the third RO stage. Elevated levels were present in the second stage CIP solution, but were negligible in the first stage CIP solution. The high levels of calcium are expected based on the high hardness (average 1,429 mg/L as CaCO3) in the RO influent. Manganese, aluminum, barium and strontium were all present in the CIP solution, with the highest concentrations observed in the third stage CIP solution. Scaling is typically most severe in the final RO element, which is what was observed in this pilot. Normalized Permeate Flow One of the primary tools available to gauge membrane performance is the analysis of the normalized permeate flow (NPF) trends. Gradual reductions in the NPF can indicate mineral scaling, colloidal or organic fouling. Rapid declines in NPF are commonly associated with metal oxide fouling or biological fouling. In contrast, dramatic increases in NPF can indicate structural damage or chemical attack on the membrane surface. Normalized permeate flow takes into account the effect of changes in temperature and net driving pressure (NDP) on the permeate flow. The NDP is calculated by subtracting CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 73 of 80 average osmotic pressure and permeate back pressure from the average feed pressure. Thus NPF is normalized for any changes in the NDP and changes in pressure drop across the membrane element. If all other operating parameters remain constant, any change in the average TDS concentration in the RO feed will affect the osmotic pressure, which in turn will affect the NDP and NPF. However the salt passage or permeate TDS concentration should not affect the NPF unless some underlying problem like scaling or membrane damage is affecting both. The initial three weeks of RO operation resulted in a rapid reduction in NPF due to several factors. New RO membranes typically display extremely high but short lived permeability which stabilize to levels that typically become the baseline permeability (which is ideally returned to after standard CIP cleaning). Significant calcium carbonate precipitation was observed in the CIP carried out on August 15th to 18th. This was attributable to operation at elevated pH upstream of the UF and precipitation during periods where the RO system was in standby. Subsequent to the CIP, operation at neutral pH and flushing the RO with permeate upon shutdown, resolved the issue. It is also possible to further isolate membrane fouling across the system by examining NPF trends for each individual RO stage (Figure 23). After the RO CIP was completed on August 19th, the second and third stages of the RO system were stable and flat. The majority of variation in NPF occurred in the first stage for the system. The significant rise in Stage 1 NPF from approximately September 27th to October 1st is noteworthy and significant as it correlates with a major change in RO pre-treatment operation. During this period, the oxidation dosing strategy was reverted back to what was pursued before August 17th. The pH upstream of the UF was increased to greater than 7.5 and permanganate dose increased to 5.0 mg/L in order to achieve complete oxidation and precipitation of reduced species such as iron, sulphide and manganese. RO influent pH was unchanged from before during and after this period due to sulphuric acid dosing immediately upstream of the RO system. This indicates that the compounds being oxidized, precipitated and eventually filtered out of solution by the UF have an immediate impact on the RO membrane operation. External lab results for RO influent indicate nondetectable iron levels (< 0.6 mg/L), but higher than average manganese levels (0.19 to 0.78 mg/L) during this time span, and all other examined compounds remain at similar levels to the immediately preceding period. Water quality results do not clearly identify the compounds or species involved in this short term improvement in RO performance. The fact that the change in NPF was focused on the first stage, and iron was the only scaling compound measured in significant quantity in the Stage 1 CIP solution, indicates that its tendency to foul the membrane at low concentrations may be involved. The RO membrane autopsy indicated that the most significant deposits on the membrane were iron and barium scaling, with much lower concentrations of sulphur and phosphorous (Appendix E). The autopsy also confirmed that membrane deposits were primarily inorganic. Only very low concentrations of organic material were measured in the deposits. The reduction in NPF on October 4th is due to increasing system recovery from 50% to 60%. Increased recovery is expected to impact NPF due to the resulting increase in RO feed pressure and consequently the increase in Net Driving Pressure. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 74 of 80 Pilot data does not indicate irreversible fouling is occurring as full permeability recovery was achieved from the CIP and operational pressures remained relatively stable during regular operation. Improved performance can likely be achieved through the use of reduced ferric coagulant doses upstream of the UF system. Alternatively, the antiscalant type and dosage could be adjusted to target iron fouling on the membrane. Based on the data from this pilot, CIPs would likely be required on a monthly or bimonthly basis. This is in line to slightly more frequent than would occur at a desalination facility. However, the mineral composition and upstream chemical dosing of the RO influent has been shown to be the governing factor in membrane fouling and scaling, so the two applications are not directly comparable. Figure 23. NPF of the RO membrane overall and for each stage CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 75 of 80 Impact of Not Softening Calcium carbonate was a significant scale-causing compound for the RO system due to the high calcium hardness and alkalinity in basal water. Other notable hardness-causing ions present in the influent in significant concentrations were iron, manganese, barium and strontium. Use of pH adjustment, ORP control and anti-scalant dosing during the pilot appeared to effectively manage the impact of hardness causing ions on the membrane. Influent pressure was relatively stable and the time interval before a CIP was required was within industry standards. Based on this data, softening is not essential for operation of the piloted treatment train. The scenario where softening may provide an advantage, is if the high hardness in the RO reject was problematic for disposal of the waste stream. RO reject disposal is examined in detail in Appendix F. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 76 of 80 6. Summary and Conclusions 6.1 Treated Water Quality The piloted treatment train proved capable of meeting the water quality objectives of TDS < 1000 mg/L and sodium < 500 mg/L for all operational settings examined. 6.2 6.3 Operational Experiences and Lessons Learned Untreated basal water is chemically unstable and requires equalization and potentially aeration or mixing in order to achieve stability Equalization and aging of the untreated basal water results in an increase in pH and ORP with the precipitation of mainly sulfides. Aeration of the water substantially accelerates this process. Any full scale design would need to account for any pH change due to water equalization or aeration incorporated into the system Bench scale chemistry did not always scale up to pilot scale, particularly for oxidation/precipitation reactions Chemical dosing (permanganate or metabisulphite) based on ORP measurement is difficult to implement because of unstable nature of basal water and rapid fouling of probe Water usage in UF CEB and BW cycles had a dramatic impact on UF recovery UF CEB frequency was governed by fouling rate UF CIPs were effective in removing fouling material More frequent cleanings are likely be required for the UF if operated in dead-end mode relative to cross-flow mode Pond water causes rapid fouling of UF due to algae and other organics Untreated basal well water contains low organics and O&G levels making organic fouling a lesser concern for membranes Elevated Mn levels (relative to industry standard of <0.1 mg/L in RO feed water) when maintained in a reduced state did not compromise RO performance, thus targeting Mn removal may not be required for optimum membrane performance Iron was identified as a major scalant for both UF & RO. Even small dosages of ferric based coagulants at low pH conditions can deteriorate this situation Hardness causing compounds in the basal water can rapidly scale up membranes and associated equipment at high pH conditions Overdosing of metabisulphite can cause higher than optimal sulphate levels in RO feed that can potentially lead to increased Barium Sulfate scaling Optimal Operational Settings Observed in Pilot (by Unit Process) Oxidation/Precipitation/Coagulation Parameter Potassium permanganate Ferric chloride Optimal Setting = 1 to 1.5 mg/L = 0 to 2 mg/L as Fe Sodium Hydroxide = 0 mg/L CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 77 of 80 Ultrafiltration (UF) System Parameter Flux (normalized to 20˚C) Recovery range Operational flow mode CEB sequence - Acid CEB - Caustic CEB CEB frequency CIP sequence - Acid CIP - Caustic CIP CIP frequency Optimal Setting = 53 lmh = 70 to 80% = Cross-flow operation = Acid CEB – Caustic CEB – Acid CEB approximately 2.5 pH 5000 mg/L citric acid 200 mg/L sodium metabisulphite 30 min soak time - approximately 12 pH using caustic - 600 mg/L NaOH - 600 mg/L NaOCl - 30 min soak time = once every 24 hrs at optimum operating conditions = Caustic CIP – Acid CIP - Caustic CIP ≤2.3 pH using citric acid, 200 mg/L sodium metabisulphite 38°C solution 10 hr soak/ recirculation period intermittent air scour approximately 12 pH using caustic 2000 mg/L NaOCl 32°C solution 10 hr soak/ recirculation period intermittent air scour = every 2 to 4 weeks Reverse Osmosis (RO) System Parameter Optimal Setting Sulphuric acid dose (to achieve 6.5 = 700 to 800 mg/L as H2SO4 pH) Sodium metabisulphite dose = 160 to 200 mg/L (observed dosage to achieve targeted ORP at RO feed; lower dosage could be possible) Anti-scalant dose (50% recovery) = 6.6 mg/L Anti-scalant dose (60% recovery) = 6.6 mg/L Biocide dose = 200 mg/L for 30 min, once per week (Nalco Permaclean PC-11) Time between CIPs = 1 to 2 months Flux rate (50% recovery) = 23 lmh (normalized to 25°C) CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 78 of 80 6.4 Primary Factors Impacting Process Performance 6.5 Presence of algae growth in feed water (pond water vs. well head source) Iron scaling of the UF membrane Water pH in the Oxidation/ Precipitation stage Coagulant dose UF flux rate Effectiveness of UF CEBs and CIPs Flushing of RO immediately after shutdown (precipitation from stagnant water will occur due to loss of effectiveness of anti-scalants over extended period) RO influent pH Iron and barium scaling of the RO membrane RO recovery RO anti-scalant type and dosage High TDS in the RO feed water resulted in high osmotic pressure, which was the primary factor which limited RO recovery to the 50% to 60% range examined in the pilot Stability of Operation Untreated Basal Water Basal feed water undergoes significant variation in Oxidation-Reduction potential immediately after exiting the well head. Aeration combined with equalization ahead of a treatment facility should be able to effectively counteract this issue and provide stable feed water. UF Fouling rate on the UF membrane is critical and susceptible to exponential increases if upstream chemistry is not optimized. Due to the high scaling nature of the water, cross flow operation of the membrane is deemed essential, in order to provide physical scouring of the membrane surface and extend production run times between CEBs and CIPs. Normalized (to 20°C) flux rates in excess of 53 lmh were not appropriate for this application due to the scaling tendencies of the feed water. Carrying out a CIP was effective in removing fouling material and restoring UF performance. However, the UF autopsy indicated that the use of a cleaning chemical targeting iron deposits may provide additional benefits. RO RO operation was stable and sustainable at a recovery of 50%, even when the upstream UF system was experiencing scaling issues. Operation at 60% recovery was also relatively stable, though examined for a significantly smaller timeframe. Anti-scalant type and dose could be re-examined in order to address iron, which was identified as the primary scaling compound. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 79 of 80 6.6 Comparison of Operation with Pond and Wellhead Basal Water Sources Pond water use was explored in the pilot due to the presumed benefits of water equalization and water aging (introduction of oxygen into the water from the atmosphere). However, the presence of significant algae in the pond water was a dominant factor which ultimately resulted in an immediate negative impact on UF performance Key differences between untreated basal water taken from the pond relative to basal water taken from the wellhead were as follows: Easily oxidized compounds had been oxidized and in some cases precipitated out of solution Reduced dissolved hydrogen sulphide Algae in the water was significant and easily observable in both water at the pilot plant and in the source pond Organic materials (algae) were most probably responsible for the immediate and rapid decrease in UF performance when basal water source was changed from the wellhead common header to directly from the pond 6.7 Impact of Not Softening Softening and degasification were initially contemplated for inclusion in the treatment train, but were ultimately not included due to the extremely high chemical consumption anticipated. Exclusion of softening eliminates the capital costs for softening infrastructure as well as the significant ongoing costs related to chemicals required for the treatment process and sludge disposal. The primary adverse impacts of not carrying out upstream softening vary based on the operational pH used in the oxidation/precipitation treatment stage. At neutral pH (6.8 to 7.0) the impacts were as follows: increased iron fouling of the UF membrane, potentially requiring frequent CEBs reduced or near eliminated issues with CaCO3 scaling on pilot plant infrastructure At elevated pH (7.4 to 8.0) the impacts were as follows: reduced impact of iron fouling on the UF membrane severe CaCO3 precipitation throughout the pilot facility, often requiring equipment such as pre-filters and pumps to be taken off line for descaling The use of anti-scalant chemicals, metabisulphite and neutral pH upstream of the RO was effective in mitigating the impact of high hardness on the RO system. However, high hardness levels in RO reject are also a major consideration in disposal of the waste stream. CNRL EWTP Pilot - Basal Water Treatment Phase CONFIDENTIAL Ver 2.0 May 29, 2013 80 of 80