26842_JOT Winter 2007_e book
Transcription
26842_JOT Winter 2007_e book
SaudiAramco Journal Of Technology A quarterly publication from the Saudi Arabian Oil Company AN EXPERIMENTAL STUDY OF HOLE CLEANING UNDER SIMULATED DOWNHOLE CONDITIONS see page 2 Saudi Aramco Journal of Technology CASE HISTORY: APPLICATION OF COILED TUBING TRACTOR TO ACID STIMULATE OPEN HOLE EXTENDED REACH POWER WATER INJECTOR WELL see page 17 WINTER 2007 Elevated temperature and pressure drilling fluids flow loop, known as Advanced Cuttings Transport Facility (ACTF) is located at the University of Tulsa, OK where the experiments were conducted. On the Cover An aerial view is shown of a Drilling Rig in operation. Saudi Aramco currently operates more than 120 Drilling Rigs. This is the largest number of Drilling Rigs in operation, not only in Saudi Aramco’s history, but in any oil company’s history anywhere. WINTER 2007 The Saudi Aramco Journal of Technology is published quarterly by the Saudi Arabian Oil Company, Dhahran, Saudi Arabia, to provide the company’s scientific and engineering communities a forum for the exchange of ideas through the presentation of technical information aimed at advancing knowledge in the hydrocarbon industry. An Experimental Study of Hole Cleaning Under Simulated Downhole Conditions Complete issues of the Journal in PDF format are available on the Internet at: http://www.saudiaramco.com (click on “publications”). Case History: Application of Coiled Tubing Tractor to Acid Stimulate Open Hole Extended Reach Power Water Injector Well SUBSCRIPTIONS Send individual subscription orders, address changes (see page 75) and related inquiries to: Saudi Aramco Public Relations Department JOT Distribution Box 5000 Dhahran 31311, Saudi Arabia Fax: +966/3-873-6478 Web site: www.saudiaramco.com EDITORIAL ADVISORS Isam A. Al-Bayat, Vice President, Engineering Services Mohammed S. Al-Gusaier, Vice President, Refining Abdulla A. Al Naim, Vice President, Exploration Amin H. Nasser, Vice President, Petroleum Engineering and Development Zuhair A. Al-Hussain, Executive Director, Drilling and Workover Saad A. Al-Turaiki, Executive Director, Southern Area Gas Operations Khaled A. Al-Buraik, Chief Petroleum Engineer Abdullah M. Al-Ghamdi, Manager, Berri Gas Plant Khalil A. Al-Shafei, Manager, Materials Planning and Systems Salahaddin H. Dardeer, Superintendent, Riyadh Refinery Engineering Abdulmuhsen A. Al-Sunaid, Senior Engineering Consultant, Environmental Protection CONTRIBUTIONS Relevant articles are welcome. Submission guidelines are printed on the last page. Please address all manuscript and editorial correspondence to: EDITOR William E. Bradshaw The Saudi Aramco Journal of Technology Room 2014 East Administration Building Dhahran 31311, Saudi Arabia Tel: +966/3-873-5803 E-mail: [email protected] Unsolicited articles will be returned only when accompanied by a selfaddressed envelope. Abdallah S. Jum‘ah President & CEO, Saudi Aramco 2 Dr. Maher M. Shariff, David Nakamura, Dr. Mengjiao Yu and Dr. Nicholas E. Takach 17 Ayedh M. Al-Shehri, Saad M. Al-Driweesh, Mazen Al-Omari and Samer Al-Sarakbi Identifying Sources of Amine Foaming Through Detailed Troubleshooting Provides More Feasible Solutions 24 Mater A. Al-Dhafeeri SmartWell Completion Utilizes Natural Reservoir Energy to Produce High Water-Cut and Low Productivity Index Well in Abqaiq Field 33 Nashi Al-Otaibi, Abdulwafi A. Al-Gamber, Michael Konopczynski and Suresh Jacob Shaft Misalignment and Vibration - A Model 41 Dr. Irvin Redmond New Coating Generations Offer Effective Solutions for Rehabilitation of Buried Pipelines 52 Dr. Moufaq I. Jafar, Faisal M. Melibari and Dr. Fikry F. Barouky Production Optimization Through Utilization of Innovative Technologies in an Offshore Field Environment 58 Konstantinos I. Zormpalas, Khalid Al-Omaireen and Karam Sami Al-Yateem Crosswell Electromagnetic Tomography in Haradh Field: Modeling to Measurements 65 Dr. Alberto F. Marsala, Dr. Saleh Al-Ruwaili, Dr. Shouxiang Mark Ma, Modiu Sanni, Zaki Al-Ali, Jean-Marc Donadille and Dr. Michael Wilt Mustafa A. Jalali Vice President, Saudi Aramco Affairs Ziyad M. Alshiha Manager, Public Relations Production Coordination: Alan Dodd, ASC Design: Pixel Creative Group, Houston, Texas, U.S.A. ISSN 1319-2388. © COPYRIGHT 2007 ARAMCO SERVICES COMPANY. ALL RIGHTS RESERVED: No articles, including art and illustrations, in The Saudi Aramco Journal of Technology, except those from copyrighted sources, may be reproduced or printed without the written permission of Saudi Aramco. Please submit requests for permission to reproduce items to the editor. The Saudi Aramco Journal of Technology gratefully acknowledges the assistance, contribution and cooperation of numerous operating organizations throughout the company. SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 1 An Experimental Study of Hole Cleaning Under Simulated Downhole Conditions Dr. Maher M. Shariff David Nakamura Dr. Mengjiao Yu Dr. Nicholas E. Takach Dr. Maher M. Shariff received a B.S. in Mechanical Engineering from Bradley University, IL in 1989, a M.S. in Mechanical Engineering from Washington University, MO in 1991, and a Master of Engineering from Vanderbilt University, TN in 1996. He received a Ph.D. in Mechanical Engineering with highest honors from Wichita State University, KS in 2000, in association with the National Institute for Aviation Research (NIAR). Dr. Shariff’s dissertation work was in the area of Computational Fluid Dynamics (CFD). From September 2000 to September 2001, he worked as an Analytical Design Engineer at Cessna Aircraft Company (a Textron Company) in Wichita, KS. In September 2001, he joined SABIC Research and Technology Center in Jubail, Saudi Arabia where he stayed until February 2003. Then he joined Saudi Aramco’s R&D Center in February 2003, and is currently working as a Research Scientist in the R&D Division. His research interests lie in the areas of drilling and completion fluids as well as gas/water/oil separation. Dr. Shariff is credited with more than 10 regional and international publications and presentations. He is a member of numerous professional societies; ASME, SPE and ACS. He is currently serving as the Vice-Chair of the ASME Eastern Saudi Arabia Section. Dr. Shariff is also a member in a myriad of honor societies, to name a few, Sigma Xi (Scientific Research), Tau Beta Pi (Engineering) and Phi Kappa Phi (Academic). David Nakamura graduated with a B.S. degree in Petroleum Engineering from the University of Oklahoma, OK in 1986 and a M.S. degree from the University of Alaska-Fairbanks, AK in 1996. He worked for 2 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 Saudi Aramco for 2½ years from 2004-2006 in the Drilling Technology group. Prior to Saudi Aramco, he worked in Alaska, Kuwait, Houston, Angola and Azerbaijan. David is currently working as a Drilling Engineer in Azerbaijan, offshore in the Caspian Sea. He is a member of the Society of Petroleum Engineers (SPE). Dr. Mengjiao Yu is assistant professor of Petroleum Engineering at the University of Tulsa, OK. He received his M.S. degree in Electrical and Computer Engineering and his Ph.D. degree in Petroleum Engineering from the University of Texas at Austin, TX. Dr. Yu also holds a B.S. degree in Chemistry and a M.S. degree in Chemical Engineering. Dr. Yu’s current research interests are in drilling fluids, cuttings transport, wellbore stability, rheology of fluids, and petroleum chemistry. He is a member of the Society of Petroleum Engineers (SPE). Dr. Nicholas E. Takach is an Associate Professor of Chemistry at The University of Tulsa, OK. He received his B.S. degree in Chemistry from California State Polytechnic University, CA and a Ph.D. in Inorganic Chemistry from the University of Nevada, NV. Dr. Takach joined TUDRP in 1996 and became Associate Director in January, 1999. His research interests include the physico-chemical properties of drilling and completion fluids, surface and environmental chemistry applied to the petroleum industry and thermodynamic modeling of natural gas stability in ultra-deep reservoirs. Dr. Takach has published in both chemistry and petroleum-related journals, and has given presentations in both areas at national and international conferences. He is a member of the Society of Petroleum Engineers (SPE) and the American Chemical Society (ACS). Dr. Takach is also a member of Sigma Xi, the Scientific Research Honor Society. ABSTRACT With increasing measured depths and horizontal displacements in extended-reach, high-angle wells, hole cleaning remains one of the major factors affecting cost, time and quality of directional, horizontal, extended reach and multilateral oil/gas wells. This study involves experimental research and theoretical analysis to enhance cuttings transport capacity in oil and gas well drilling operations. The effects of drilling fluid rheology, mud density, temperature, borehole inclination, pipe rotation, eccentricity, rate of penetration (ROP) and flow rates were investigated experimentally. Volumetric cuttings concentration in the test section and frictional pressure losses were measured during the tests using two nuclear densitometers and a differential pressure transducer. A total of 116 experiments were conducted on a full- scale, Elevated-Pressure Elevated-Temperature Flow Loop (57.4 ft long, 5.76” x 3.5” annular section) at the University of Tulsa under controlled experimental conditions (up to 200 ºF and 2,000 psi). Experimental results show that drill pipe rotation, temperature and rheological parameters of the drilling fluids have significant effects on cuttings transport efficiency. A dimensional analysis was conducted in this study to develop correlations that can be used for field applications. A user-friendly simulator was developed based on the results of the dimensional analysis and correlations. This simulator can be used by drilling engineers for design and sensitivity study. Results from this study can be used to determine critical conditions for efficient hole cleaning, as well as to optimize the mud program during the planning and operational phases of drilling. INTRODUCTION As the need for directional and horizontal wells increased, the interest in cuttings transport problems has shifted from vertical to inclined and horizontal geometries in the last 20 years. With increasing measured depths and horizontal displacements in extended reach high angle wells, good hole cleaning remains one of the major factors affecting cost, time and quality of directional, horizontal, extended reach and multilateral oil/gas wells, during both the drilling and completion phases. It has been recognized for many years that removal of cuttings from the wellbore during drilling of highly inclined wells poses special problems. Poor hole cleaning can result in expensive drilling problems such as a stuck pipe, lost circulation, slow drilling, high torque and drag, loose control on density, poor cement jobs, problems running lower completions, etc. If the situation is not handled properly, the problem can lead to loss of the well. Although cuttings transport in horizontal and inclined wells has been studied for many years, inefficient cleaning of the wellbore remains one of the most serious problems in drilling operations. To address deep gas drilling operations in Saudi Aramco, continuous hole cleaning problems have been reported when drilling 83⁄8” and 57⁄8” horizontal holes through carbonate and sandstone formations. In one well, when drilling an 83⁄8” hole through the sandstone formation, high rotational torque was generated due to cuttings bed buildup. It took approximately five days to drill 519 ft at a very high cost after the hole was properly cleaned and torque was reduced. This study involves experimental research and data analysis to enhance cuttings transport capacity in oil and gas well drilling operations. Results from this research will be used to predict the critical conditions for efficient hole cleaning. SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 3 Rheology of Fluid Much has been written about the role of drilling fluids in the cuttings transport literature1, 2, 3. These studies and others debated high viscosity vs. low viscosity and which rheological parameters are most useful for characterizing hole cleaning efficiency. Due to the lack of consensus on the selection of the drilling fluid rheological properties, a variety of fluids with different rheological parameters and densities were selected for this study. Past work1, 2, 3 indicates that the rheological parameters of the drilling fluid play an important role in controlling wellbore hydraulics and cuttings transport efficiency. Therefore, characterization of the fluids in terms of the rheological parameters is of great importance in this study. As of now, no single rheology model has been proved to describe exactly the shear stress-shear rate relationships of all non-Newtonian fluids over all ranges of shear rate. As a practical consideration, there are many situations4, 5 where a different rheology model can be found to approximate the behavior of an actual fluid (within certain ranges) with accuracy commensurate with the reproducibility of measured field data. Among the existing models, some have gained widespread usage in the oil industry. They are the Ostwald-de-Walle5 or Power Law Model: (1) The Bingham Plastic Model6: (2) The Herschel-Buckley or Yield Power Law Model: (3) Other models such as the Robertson-Stiff Model have found applications, specifically in the cementing industry, and were shown7 to provide a good fit to rheological data. The Bingham Plastic Model was adopted to characterize the fluids in this study based on the information provided. Effect of Density There are very limited tests conducted in the past to investigate the effects of drilling fluid density. On the basis of tests conducted8 it was concluded that, although limited (in terms of number of experiments conducted), mud weight has a significant effect on hole cleaning, with or without pipe rotation. As shown in Fig. 1, we see that at horizontal conditions, the cuttings weight remaining in the test section during erosion tests is considerably reduced, as the weight of the fluid is increased from 7 lb/gal to 13.7 lb/gal. 4 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 Cuttings wt (lbs) remaining in annulus BACKGROUND 2000 1800 1600 1400 1200 1000 800 600 400 200 0 5 7 9 11 13 15 Mud Weight, lb/gal. Fig. 1. Cuttings Weight vs. Mud Weights8. The effects of the mud density were investigated in this study. Both low density fluids (polymeric fluid and water) and weighted mud (density increased with barite) were tested on the full-scale elevated pressure, elevated temperature flow loop (hereafter referred to as the ACTF (Advance Cuttings Transport Facility)) to study the effects of mud density. Effect of Pipe Rotation Pipe rotation influences the cuttings bed erosion significantly9. Results indicate that rotation produces a velocity profile difference that makes bed erosion easier. Optimizing the use of rotation can also contribute to an improvement of drilling efficiency. Sanchez, et al.9, focused on investigating the effects of drill pipe rotation in hole cleaning. Their study shows that the effect of drill pipe rotation is significant and promising enough that it should not be neglected. Thus to understand the effect of pipe rotation on the cutting transport efficiency, pipe rotation was added to the test matrix in this project. Effect of Temperature Data collected over the years shows that the drilling fluid viscosities vary with temperature and pressure. Recent experiments10 done on cuttings transport by using water as the test fluid at the University of Tulsa suggest that cuttings transport is significantly affected by a change in temperature. Lab experiments also show that the rheology of drilling fluids changes significantly with temperature. Due to the change of rheological properties of the drilling fluids, viscous drag forces applied on drilled cuttings will be significantly changed. Therefore, effects of temperature on cuttings transport were considered in this study. Other Parameters Borehole inclination angle, rate of penetration (ROP), pipe eccentricity and flow rates of the drilling fluids were also considered and tested in this project. Compressed Air Tank Injection Tower F1 Metering Pump F3 CV5 Air Compressor F2 Multiphase Pump Fracturing Pump (Mud Pump) Cooling Tower 2-inch Pipe Cooler 3-inch Pipe Storage Tank Heater Boiler Mud Tank Air Expansion Tank V1 DN1 DN2 V3 CV2 Seperation Tower CV3 Centrifugal Pump Annular Section V3 4-inch Pipe Fig. 2. Schematic of the ACTF flow loop. E X P E R I M E N TA L S E C T I O N Experimental Setup Fig. 3. ACTF flow loop. Fig. 4. Centrifugal pump. This experimental study was conducted at the ACTF flow loop (Figs. 2 and 3) of the University of Tulsa. The test facility consists of: 1) pump system, 2) heating and chilling system, 3) cuttings injection/collection system, 4) piping system, 5) test section measurement system, 6) storage tanks, and 7) data acquisition and control systems. A simplified schematic drawing of the flow loop is shown in Fig. 2. The pump system consists of four pumps: a centrifugal, a triplex (Halliburton), a multiphase (Moyno), and a water metering pump. The centrifugal pump shown in Fig. 4 takes water from a 100 bbl holding tank and is used to feed a water metering pump (200 psi, 100 gpm max). The discharge pressure from the air compressor has a maximum Fig. 5. Polymer mixing system. SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 5 Fig. 6. Primary tank (Polymer tank). Fig. 8. Heat exchanger. Fig. 7. Secondary tank (Water tank). of 200 psi. Water and air are mixed at the suction side of the multiphase pump, which then compresses the mixture. The multiphase pump can provide a maximum differential pressure of 500 psi. Flow rate is controlled by a control valve and the multiphase pump rotational speed. Polymeric solutions were pre-mixed, using the mixing system shown in Fig. 5 in the 100 bbl primary tank (Fig. 6) and water was stored in the secondary tank, Fig. 7. After polymer solution flows through the pipes and annulus, it reaches the section between the outlet of the 4” pipe and injection tower. The piping system of the ACTF flow loop consists of: 1) a 2” pipe, 52.9 ft in length, 2) a 3” pipe, 52.9 ft in length, 3) a 4” pipe, 66.6 ft in length, and 4) an annular section (5.76” x 3.5”), 57.4 ft in length. On each of the 2” and 3” pipes, and in the annular section, view ports are installed to offer online visual observation of flow behavior. Most of the flow lines are covered with heat insulation material, which maintains the loop at the desired temperature. The heating system includes: 1) an indirect-fired natural 6 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 Fig. 9. Cuttings injection tank. gas boiler, 2) an oil circulation tank, 3) two heat exchangers, Fig. 8, and 4) an automatic control/alarm system. The test fluid can be heated up to 200 °F. The cuttings injection and collection systems (Figs. 9 and 10) consist of: 1) an injection tower, 2) a separation (and collection) tower, 3) a transfer auger to load cuttings into the injection tower, 4) an injection auger to feed cuttings into the flow loop, and 5) a weight measurement system. The injection tower is 22 ft high, and is used to hold cuttings. The collection (or separation) tower, is 36 ft in height, and separates fluids from solids. The cuttings are loaded into the top of the injection tower with a transfer auger. A motor-driven injection auger is installed at the bottom of the injection tower in a vertical position. By turning this auger, cuttings are fed into the 4” pipe, which is below the injection tower; then the cuttings are carried by Fig. 12. Data acquisition system. Fig. 10. Cuttings collection tank. When steady-state flow is established in the annular section, the pressure differential in the annulus increases from a lower value to a higher value and stabilizes, and the pressure differential in the 4” pipes continues to increase. At that point, quick-close valves are closed nearly simultaneously. At the same time, a bypass valve is opened to allow the mixture to flow directly to the collection tower. This enables a certain amount of water/cuttings to be trapped in the annular test section. Two nuclear densitometers measure the mixture density, which, in turn, can be used to back calculate the volumetric concentrations of each phase. A flushing system is installed in the annular section. The purpose of the flushing line is to measure the weight of cuttings trapped in the annular section. Two tanks are included in the ACTF flow loop: one to hold the polymeric test solution, Fig. 6, and the second to hold water, Fig. 7, for the tests and for clean up. The capacity of each tank is 100 bbl. Both tanks are covered with heat insulation material to minimize heat losses. A Labview® data acquisition system is installed to monitor and control tests as shown in Fig. 12. Preparation of Testing Fluids Fig. 11. Test section. water. The weight measurement system consists of load cells, transducers, and an indicator. At the bottom of the injection and collection towers, there are three load cells, installed at 120° apart, to measure the weight of each tower. The real time readings of the weight can be shown on the indicators and a computer screen in the control room. This enables the cuttings injection and collection rates to be known and controlled. The annular test section, Fig. 11, has five components: 1) two-quick closing valves, 2) one bypass valve, 3) two nuclear densitometers, 4) flushing lines, and 5) an expansion tank. Two polymers, polyanionic cellulose (PAC) and dispersible xanthan gum (XCD) were used in this project to control the rheological parameters, yield point (YP) and plastic viscosity (PV), of the testing fluids. To prepare the testing fluids, the polymer mixing tank was first filled with water and heated to the testing temperature. PAC was dissolved in the water using a mixer. The amount of PAC was predetermined in the lab on a small scale. After the PAC was mixed, XCD was added to adjust the yield point and plastic viscosity. After adding the polymers, the fluid was agitated for at least 40 minutes for hydration. After the mixing, a sample was taken from the mixing tank for characterization. Based on the SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 7 Testing Parameter Values Annular Size 5.76” Casing ID x 3.5” Drill String OD Rotation (rpm) 0 Eccentricity Mud Rheology Fluid Label Yield Point 20, 40 lb/100 ft2 Plastic Viscosity 10, 20 cP Density, (lb/gal) Plastic Viscosity, (cP) Yield Point (lb/100 ft2) Fluid A 10 20 8.33 Fluid B 20 40 8.33 Fluid C 20 40 12 80 0.541,” 0.881” offset Rheological Parameters Temperature (ºF) 80, 120, 180 Fluid D 10 20 12 ROP (ft/hr) 15, 20, 30, 40 Water 1 0 8.33 Flow Rate (GPM) 75~250 Table 2. Different fluids used Density (ppg) 8.3 12 Inclination (degrees) 90 67 Table 1. Test matrix measured yield point and plastic viscosity, additional polymer or water was added to adjust the rheological parameters to the predetermined values. High density fluids were prepared in the mixing tank of an adjoining loop called the Low-Pressure Ambient Pressure flow loop. Again, polymers were first added to the heated water and then agitated for at least 40 minutes for hydration. An Excel® program was developed to calculate the amount of barite needed for increasing the density of the testing fluid. Barite was added to the pre-mixed polymeric fluid to increase the density of the testing fluid to 12 ppg. The weighted fluid was agitated for at least 40 minutes before a sample was taken. A mud balance was used to make sure the density of the fluid was 12 ppg. Also, Variable rheological parameters were measured to make sure the desired yield point and plastic viscosity were reached. Below is the generic procedures used to prepare 70 bbls of testing fluid. 1. Prefill 60.36 bbl heated water to low pressure mixer. 2. Add 44.12 pound mass (lbm) PAC (30/40 rheology) or 9.8 lbm PAC (10/20 rheology). 3. Add 68.65 lbm XCD (30/40 rheology) or 39.2 lbm XCD (10/20 rheology). 4. Mix well for 40 minutes. 5. Check the rheology (verify the number before adding barite). 6. Add 14,173.5 lbm barite (141.7 bags). 7. Mix well for at least 40 minutes. 8. Check the rheology and density. Characterization of Testing Fluids A Chandler 35 rotational viscometer (see Fig. 16 in Symbol Units 1. Cuttings Volumetric Concentration Cc 2. Wellbore Diameter Dimensions M L T Dimensionless 0 0 0 D Length 0 1 0 d Length 0 1 0 Vsl Length/Time 0 1 -1 5. Hole Angle (Inclination) θ Dimensionless 0 0 0 6. Drill Pipe Rotation Speed Ω 1/Time 0 0 -1 7. Plastic Viscosity PV Mass/(Length*Time) 1 -1 -1 8. Yield Point YP Mass/(Length)2 1 -1 -2 9. Fluid Density ρ Mass/(Length)3 1 -3 0 10. Acceleration due to Gravity g Length/(Time)2 0 1 -2 ROP Length/Time 0 1 -1 e Length 0 1 0 Tact/Tst Dimensionless 0 0 0 3. Drill Pipe Diameter 4. Superficial Liquid Velocity, 4Q/Pi (D2-d2) 11. Injection Rate 12. Eccentricity 13. Tactual/Tstandard (Dimensionless Temperature) Table 3. Dimensional analysis 8 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 Appendix A) was used to measure the rheological parameters of the testing fluids under ambient temperature and pressure. A Fann 75 (see Fig. 17 in Appendix A) was also used in this study to measure the rheological parameters at high-pressure, high temperature conditions. Although the Bingham Plastic rheological model was adopted for this study, the prepared testing fluid was tested under 1, 2, 3, 6, 10, 20, 30, 60, 100, 200, 300 and 600 rpm and the dial readings were recorded. Yield point and plastic viscosity were calculated to make sure that desired rheological parameters were reached. Test Procedure The experiments contain the following major steps. The detailed test procedure can be found in Appendix B. • Prepare testing fluids. • Mix polymer. • Add Barite to increase mud density (when necessary). • Circulate fluid through the flow loop and control the test temperature. • Inject cuttings at the desired injection rate. • Wait for the steady-state by monitoring the differential pressure transducers (DP) and densitometers on the test section. • Flush the cuttings and clean up. Test Matrix After conducting some pilot tests, the following test matrix (Table 1) was determined for use in this study for a better understanding of the hole cleaning process. R E S U LT S A N D D I S C U S S I O N Fluid Characterization As mentioned, fluid characterization was performed to determine the effects that different rheological parameters have on cutting transport. As a result of the fluid characterization tests performed using Chandler 35 and Fann 75 viscometers; the following table describes the five different fluids used in the experiments. Physical properties of the fluids used are shown in Table 2. Summary of the Tests Completed on the ACTF Flow Loop A total of 116 tests were conducted in this study. Table 7 in Appendix C, shows in detail all the tests conducted in this project. Dimensional Analysis A dimensional analysis was conducted to develop correlations that can be used to predict the cuttings volumetric concentration in the annulus based on the experimental data. In order to account for the effects of the independent variables (liquid flow rate, cuttings size, hole angle, fluid properties, temperature, eccentricity and drill pipe rotational speed), the following 13 variables, Table 3, are used in dimensional analysis for cuttings volumetric concentration. The unit of each variable in terms of the three basic dimensions (M, L and T) is listed in Table 3. Dimensional analysis is performed as follows: Dimensions Involved: [MLT] = 3 No. of Dimensional groups: 13-3 = 10 Terms Used: 1. 2. 3. 4. (Ratio of equivalent diameter to hydraulic diameter) (Equivalent diameter of annulus) (Ratio of inner to outer diameter of the annulus) (Hydraulic diameter) Correlations for Cuttings Volumetric Concentration All experimental results were considered in the dimensional analysis. The above dimensionless groups indicate all the parameters that are likely to affect the correlation for cuttings concentration. This is established by examination of the experimental results. Correlations for “Polymer” and “Weighted PAC” (both these terms are used to describe the fluid types used in the tests) may have to be developed separately because one model may not be able to accommodate both fluids. The effects of flow rate are reflected both in Re and Fr. Since the yield point, the plastic viscosity and the density of the fluids were varied for the experiments under study; both of these dimensionless groups were used in the correlation. Since the influence of different wellbore/pipe diameter ratios is not studied here, the dimensionless group π6 was not included in the correlation. Since pipe rotation has shown to have a significant effect on the cuttings concentration, Ta (Taylor number) was included in the regression analysis. A generalized Taylor number, Ta, was used for Bingham Plastic fluids as described in the above Table. The effect of temperature on the cuttings concentration was also considered in the dimensional analysis. We first considered incorporating the effect of temperature by developing several separate regression models for the effect of temperature on the rheological parameters of the fluids SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 9 transport was incorporated by using the Hedstrom number, He, in the regression analysis. The effect of variation of injection rate was incorporated by Drp, the dimensionless rate of penetration. The dimensionless rate of penetration is typically represented by the equation: 0.50 0.45 0.40 Prediction 0.35 0.30 0.25 0.20 (4) 0.15 0.10 0.05 0.00 0.00 0.10 0.20 0.30 0.40 0.50 Observed Due to the lack of sufficient information, the current form as shown in the Table 4 was adopted. The effect of variation in eccentricity is represented by Decc, dimensionless eccentricity, represented by the equation shown in Table 4. Fig. 13. Observed vs. predicted cuttings concentration for polymer solution. No. Dimensionless Group Remarks 35% 30% π1 Taylor number, Ta Predicted 25% π2 20% Cc Cuttings Concentration 15% 10% π3 Hedstrom number, He π4 Generalized Reynolds number, Regen 5% 0% 0% 5% 10% 15% 20% 25% 30% 35% Observed Fig. 14. Observed vs. predicted cuttings concentration for water. π5 T(actual)/T(standard) Temperature Ratio, Tr π6 d/D Rd π7 Froude number, Fr π8 Dimensionless Inclination Angle, α π9 Drp (Dimensionless ROP) π10 Decc (Dimensionless Eccentricity) Table 4. Dimensionless groups Fig. 15. Cuttings transport simulator. alone. But this may complicate the analysis of cuttings transport. Therefore, a temperature ratio, Tr, was used in the regression analysis. The effect of the rheological parameters on cuttings 10 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 k b1 b2 b3 b4 39541 -0.914 -0.275 -0.090 -1.093 b5 b6 b7 b8 -1.335 -0.803 0.287 -0.534 Table 5. Parameters for the above model k b1 b2 b3 b4 b5 0.062 -1.31 0.157 0.165 0.045 -0.0043 Table 6. Parameters for the above model Appendix A. Rotational Viscometers used in this Study Appendix B. Experimental Procedure Diagram Preparation Stage Estimated Time (4 hours) Check fuel level Heat water Mix polymer Heat polymer Check the loop and fluid path Cutting Transport Test Circulate the fluid Set the test pressure Test rheology at steady-state Set cuttings injection rate Set pipe rotation speed Steady-state Vary flow rate (until pipe is clean) Stop pipe rotation and cuttings injection Decrease the pressure slowly Stop mud pump Fig. 16. Chandler 35 Viscometer. Cleaning up the loop and maintenance Estimated Time (2 hours) Flush out and drain cuttings from loop and tanks Rinse loop with water Fill tanks #1 and #2 with fresh water Fill fuel tanks of mud pump and compressor Clean the floor Check the loop piping and valves Fig. 17. Fann 75 Viscometer. The relationship between these dimensionless groups for cuttings volumetric concentration is expressed as (5) A N A LY S I S An attempt was made to combine all 116 tests together to obtain one equation. The following equation was adopted to correlate the experimental data. Using Statistica®, the model parameters were obtained and are shown Tables 5 and 6. Overall Correlation for 116 Tests (6) Figure 13 shows the comparison between model predictions with the experimental data using polymer solutions. Water Test In the case of water, the He (Hedstrom number), Alpha Download and backup the data (Dimensionless Inclination), and the Decc (Dimensionless Eccentricity) were removed from the analysis since they are all constant. The Taylor number (Ta) was modified for water and has the following form: (7) The generalized Reynolds number was also modified for water and has the following form: (8) Using Statistica we obtain: (9) Figure 14 shows comparison of experimental data and SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 11 Appendix C Pipe Flow Rate Rotation Inclination gpm RPM 0 100 90 TEST No. Density lb/gal PV, μp YP, lb/100 ft2 Temperature ROP fph Eccentricity Cc 1 8.314 10 20 80 30 2 8.314 10 20 80 30 0 200 90 0.881 35% 0.881 14% 3 8.314 10 20 80 30 80 100 90 0.881 6% 4 8.314 10 20 80 30 80 200 90 0.881 2% 5 8.314 10 20 180 30 0 100 90 0.881 11% 6 8.314 10 20 180 30 0 200 90 0.881 4% 7 8.314 10 20 180 30 80 100 90 0.881 15% 8 8.314 10 20 180 30 80 200 90 0.881 0% 9 8.314 20 40 180 30 0 100 90 0.881 20% 10 8.314 20 40 180 30 80 100 90 0.881 15% 11 8.314 20 40 180 30 0 200 90 0.881 0% 12 8.314 20 40 180 30 80 200 90 0.881 0% 13 8.314 20 40 80 30 0 100 90 0.881 30% 14 8.314 20 40 80 30 80 100 90 0.881 9% 15 8.314 20 40 80 30 0 200 90 0.881 0% 16 8.314 20 40 80 30 80 200 90 0.881 0% 17 12 20 40 80 30 0 100 90 0.881 19% 18 12 20 40 80 30 80 100 90 0.881 1% 19 12 20 40 80 30 0 150 90 0.881 5% 20 12 20 40 80 30 80 150 90 0.881 0% 21 12 20 40 180 30 0 100 90 0.881 1% 22 12 20 40 180 30 80 100 90 0.881 0% 23 12 10 20 80 30 0 100 90 0.881 17% 24 12 10 20 80 30 80 100 90 0.881 1% 25 12 10 20 80 30 0 150 90 0.881 8% 26 12 10 20 80 30 80 150 90 0.881 0% 27 12 10 20 180 30 0 100 90 0.881 15% 28 12 10 20 180 30 80 100 90 0.881 1% 29 12 10 20 180 30 0 150 90 0.881 3% 30 12 10 20 180 30 80 150 90 0.881 0% 31 12 20 40 180 30 0 150 90 0.881 1% 32 12 20 40 180 30 80 150 90 0.881 0% 33 8.314 10 20 180 30 0 100 67 0.881 32% 34 8.314 10 20 180 30 0 200 67 0.881 4% 35 8.314 10 20 180 30 80 100 67 0.881 23% 36 8.314 10 20 180 30 80 200 67 0.881 1% 37 8.314 10 20 80 30 0 100 67 0.881 17% 38 8.314 10 20 80 30 80 100 67 0.881 27% 39 8.314 10 20 80 30 0 200 67 0.881 12% 40 8.314 10 20 80 30 80 200 67 0.881 12% 41 8.314 20 40 180 30 0 100 67 0.881 34% 42 8.314 20 40 180 30 80 100 67 0.881 22% 43 8.314 20 40 80 30 0 100 67 0.881 41% 12 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 Pipe Flow Rate Rotation Inclination gpm RPM TEST No. Density lb/gal PV, μp YP, lb/100 ft2 Temperature ROP fph Eccentricity Cc 44 8.314 20 40 80 30 80 100 67 0.881 19% 45 8.314 20 40 80 30 0 200 67 0.881 12% 46 8.314 20 40 80 30 47 8.314 20 40 180 30 80 200 67 0.881 1% 0 200 67 0.881 10% 48 8.314 20 40 180 49 12 20 40 80 30 80 200 67 0.881 5% 30 0 100 67 0.881 21% 50 12 20 40 51 12 20 40 80 30 80 100 67 0.881 4% 80 30 0 150 67 0.881 11% 52 12 10 20 80 30 0 100 67 0.881 17% 53 12 54 12 10 20 80 30 0 150 67 0.881 4% 10 20 80 30 80 150 67 0.881 0% 55 56 12 10 20 80 30 80 100 67 0.881 0% 12 10 20 180 30 0 100 67 0.881 22% 57 12 10 20 180 30 0 150 67 0.881 13% 58 12 10 20 180 30 80 100 67 0.881 2% 59 12 10 20 180 30 80 150 67 0.881 0% 60 12 20 40 180 30 0 100 67 0.881 14% 61 12 20 40 180 30 80 100 67 0.881 0% 62 12 20 40 180 30 0 150 67 0.881 4% 63 12 20 40 180 30 80 150 67 0.881 0% 64 8.314 10 20 180 40 0 100 90 0.541 25% 65 8.314 10 20 180 40 0 150 90 0.541 18% 66 8.314 10 20 180 40 0 200 90 0.541 5% 67 8.314 10 20 180 40 0 250 90 0.541 0% 68 8.314 10 20 120 40 0 100 90 0.541 28% 69 8.314 10 20 120 40 0 150 90 0.541 22% 70 8.314 10 20 120 40 0 200 90 0.541 14% 71 8.314 10 20 120 40 0 250 90 0.541 5% 72 8.314 10 20 120 40 80 75 90 0.541 6% 73 8.314 10 20 120 40 80 100 90 0.541 5% 74 8.314 10 20 120 40 80 150 90 0.541 3% 75 8.314 10 20 120 20 80 75 90 0.541 11% 76 8.314 10 20 120 20 80 100 90 0.541 7% 77 8.314 10 20 120 20 80 150 90 0.541 0% 78 8.314 10 20 120 20 0 100 90 0.541 20% 79 8.314 10 20 120 20 0 150 90 0.541 16% 80 8.314 10 20 120 20 0 200 90 0.541 2% 81 8.314 10 20 120 20 0 250 90 0.541 0% 82 12 20 40 180 30 80 150 67 0.881 3% 83 8.33 10 20 180 20 0 100 90 0.541 25% 84 8.33 10 20 180 20 0 150 90 0.541 18% 85 8.33 10 20 180 20 0 200 90 0.541 5% 86 8.33 10 20 180 20 0 250 90 0.541 0% 87 8.33 10 20 80 30 0 150 90 0.881 10% 88 8.33 10 20 80 30 0 200 90 0.881 7% SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 13 Pipe Flow Rate Rotation Inclination gpm RPM TEST No. Density lb/gal PV, μp YP, lb/100 ft2 Temperature ROP fph Eccentricity Cc 89 8.33 10 20 80 30 0 100 67 0.881 41% 90 8.33 10 20 80 30 80 100 67 0.881 21% 91 8.33 20 40 80 30 92 8.33 10 20 120 40 0 100 90 0.881 30% 0 100 90 0.881 39% 93 8.33 10 20 120 94 8.33 10 20 120 40 0 150 90 0.881 20% 40 0 200 90 0.881 18% 95 8.33 10 20 180 40 0 100 90 0.881 28% 96 8.33 10 97 8.33 10 20 180 40 0 150 90 0.881 17% 20 180 40 0 200 90 0.881 3% 98 8.33 99 8.33 10 20 180 40 80 100 90 0.881 7% 10 20 180 40 80 150 90 0.881 6% 100 101 8.33 10 20 180 40 80 200 90 0.881 0% 8.314 1 0 180 40 0 100 90 0.541 33% 102 8.314 1 0 180 40 0 150 90 0.541 24% 103 8.314 1 0 180 40 0 200 90 0.541 7% 104 8.314 1 0 180 40 80 100 90 0.541 6% 105 8.314 1 0 180 40 80 150 90 0.541 4% 106 8.314 1 0 180 40 80 200 90 0.541 0% 107 8.314 1 0 120 15 0 100 90 0.541 30% 108 8.314 1 0 120 15 0 150 90 0.541 19% 109 8.314 1 0 120 40 0 100 90 0.541 23% 110 8.314 1 0 120 40 0 150 90 0.541 15% 111 8.314 1 0 120 40 0 200 90 0.541 13% 112 8.314 1 0 120 40 80 100 90 0.541 5% 113 8.314 1 0 120 40 80 150 90 0.541 2% 114 8.314 1 0 120 40 80 200 90 0.541 0% 115 8.314 1 0 180 15 0 100 90 0.541 23% 116 8.314 1 0 180 15 0 200 90 0.541 12% Table 7. Experimental results the model predictions for water tests. Good agreement was achieved. Development of the Cuttings Transport Simulator A user-friendly cuttings transport simulator was developed in this project to help use the correlations obtained from this study. The simulator was implemented in Visual C++ under a Windows® platform. A sensitivity study can be conducted using this cuttings transport simulator. Results can be used for optimization of the drilling operations at the design stage or on the rig. A screenshot of the simulator is shown in Fig. 15. S U M M A RY A N D C O N C L U D I N G R E M A R K S 1. An experimental study on cuttings transport under simulated downhole conditions was conducted at the 14 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 University of Tulsa using the ACTF flow loop. 2. A total of 116 experiments were conducted under well controlled testing conditions. 3. The effects of drilling fluid rheological parameters, ROP, temperature, borehole inclination angle, flow rates, pipe rotation, eccentricity and drilling fluid density on cuttings transport were studied experimentally. 4. Experimental results show that drill pipe rotation, temperature and rheological parameters of the drilling fluids have significant effects on cuttings transport efficiency. 5. A dimensional analysis was conducted to develop correlations that can be used for field applications. 6. A user-friendly simulator was developed to help use the correlations developed in this study. This simulator can be used by drilling engineers for design and sensitivity study. 7. Critical conditions for efficient hole cleaning can be determined using the results obtained from this study. 8. The correlations and experimental data provided in this study are useful for field applications and operation optimization. ACKNOWLEDGEMENTS The authors wish to thank Saudi Aramco for financial and technical support and the University of Tulsa for providing the testing facility. The authors also wish to thank the U.S. Department of Energy and members of Tulsa University Drilling Research Projects for their financial and technical support of the construction of the University of Tulsa’s Advanced Cuttings Transport Facility, which made this study possible. REFERENCES 1. Clark, R.K., Bickham, K.L.: “A Mechanistic Model for Cuttings Transportation,” SPE paper 28306, 69th annual SPE Technical Conference and Exhibition, New Orleans, Louisiana, 1994. 2. Rasi, M.: “Hole Cleaning in Large, High-Angle Wellbores,” IADC/SPE paper 27464 presented at the IADC/SPE Drilling Conference in Dallas, Texas, February 15-18, 1994. 3. Luo, Y., Bern, P.A. and Chambers, B.D.: “Flow Rate Predictions for Cleaning Deviated Wells,” IADC/SPE paper 23884 presented at the IADC/SPE Drilling Conference in New Orleans, Louisiana, February 18-21, 1992. 4. Okafor, M.N. and Evers, J.F.: “Experimental Comparison of Rheology Models for Drilling Fluids,” SPE paper 24086. 5. Bird, R.B., Stewart, W.E. and Lightfoot, E.N.: “High Temperature High-Pressure Rheology of Water-Based Mud,” Transport Phenomena, John Wiley and Sons, Inc., New York, 1960, p. 11. 6. Bingham, E.C.: “Fluidity and Plasticity,” McGraw-Hill Book Co., Inc., New York, 1922. 7. Beirute, R.M. and Flumerfelt, R.W.: “Mechanics of the Displacement Process of Drilling Muds by Cement Slurries using an Accurate Rheological Model,” SPE paper 5801, 1977. 8. Eddy, K.: “An Experimental Study of the Effect of Mud Weight and Drill Pipe Rotation on Cuttings Transport in Horizontal and Inclined Wells,” University of Tulsa, Oklahoma, 1996. on Hole Cleaning during Directional Well Drilling,” SPE paper, presented at Amsterdam, March 4-6, 1997. 10. Zhu, C., Ph.D. Dissertation: “Cuttings Transport with Foam in Horizontal Concentric Annulus under Elevated Pressure and Temperature Conditions,” University of Tulsa, Oklahoma, 2005. E X P E R I M E N TA L P R O C E D U R E The following procedures are to perform experiments on hole cleaning under simulated downhole conditions using the ACTF, elevated-temperature, elevated-pressure flow loop, part of the Tulsa University Drilling Research Project’s (TUDRP) facilities. 1. Before going to the flow loop a. b. c. d. Establish the test matrix data points to be obtained. Check the current status of the flow loop. Review test procedures. Review safety procedures. 2. Check the fuel level in the mud pump to make sure fuel level is full. 3. Cuttings preparation a. Sieve the cuttings as required for the upcoming the experiments. b. Open the top of the injection tower. c. Fill the injection tower to 75% of its capacity. d. Close the top of the injection tower. 4. Fluid preparation a. Fill tank #1 with water. b. Heat water to the test temperature while circulating through the flow loop. c. Transfer water to the mixing tank. d. Add and mix polymer as detailed in mud program. e. During and after the mixing process, take samples and measure the rheology in the lab using Fann 75 at the test temperature and pressure, and Chandler 35 at ambient conditions. f. Transfer mixed polymer back to tank #1. g. Heat mixed polymer to the test temperature while circulating through the flow loop. 5. Rheology test a. Line up valves to flow through rheology section. b. Wait for steady state conditions. c. Record at least two minutes of data at steady-state conditions. 9. Sanchez, R.A., et al.: “The Effect of Drill Pipe Rotation SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 15 d. Increase the flow rate at agreed intervals (LAMINAR FLOW must be maintained). e. Return valves to their original position. f. Take a sample of the liquid from the tank and measure the rheology using Fann 75 and Chandler 35. 6. Cuttings transport test a. Increase the flow rate to initial test conditions. b. Use the Swaco system or Ceramic angle chokes to control the back pressure to test condition. c. Wait for steady-state flow rate and pressure conditions. d. Start the hydraulic pump and auger rotation. e. Open the cuttings injection valve located at the injection tower. f. Pressurize the injection tower. g. Control the cuttings injection rate at the test rate of penetration. h. Wait for steady-state in the annular section. i. Start pipe rotation at test speed. j. Wait for steady-state conditions in annular section. k. Record at least 2 minutes of data at steady-state conditions. l. Increase the flow rate by agreed increment. m. Wait for steady-state conditions in the annular section. n. Repeat steps k, l and m until annular section is clean. o. Close the cuttings injection valve and stop the auger rotation. p. Take a sample of liquid from the tank and measure the rheology using Fann 75 and Chandler 35. q. Turn off the hydraulic pump. r. Decrease the back pressure slowly. 7. Clean up a. Flush out all cuttings from the flow loop piping using water. b. Rinse and drain tank #1 with water. c. Rinse the flow loop with hot water. d. Rinse the flow loop with fresh water. e. Stop all pumps and return valves to their original position. f. Turn off heater. g. Fill tanks #1 and #2 with fresh water. h. Fill fuel tanks of mud pump and compressor. i. Clean the concrete pad of the flow loop. j. Check the loop piping and valves. 8. Download and backup the data from the acquisition system. 16 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 Case History: Application of Coiled Tubing Tractor to Acid Stimulate Open Hole Extended Reach Power Water Injector Well Ayedh M. Al-Shehri Saad M. Al-Driweesh Mazen Al-Omari Samer Al-Sarakbi Ayedh M. Al-Shehri is a Senior Production Engineer with the ‘Udhailiyah Production Engineering Division of the Southern Area Production Engineering Department. He received a B.S. in Petroleum Engineering from King Fahd University of Petroleum and Minerals (KFUPM), Saudi Arabia in 1999. Ayedh has 8 years of oil production experience in different south Ghawar fields. He is also a member of the Society of Petroleum Engineers (SPE). Saad M. Al-Driweesh is a Production Engineering general supervisor in Saudi Aramco, where he is involved in gas and oil production engineering, well completion and stimulation activities. He is mainly interested in the field of production engineering, production optimization and new well completion applications. He received a B.S. degree in Petroleum Engineering from King Fahd University of Petroleum and Minerals (KFUPM), Saudi Arabia in 1988. Saad has been working with Saudi Aramco for the past 19 years in areas related to gas and oil production engineering. Mazen Al-Omari is currently the Operations Manager for Welltec Middle East. A graduate of Master in Civil Engineering, he has 16 years experience in the oil field services industry, mostly in cementing, stimulation, well intervention and sand control. Mazen has worked in many countries, including Syria, Turkey, Iran, U.A.E., India, Pakistan, Indonesia and the USA. Samer Al-Sarakbi is a General Field Engineer in Schlumberger. He is involved in coiled tubing and stimulation operations. Samer’s main interest is in extended reach coiled tubing applications, downhole tools, carbonate stimulation and water shut off. He received a B.S. degree in Mechanical Engineering from Damascus University, Syria, in 2003. ABSTRACT With the increasing complexity of well completion, the rigless intervention work is becoming more challenging. Conventional techniques are no more adequate to access long horizontal wells to perform intervention work, such as acid stimulation, logging, and zonal isolation. This article will describe the process of using a downhole coiled tubing (CT) downhole tractor to access a horizontal open hole (OH) extended reach power water injector (PWI) well in the Ghawar field, the world’s largest oil field, to perform a huge matrix acid stimulation job. The volume of the treatment is considered one of the largest for a PWI and the first utilization of a CT tractor in the Ghawar field. It will also review the process of candidate selection, job design and planning, execution, and results and post job evaluation. The job set an excellent example of advancement in intervention technique accessing long horizontal wells beyond the normal reach of coiled tubing. In this job, the CT tractor has increased the reach of CT by 54% and a world record of coiled tubing tractored interval in horizontal OH of more than 5,000 ft was achieved. The injection rate of the stimulated wells was increased by more than twofold. INTRODUCTION The giant Ghawar field, located in the Eastern Region of Saudi Arabia, is a carbonate reservoir, more than 200 km long and 40 km wide with a continuous oil column, Fig. 1. The production from the field was started in 1951 from the northern part and thereafter the field was developed toward the southern tip with the last increment put on stream in 20061. Fig. 2. Well lateral trajectory. Reservoir characterizations change along the north-south lateral with the southern part known for lower reservoir quality dominated by low permeability fractured formation. To maximize recovery of oil from this unique reservoir, peripheral water injection was started in 19662. As the development reached the southern part of the Ghawar, the reservoir quality dictated the necessity to utilize the latest advancement in drilling technology including long horizontal, maximum reservoir contact (MRC), real-time geosteering, and I-Field initiatives. These complex completion wells present a challenge to production engineers to riglessly access them in order to perform intervention work to enhance performance or remedy downhole problems. Due to tightness of reservoir formation combined with formation damage, matrix acid stimulation jobs were deemed necessary to improve injectivity supporting the reservoir pressure in this part of the field. In extended reach horizontal wells, bullheading of treatment fluid is not efficient due to the nature of this fractured reservoir and a coiled tubing unit (CTU) should be used to provide uniform distribution of the acid across the horizontal treatment interval. Field experience indicated that accessibility of a CTU in horizontal wells is limited due to increased friction generated when the pipe starts to get helically buckled and finally reaches a lockup point where the total down acting forces are no more sufficient to move the CT pipe further in the well. This limits the capability to distribute the treatment across the horizontal section. Different techniques have been used to overcome this limitation of CT to perform intervention work such as using large outside diameter (OD) coiled tubing, downhole vibration tools, and friction reducer chemicals3, 5. W E L L C O M P L E T I O N A N D H I S T O RY Fig. 1. 3D map of Ghawar field. 18 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 The well was drilled and completed as an extended reach horizontal OH PWI to a total depth (TD) of 17,716 ft and Fig. 3. Well completion schematic. true vertical depth (TVD) of 7,690 ft, Fig. 2. The 61⁄8” OH was drilled from 8,322 ft to TD. The well was completed with 7” completion packer and a tail pipe assembly at 7,358 ft with the end of the tail pipe at 8,794 ft, leaving 8,922 ft of horizontally exposed reservoir formation with a maximum inclination angle of 93°. The average reservoir porosity is 10%. The objective of this completion is to cover the anhydrite formation in the 61⁄8” OH below the 7” liner to the top of the injection formation, Fig. 3. The decision to set the packer was taken during the drilling course due to unexpected formation development and dipping where the setting of the 7” liner was found above the injection formation leaving the anhydrite formation exposed. While the rig was on location, an injectivity test was conducted at a surface pumping pressure of 1,000 psig achieving an injection rate of 2.4 barrels per minute (bbl/min); the rate was considered very low and a clear indication of formation damage. Performing the acid stimulation while the rig was on location was not a viable option; mainly due to safety concerns and the high cost of rig time; considering the large amount of acid that would be needed for such treatment. The well was initially put on injection with an injection rate of 13,000 barrels of water per day (BWPD) at an average injection pressure of 2,350 psig. This rate is much less than the rates of offset wells with even a shorter horizontal section. treatment. With bullheading, the acid tends to go to the least resistance intervals, mostly close to the vertical section or high permeability streaks; resulting in partial acid treatment5. A uniform placement of treatment fluids across the damaged interval is very essential for the success of the planned matrix stimulation job. Chemical diversion and mechanical isolation methods have been applied with limited effectiveness to distribute the acid evenly along the horizontal section, especially with long horizontal wells. Coiled tubing has been used effectively for acid displacement in vertical and horizontal wells as a means of acid placement, where the CT pipe would be run to the end of the treatment interval and then the acid is pumped across the formation while pulling out of hole (POOH) or reciprocating across the treatment interval. This technique has been also used in combination with chemical diversion systems, such as foamed viscoelastic diversion, for optimum acidizing results. In long horizontal and extended reach wells, this technique application is limited, where CT usually locks up due to the stacked weight of the CT pipe in the horizontal section preventing the CT from reaching the target depth. In such cases, part of the treatment has to be bullheaded from the lockup point and the rest will be pumped evenly across the treatment zone while POOH. Although the maximum available size of the CT during the job design was only 2”, it was clear from the performed simulation runs that even bigger OD pipe can not reach the TD of the well. Simulation runs were also carried out for a 2” CT combined with a vibrational tool and TD would not be reached. Review of recent technology advancements to access long horizontal wells, concluded the CT tractor to be the best option for reaching MD to displace the treatment fluids. Although the experience with the CT tractor applications in OH horizontal wells was very limited, especially with large acid treatments, it was decided to test this technology to JOB DESIGN AND PLANNING Acid Placement Technique Prior to the acid treatment design, the acid placement technique into this extended reach PWI was an issue. Conventional surface pumping through casing, bullheading, would not give the desired results since diversion of acid across the damaged interval is a key factor for effective Fig. 4. Simulation runs for different access techniques. SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 19 perform the acid job. Simulation runs were very encouraging and showed that a 2” CT in combination with two units of CT tractor can reach TD, Fig. 4. CT Tractor The CT tractor is a mechanical device that produces a concentrated pull force when engaged hydraulically. The CT tractor is normally made up at the bottom of the CT and is engaged by pumping a noncorrosive fluid through a turbine, which acts as a prime mover. A hydraulic pump then produces the force required to activate a set of wheels that are hydraulically deployed out of the tool body to engage the open hole and rotate causing forward movement. Schematic and typical specifications of the CT tractor are shown in Fig. 5. Due to the length of the OH section, a tandem (double) configuration of the CT tractor was deemed necessary for this operation. This would both double the force generated as well as double the grip with the formation allowing it to negotiate reasonable washed out sections of the OH. Two CT tractors of 31⁄8” size were planned to be used for this operation with a combined pulling force of 7,000 lb7. Acid Treatment Design The objective of the acid system treatment is to remove the suspected formation damage and create deep wormholes in the formation to improve the well’s injectivity. Several acid systems have been experimented and applied in this part of the Ghawar field; including plain, diesel emulsified, and nitrified acid systems. Due to the length of the treatment interval, volumes of treatment fluids have to be optimized efficiently without compromising the desired results of the treatment. Review of different acid systems applied in the area for horizontal wells indicated most favorable results were Fig. 5. Coiled tubing tractor schematic and specifications. 20 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 obtained using an acid system consisting of multiple stages of 20 wt% HCl acid followed by 20 wt% diesel emulsified acid, then finally followed by foamed viscoelastic surfactant-based water for diversion4, 6. An engineering detailed program was prepared for the acid treatment procedure. The treatment interval was divided into 16 treatment stages of 500 ft each. Below is the general pumping sequence for each stage: 1. First, the treatment interval has to be washed with plain 20 wt% HCl for filter-cake clean up and provide initial wormholes. The main additives to the plain acid are a corrosion inhibitor, surfactant, and friction reducer. Plain acid was used at 10 gal/ft, including additives, resulting in a total acid volume of 77,000 gallons. 2. Plain acid was followed by 20 wt% diesel emulsified acid at 20 gal/ft with a total of 154,000 gallons for the 16 treatment stages. The higher concentration of retarded acid is meant to provide deeper wormholes. 3. To achieve better acid diversion at the end of each pumping stage, viscoelastic surfactant-based (VES) water will be used at 10 gal/ft at a total volume of 7,500 gallons. 4. Finally, water over-flush of 10,000 gallons is to be pumped following the previous 16 treatment stages to break micelles formed by VES. The over-flush contained brine water mixed with 3 vol% of mutual solvent. The total treatment fluid to be injected in this job is 248,500 gallons; this large acid job is considered one of the biggest stimulation jobs for any well in the Ghawar field. Planning and Logistics The main two parts to plan were the transporting and mixing of the treatment fluids and the deployment of the CT and tool string. Also, due to the expected long mixing and pumping time of corrosive fluids, the safety of personnel on-site was a concern to ensure safe handling of chemicals. Due to the volume significance of the treatment, a total of 231,000 gal of 20% HCl systems and 17,500 gal of inert fluids were needed, in addition to the required water to operate the downhole CT tractor. The main challenges of material delivering, hauling and mixing were as follows: • Adequate water and raw acid supply, which was covered by four water transporters and six raw acid transporters with a total capacity of 39,000 gal of raw acid. • Adequate fluid storage capacity, which was covered by 16 storage tanks with a total storage capacity of 336,000 gal of mixed fluids, Fig. 6. Fig. 6. Total of 16 500 bbl storage and mixing tanks used to handle the treatment fluids. • Mixing all systems on location. This was handled by the best developed field practices for mixing large treatment volumes and equipment layout. As the total length of the designed bottom hole assembly (BHA) was 48 ft, including the two CT tractor units, and to avoid the risk associated with high rig up, the pressure deployment method was used by utilizing a slick line unit. This method assures the safe deployment of tool strings into a live well without the use of a long lubricator, longer than 48 ft, and a heavy injector head weight which would require a large crane and numerous guy wires for stability. Due to the extensive nature of the operation, safety of personnel on-site was a concern to all involved parties; extra safety measures were taken to guarantee safe execution. A Risk Assessment was conducted to identify potential hazards throughout the operation to ensure readiness to handle any safety or operational emergency. Several safety meetings were held, in both office and on-site, involving operator and service companies to ensure full awareness of potential hazards and emergency response plans. JOB EXECUTION AND PROCEDURE The main steps of the job execution were the following: • Function test and deployment of the tool string in the well. • Run the CT tractor 1,000 ft below the tubing end. • Activate the CT tractor and run to the MD possible. • Mix and pump the stimulation treatment while pulling out of the well. • Un-deploy the tool. The tool string was deployed in the well taking in consideration the main risk involved with the snubbing forces, the pressure control barriers, the CT connector integrity, the bi-directional strength and the shear capability of the deployment bar. Successfully, the tool was deployed in the well keeping two barriers at all times, and following established best practices and procedures. Deployment surface equipment mainly consisted of a blowout preventer Fig. 7. Running in hole and pulling out of hole vs. time. (BOP) and lubricator for the slick line unit. The deployed BHA consisted of: • 2” CT connector • CT Motor Head Assembly (MHA) • Circulation sub • Deployment bar • Double check valve • Double ball valve • Crossover • Upper CT tractor (Flow Through type) • Bottom CT tractor (Top Vented type) The tool was run in the well at an average speed of 45 ft/min while pumping at minimum rate to keep the CT full with water and conducting the required pull tests until a 9,580 ft depth, where the CT tractor was engaged by increasing the pumping rate to 1.5 bbl/min. The CT tractor engagement was confirmed by the reduction in the weight during the running in the well. The running speed was adjusted to synchronize the CT and CT tractor movements at an average run in hole (RIH) speed of 15 ft/min – 20 ft/min. Between 13,026 ft and 13,148 ft, the CT tractor encountered a washout; the CT tractor progress was stopped and the CT could not be run further in the well. Therefore, the CT tractor was pulled out 100 ft above the washout area and the running speed increased from 30 ft/min to 40 ft/min trying to create additional inertia for the pipe to help the CT tractor pass the washout. This technique was successful and the CT tractor was engaged with the hole again at 13,148 ft and continued the progress until reaching 14,770 ft where another washout was encountered. Three trials were made to POOH and run on a higher CT speed, but without success, which impeded the CT from reaching MD and stopped at 14,656 ft. It was decided to bullhead the first four bottom treatment stages from the maximum reached depth, 14,656 ft, and the rest of the treatment will be pumped as per design while POOH, Fig. 7. A ball was dropped to open the pumping ports on the BHA and create a barrier to isolate the internal parts of the SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 21 CT tractor from the acid. After 15 hours of mixing of the first six stages, pumping started and the rest of the treatment fluid was mixed while pumping. The total pumping time of the treatment was 52 hours of continuous pumping at an average pumping rate of 2.0 bbl/min. Once all acid stages and over-flush were pumped, the tool was POOH to surface and un-deployment (reverse deployment) was successfully conducted using the slick line unit. The whole operation lasted for seven days of around-the-clock operations. R E S U LT S A N D J O B E VA L U AT I O N Injection Gain Following the successful acid treatment, the well was put back on injection and the injection potential was effectively enhanced by more than twofold where the rate increased from 13,000 BWPD to 28,000 BWPD. This increase in the injection rate helped to sustain the reservoir pressure in the area while increasing the oil production target. Coiled Tubing Tractor Performance In general, the CT tractor performed very well in this job although the TD of the well was not reached. Using the CT tractor increased the reach of the CT in this well by 54% after tractoring for 5,190 ft in the OH. The CT tractor could not reach TD mainly due to two main possible reasons; presence of a washout interval and the high horizontal friction of CT, making it difficult for the tool to pull the CT and overcome minimal hole enlargement. A larger CT tractor could have provided further reach; however, due to the minimum restriction in this well of 3.725” it was not applicable. The inhibition of the CT tractor was an issue, especially in such a big treatment. In preparation for this job, the body of the CT tractor was silver coated and extra protective sleeves were installed, anticipating exposure to huge amounts of corrosive fluids. This enhancement provided good protection of the outer body of the CT tractor, however, minor internal damage was observed on parts, such as the turbine driving shaft and connection pipes. This internal damage is a result of having some acid flowing through the tool body; it is clear that the circulation sub did not provide full isolation of the CT tractor. LESSONS LEARNED Since this was the first CT tractor job in the Ghawar field, many lessons were learned. During this job, it was evidenced that the CT speed can help the CT tractor to pass 22 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 washouts in the OH; the inertia force of the CT pushing the CT tractor can help it to pass through long washouts. When the CT becomes very long in the horizontal section; it becomes hard to initiate CT movement when the CT tractor is stopped by a washout. The function test for the slick line wire during deployment and un-deployment is essential. Before opening the pipe/slip rams the slick line should apply a pull force equal to the tool weight, 1,000 lb in this case. While testing the wire for un-deployment the wire was cut at 500 lb weight. As some of the internal parts of the CT tractor were damaged, it is suggested to install a hydraulic valve above the top CT tractor to ensure complete isolation prior to pumping the acid; the current configuration is not providing adequate isolation to protect the internal parts of the CT tractor from being exposed to corrosive fluids. S U M M A RY The operation was successfully completed in one run. The CT tractor was deployed in the well, engaged at 9,580 ft in the OH and reached a MD of 14,770 ft. A slick line unit was used to perform the deployment and un-deployment to avoid high rig up of the CT injector. At different depths, while RIH, washout intervals were experienced where the CT tractor could not give any help to move the CT. In these situations, the CT string was POOH and RIH again at a higher speed. This practice was successful in extending the reach of CT tractor. A total volume of 248,500 gal of treatment fluids was pumped to stimulate the well. Objectives of the job was met with post-acid increase of the injection rate from 13,000 BWPD to 28,000 BWPD. CONCLUSION 1. A CT tractor can provide an increase of CT reach in horizontal open hole wells by 54%. 2. CT tractor technology is partially filling the gap between completion advancement and intervention services. Enhancement on current tools and development of new technology is needed to overcome this challenge. 3. Intervention in extended reach wells is both costly and challenging operationally compared to intervention in conventional wells. 4. More maintenance is needed for the CT tractor when used during acid treatment jobs. Availability of handy spare parts and adequate manpower on-site is essential for a quick turnaround. ACKNOWLEDGEMENT The authors would like to thank Saudi Aramco, Welltec and Schlumberger for permission to publish and present this paper. N O M E N C L AT U R E BHA BOP BWPD CT CTU HCl MD MRC OD OH POOH PWI RIH TD TVD Bottom Hole Assembly Blowout Preventer Equipment Barrels Water per Day Coiled Tubing Coiled Tubing Unit Hydrochloric Acid Measured Depth, ft Maximum Reservoir Contact Outside Diameter, in Open Hole Pull Out of Hole Power Water Injector Run in Hole Total Depth, ft True Vertical Depth, ft 5. Nasr-El-Din, H.A, Aranaout, I.H, Chesson, J.B. and Cawiezel, K.: “Novel Technique for Improved CT Access and Stimulation in an Extended Reach Well,” SPE paper 94044 prepared for presentation at SPE/ICoTA Coiled Tubing Conference and Exhibition, Woodlands, Texas, April 12-13, 2005. 6. Nasr-El-Din, H.A. and Samuel, M.: “Lessons Learned from Using Viscoelastic Surfactants in Well Stimulation,” SPE paper 90383 prepared for presentation at the 2004 SPE Annual Technical Conference and Exhibition, Houston, Texas, September 26-29, 2004. 7. Omari, M. and Plessing, H.: “Innovation in Coiled Tubing Tractor Technology Extend the Accessibility of Coiled Tubing in Horizontal Wells, Allowing Better Possibilities for Well Intervention,” SPE paper 105225 prepared for presentation at 15th SPE Middle East Oil Show, Manama, Bahrain, March 11-14, 2007. REFERENCES 1. Al-Ali, Z.A. and Stenger, B.A.: “A Case History on Integrated Fracture Modeling in a Giant Field,” SPE paper 71340 for presentation at the 2001 SPE Annual Technical Conference and Exhibition, New Orleans, Louisiana, September 30-October 3, 2001. 2. Bayona, H.J.: “A Review of Well Injectivity Performance in Saudi Arabia’s Ghawar Field Seawater Injection Program,” SPE paper 25531 prepared for presentation at the SPE Middle East Oil Show, Manama, Bahrain, April 3-6, 1993. 3. Blount, C.G., Moony, M.B., Behenna, F.R., Stephens, R.K. and Smith, R.D.: “Well-Intervention Challenge to Service Wells that can be Drilled,” SPE paper 100172 prepared for 2006 SPE/ICoTA Coiled Tubing Conference and Exhibition, Woodlands, Texas, April 4-5, 2006. 4. Harbi, M.I., Al-Dhafeeri, A.M., Al-Rufai, Y.A. and Mohammed, S.K.: “Evaluation of Acid Treatment Results for Water Injection Wells in Saudi Arabia,” SPE paper 101345 prepared for presentation at SPE/IADC Indian Drilling Technology Conference and Exhibition, Mumbai, India, October 16-18, 2006. SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 23 Identifying Sources of Amine Foaming Through Detailed Troubleshooting Provides More Feasible Solutions Mater A. Al-Dhafeeri Mater A. Al-Dhafeeri is a Senior Gas Processing Engineer working for Saudi Aramco since 1995. He has worked in most of Saudi Aramco’s gas processing facilities and NGL areas of the refineries. Mater received a B.S. degree in Chemical Engineering from Tulsa University, Tulsa, OK in 1995 and a M.S. degree in Natural Gas Engineering and Management from the University of Oklahoma, Norman, OK in 2001. ABSTRACT Diglycolamine (DGA) is the most widely used amine sweetening agent in Saudi Aramco facilities. Similar to other types of amines such as monoethanolamine (MEA), diethanolamine (DEA) and methyl diethanolamine (MDEA), foaming is a major concern especially in highpressure (HP) systems. Two case studies revealed that the major cause of foaming in two different gas processing plants was the high liquid hydrocarbon entrainment in the sour feed gas. Focusing on potential causes of the problem and detailed troubleshooting of amine treatment allowed us to identify the problem and find the most feasible option to abate the foam or at least reduce its severity. This article will demonstrate the benefits of proper troubleshooting to identify the sources of amine foaming in two gas processing facilities at Saudi Aramco. It will also provide some general information about amine foaming, causes, symptoms, and troubleshooting guidelines. FOAMING Amine solvent foaming has been widely discussed in the gas processing industry and several pieces of literature address the same problem. Foaming problems continue to be encountered in amine facilities due to various factors that induce foaming and lack of operational knowledge to troubleshoot foaming incidents. Many operational practices regarding foaming problems are of a reactive type trying to solve what caused such incidents rather than developing a strategy to track the main sources of foaming and trying to alleviate them or reduce their impact. High capital loss is reported annually due to the foaming in amine systems; these could be in the form of 24 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 temporarily losing sour gas processing capability, and hence, reducing sales/fuel gas production, solvent loss, and violating environmental regulation. Foaming in any Saudi Aramco treating facility generates serious revenue loss due to the huge size of the gas sweetening units treating approximately 7.0 billion standard cubic feet per day (scfd) of sour gas using the DGA agent. Continuous anti-foam injection has been the most common method used in the facilities to suppress foaming. The utilization of anti-foam injection is well known and documented throughout the gas processing industry; however, it is only recommended as a last resort and only on an intermittent basis. Most of the anti-foams are surface active and a high dosage could aggravate foaming problems. Besides, there have been some recent findings that anti-foam reduces the absorption capacity of CO2 by 40%-55%; however that was based on utilizing MDEA1. In an effort to reduce the reliance on anti-foams and to increase operational confidence in the HP amine systems, the central engineering group of Saudi Aramco in partnership with field/operation engineering in two Gas Processing Facilities (Gas Plants) decided to focus on identifying the sources of foam and eliminate them rather than trying to suppress the foam. facilities where most of the current foaming concerns are in the amine plants that are operating at high-pressures. Having a low surface tension does not indicate having stable foam, and hence, a foaming problem. Stability, which is related to the nature of the surface layer, is the other key factor of having a foaming concern. Foam stability is dependent on three main characteristics; elasticity, gelatinous layer formation, and film drainage4. • Having higher elasticity, resistance to thinning, generates lower foaming stability. The major function of most anti-foam is to increase the solution elasticity and reduce the foam stability. • Gelatinous or plastic layer is a surface structure related to the nature of molecular composition of the aqueous solution, solutions which are prone to form gelatinous layers tend to have higher foaming stability4. Secondary (DEA) and tertiary (MDEA) amines form this layer easier than primary (MEA and DGA) amines and therefore, they are more susceptible to foam. Contaminants, such as amine degradation products, induce the formation of the gelatinous layer. • Faster film drainage reduces foam stability. However, fine particulates, such as iron sulfide, tend to retard film drainage and increase foam stability. FOAMING IN AMINE SYSTEMS FOAM INDUCERS Foaming is defined as “a result of a mechanical incorporation of a gas into a liquid, where the liquid film surrounds a volume of gas creating a bubble2.” Two key characteristics need to be present in order to have a foaming concern; solution tendency to foam (the easiness of a solution to form a foam bubble) and foam stability (foam resistance to break into the continuous liquid phase). The higher the foam tendency and stability, the higher the possibility of having a foaming problem. Surface tension is the primary indication of foaming tendency. Lower surface tension leads to more solution susceptibility to foam. The major source of reducing the surface tension of an amine solution is solution contamination with surface active agents which include liquid hydrocarbons. Surface tension is also affected by operating conditions; higher temperature and pressure tend to reduce the surface tension. Temperature has the upper hand in impacting the surface tension of an aqueous amine solution. To a lesser extent, higher pressure has a negative impact on the solution foaming tendency. At higher pressures, the solubility of liquid hydrocarbons in the amine solution increases, therefore this changes the surface structure of the aqueous solution rendering a lower surface tension and hence increased system tendency to foam3. That is exactly what has been observed in Saudi Aramco gas processing Clean uncontaminated amine does not form stable foam. Amine system foaming is caused by contaminants that are either introduced to the system through the feed gas, make up water, and recycled streams or, generated in the system such as degradation and corrosion products. Listed below are the most common causes of foaming5-8. 1. Liquid hydrocarbon introduced by sour feed gas is the primary cause of foaming problems in gas sweetening plants. Liquids can be introduced as mist entrainment or carry over, or can be formed inside the column if the lean amine entering the column is at a lower temperature than the sour gas dew point. The impact of liquid hydrocarbon comes from the fact that it is soluble in the aqueous amine solution and therefore reduces its surface tension. Secondary and tertiary amines tend to foam in the presence of liquid hydrocarbons more than primary amines due to the higher solubility of liquid hydrocarbon in secondary and tertiary amines. One of the challenges is the removal of liquid hydrocarbon droplets of aerosol size. Droplet sizes greater than 3 microns are generally controllable; however, smaller sizes require careful filterseparator and coalescer design. Some plants were able to reduce the liquid carry over by installing 0.3 micron coalescers upstream of the amine absorber columns9. 2. Solid particulate contamination, especially iron sulfide, is SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 25 3. 4. 5. 6. 7. one of the major causes of foaming. Iron sulfides can be very fine particulates, which are difficult to remove by conventional mechanical filters, tend to concentrate in liquid-gas interface and therefore increase the foaming stability. Iron sulfide is a byproduct of corrosion activities of hydrogen sulfide and carbon steel piping. It could be carried over from the sour feed gas, or generated in the amine solution due to various reasons such as high solution acid gas loading, high velocities, and formation of acidic degradation products. Water soluble surfactants such as corrosion inhibitors, well treating compounds, and excessive anti-foam agents tend to dissolve in aqueous solutions and reduce surface tension. Such contaminants are often much more problematic than liquid hydrocarbons, if an appreciable amount exists in the sour gas, due to their higher solubility in amine solution. Amine degradation products lead to changes in the amine solution structure and may increase the foaming tendency. Degradation products are compounds which are formed either by the direct reaction of the amine and constituents in the feed gas (such as CO2, COS, CO, O2 and CS2) or by thermal decomposition of the amine. Conversion of the amine, irrespective of the mechanism, represents a loss of active and valuable amine. Heat Stable Salts not only tend to reduce the system sweetening capability, but also increase corrosion and subsequently increases iron sulfide production and affects the physical properties of the solution. Corrosion products and changes in solution properties tend to increase the foaming tendency and stability. Heat Stable Salts are not thermally regenerable causing them to accumulate in the circulating amine solution and contaminating it. Such heavy salts are products of amine reaction with other anionic species and/or stronger acidic components (other than H2S and CO2) which are present in the sour feed gas. Oxygen ingress in the feed or the amine solution, even in ppm levels, leads to the formation of carboxylic acids that react with amine to form Heat Stable Salts and therefore increases the system tendency to foam. Positive pressure is always required to avoid any accidental oxygen leakage to the system. One area that needs to be monitored is the amine storage tank that should be normally protected by an inert gas blanket; commonly nitrogen blanket gas is used. Makeup water could be another source of introducing various contaminants to the system. The main source of the makeup water is the utility plant where various chemical additives are introduced to treat it prior to 26 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 feeding it to the steam boilers. Such chemicals include corrosion inhibitors and boiler feed water chemicals. Demineralized water could provide a very safe source of makeup. FOAMING SYMPTOMS An amine system subjected to foaming exhibits the following behavior: • Sudden increase in the column differential pressure is the first alarming sign of a foaming system. Normally, amine absorber columns are equipped with differential pressure cells to monitor system abnormalities. When the contactor is facing a foaming problem and as the foam height is increased, the void volume inside the column is reduced. Reduction in void volume leads to higher pressure drop. • Off specification sweet gas due to the loss of some absorption capacity of amine solution. Foaming reduces the vapor-liquid contact area, generating a reduced effective mass transfer zone and thus less acid gas is picked up by the amine. Most of the gas processing facilities are equipment with an online analyzer to detect an H2S concentration in the sweet gas to avoid producing an off specification sales/fuel gas. Unexpected high H2S content in the sweet gas indicates a possible foaming problem in the system. • Amines carry over to the downstream equipment. This is a late warning sign of foaming in the column and could be noticed by some erratic and/or abnormal levels in the downstream knockout drums. • Loss or reduction in rich amine flow rate accompanied with an erratic and/or abnormal level indication in the absorber column bottom section. • Abnormal absorber column temperature profile. A typical temperature profile has a shape of a pregnant woman, where the bulge (maximum) temperature is in the lower trays where the main reaction between acid gas and amine solution takes place, Fig. 1. Normally, during foaming, the bulge temperature shifts from the lower trays to the upper trays, especially if foaming was caused by a contaminated sour gas. ANTI-FOAM INJECTION Anti-foam does not eliminate the foaming problem; rather, it is used to reduce its severity. Most anti-foams tend to increase the surface layer elasticity allowing it to resist film thinning7. Once the anti-foam injection is stopped, the system becomes vulnerable to foaming at anytime due to the fact that the foam inducing contaminants are still within the system. Relying solely on anti-foam to avoid foaming problems leads to contaminants build up in the system, this will lead to other serious problems such as amine degradation, solvent losses and corrosion. Excessive antifoam dosage reverses its function and makes it a foam promoter. This phenomenon has been clearly demonstrated by Saudi Aramco Research & Development Center where it was found that silicon based anti-foam increases its foam reducing power in a DGA system up to a concentration of 25 ppm and nothing was gained beyond that. At 9,000 ppm, anti-foam begins to stabilize the foam, and therefore increases the foaming severity10. Another side effect that has yet to be fully proven for the primary amines is the impact of anti-foam on the reduction of the mass transfer rate. A study1 concluded that presence of anti-foam renders lower diffusion of the acid gases into the amine solution and therefore, reducing amine absorption capacity. Because of the above reasons and the extra cost associated with antifoam chemicals, anti-foam should be the last option. Consequently, preventing contaminants and maintaining a good quality amine should be the primary target. CASE STUDIES IN AMINE FOAMING Foaming in HP gas treatment facilities at Saudi Aramco has been a concern since their startup. Currently, there are seven HP treatment trains in Saudi Aramco; five are processing non-associated sour gas located in the southern area and two at Berri Gas Plant treating HP offshore associated gas. Continuous anti-foam is being extensively utilized in the southern area gas plants. In Berri Gas Plant, anti-foam injection was subjected to various changes from batch injection to continuous injection as a reaction to some foaming incidents where the plant management could not tolerate any further reduction in gas supply. The central engineering group decided to tackle the foaming problem in two locations where there have been elevated concerns regarding foaming. The main target of the troubleshooting was to identify the source of foaming rather than relying on the practice of optimizing the antifoam injection rate. Listed below are the two case studies with some background on the plants, causes of the problems, and recommendations to abate foaming or reduce its severity. CASE 1: SHEDGUM GAS PLANT (SHGP) History Foaming in the HP amine contactor has been a problem since the startup of the plant. The sour non-associated Khuff gas was first introduced to the unit in 1991 with the amine being regenerated in one of the low-pressure (LP) gas treatment facilities. Maximum throughput attained at that time was 280 million standard cubic feet per day (MMscfd) (Design rate is 440 MMscfd). Even at that rate, the system did not stabilize due to the onset of early foaming symptoms. Based on the commissioning tests, it was concluded that foaming in the HP contactor was caused by some contaminants present in the amine system. Therefore, activated carbon beds were installed temporarily to remove dissolved hydrocarbons. After applying three batches of activated carbon, which were exhausted within 35 days, the plant was only capable of processing 250 MMscfd of sour gas. No more activated carbon was added and the system was dismantled for economical reasons. With the continuous anti-foam injection of 0.72 ppm, the train was able to process a maximum sustainable sour gas rate of 460 MMscfd. Since then, the plant has been utilizing continuous anti-foam. With time, the plant processing capacity has declined and symptoms of foaming have occurred when the plant has been operating around the design rate even with continuous anti-foam injection. Table 1 shows the basic information about the HP unit. The team that was formed to resolve the problem focused on three major areas. Two of them address potential causes of foaming. The third explores some possible options to reduce the foaming problems. These areas are: • Amine solvent quality • Sour feed gas pretreatment • Areas of improvements Amine Solvent Quality Amine solution quality is a crucial factor in predicting and preventing foaming. The first step taken was to check the lean amine solution quality. Analyses were performed to show a detailed breakdown of the amine solution constituents; however, these analyses did not show the content of either the dissolved hydrocarbon or dissolved solids, which were expected to be the major cause of foaming in the plant. The results revealed 15 wt% degradation products in the solution. The conventional titration method was showing prior to the detailed analysis an amine concentration of around 40 wt% - 50 wt%; however, it was found to be < 34 wt%. Refer to Table 1 for the complete analyses results. This is a clear sign that there is a poor amine quality circulating within the system. The main reason behind this was the system configuration at that time where a common regenerator was used for the HP and LP trains. Hydrocarbons were speculated to be in an appreciable amount due to the amine filtration system which does not contain activated carbon beds. Existing filtration consists of SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 27 a pre-coat filter (1 micron rating) and a mechanical cotton fiber filter (5 micron rating) designed to process 10% of the circulating amine solution. Earlier studies showed that when activated carbon beds were installed, they were exhausted in less than 35 days. This indicated that amine was severely contaminated with dissolved hydrocarbon that was introduced by the sour feed gas. Sour Gas Pretreatment The HP unit is equipped with a slug catcher for removing bulk liquids and two vertical three phase filter separators for removing liquid aerosols and solid particulates with diameters of > 0.5 microns. The filters were equipped with two separate compartments, 42 filter coalescing elements, and vane pack. Estimated clean pressure drop (criteria for replacing the filter element) across the filter separator was 1.25 psi. A HP drop has never been a concern in the plant since the unit startup. It was concluded that the presence of solids in the gas phase was not a major concern. Therefore, we decided to inspect the filter separator for mechanical damage to the filter elements. Most of the filter elements were found to be in good mechanical condition except for three elements that had some cracks that could have been caused by improper installation and/or damage during the removal process. Another important issue we looked at was to verify the liquid loading inside the filter Fig. 1. Typical contactor temperature profile. 28 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 separator. To do that we collected samples from locations #1 and #2 in Fig. 2. Samples from location #2 were used as simulation input and the samples from location #1 were analyzed for liquid loading to confirm the simulation results. In location #1 we collected the samples from the vertical segment of the pipeline to have a representative sample. The collection point was carefully chosen to be as close as possible to the exit nozzle of the heat exchanger to minimize liquid settling. Location #2 was used to collect gas stream samples where the possibility of having liquid is minimal. This stream was then analyzed and the analyses’ results were used in the simulation to estimate the liquid formation downstream of the heat exchanger. A combination of both methods provided a good representation of the liquid loading. Simulated cases showed a liquid loading of 320 gpm, while the design rate for each filter separator was 62 gpm. Liquid loading measured from location #1 showed liquid loadings varying from as low as 15 gpm to as high as 320 gpm. This indicated that the filter separators were well under designed for handling the high liquid loadings; this was mainly due to operating the plant under an inlet gas composition that is different from the design. Areas of Improvement It was clearly shown that high liquid loading that exceeds the design of the exiting filter separator is the main cause of the foaming problem in the facility. Nonetheless, due to the high capital cost associated with installing additional filter separators and the commissioning of a new regeneration system for the HP unit, it was decided to continue using continuous anti-foam injection as the primary option to suppress foaming. Several low cost modifications and operational practices were adapted to improve the unit performance and reduce the foaming severity. These include: • Retrofitted perforated liquid surface protection plate above the maximum liquid level. This will reduce agitation activities at the liquid surface and also reduce the liquid carry over rate. • Modified the level control system to have one controller for the liquid hydrocarbon and water levels indistinctively. This will allow faster drainage of the liquid and reduce carry over. • Enhanced operational awareness of some of the important practices; such as routine skimming of hydrocarbon liquids from the flash drum and the reflux drum, eliminating the oxygen ingress to the amine storage facilities, and operating the flash drum at pressures as low as possible to flash more hydrocarbons. Fig. 2. Sample collection locations. Fig. 3. Berri Gas Plant slug catcher level trend during the November 26 foaming incident. CASE 2: BERRI GAS PLANT (BGP) Background Berri Gas Plant treating an offshore HP sour gas at two amine treating units were commissioned in 1998 and 2000, see Table 1. Since their startup, the units were hit by a series of foaming incidents during the winter season. During each incident the plant used batch anti-foam to control the problem; however, after some recent incidents, a continuous anti-foam injection has been practiced. The two HP trains use activated carbon beds to treat the amine solution with upstream and downstream guard filters. Being surface active, anti-foam usually is adsorbed by the activated carbon beds and therefore exhausts them quickly. It was a common practice to have the beds offline during anti-foam injection. Having the activated carbon beds offline leads to the dilemma of not having a sink source for the anti-foam. Continuous anti-foam injection means continuous build up of the anti-foam agent in the system that could after some time reverse the functionality of anti-foam. Continuous anti-foam at Berri Gas Plant has a more severe impact on the system compared to ShGP in the previous case study. ShGP is equipped with a pre-coat filter that acts as a sink for the anti-foam agent. Our laboratory found that silicon based anti-foam (100 ppm) was completely removed from the amine solution by one pass through 1” pre-coat filter media. It was estimated that 70% of the anti-foam was removed by the pre-coat filter at the plant10. Therefore, identifying the causes of foaming was imperative to convince the plant management to stop practicing continuous anti-foam injection. By reviewing the recent two foaming incidents, foaming problem in the HP system, its causes, and recommended remedies are addressed by answering the following questions: • What went wrong in the BGP HP amine unit? • How did we identify the causes? • What is recommended to alleviate foaming reoccurrence? What Went Wrong in BGP HP Amine Unit? The main cause of the foaming incidents was determined to be liquid carry over with the sour gas stream mainly as a result of liquid condensation in the pipeline after an upset in the offshore gas producing facilities. The upstream facilities use a refrigeration system to control the hydrocarbon dew point at approximately 60 °F to condense heavy hydrocarbons and thus avoid their condensation along the pipeline. Immediately preceding the last two foaming incidents, the upstream Gas Compression Plant (GCP) and the refrigeration systems were shutdown temporarily. This upset resulted in hydrocarbon condensation and liquid buildup in the pipeline that was carried to the BGP slug catcher. Inadequate drainage of the slug catcher liquid level caused liquid carry over to the HP contactor. SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 29 Fig. 4. Berri Gas Plant slug catcher level trend during the January 18 foaming incident. Fig. 6. Offshore gas compression facility outlet flow reading, January 18. Fig. 7. Amine contactor temperature profile during November 26 foaming incident. Fig. 5. Offshore gas compression facility outlet flow reading, November 26. How did we Identify the Causes? Several indications showed that the cause of foaming was liquid carry over resulting from an upset in upstream operation. These indications are listed below: • High Level Indication in BGP Slug Catcher There was a sharp increase in the slug catcher level indicator reading immediately prior to each foaming incident (Figs. 3 and 4) which is not normal due to the dry nature of the sour feed gas. The sour gas is considered a dry gas because of the removal of heavy H/C by the dew point control unit. It is concluded from this that a rapid increase in the slug catcher level is very remote except during upsets in the upstream operation or during pipeline scraping activities. • Outage in Upstream Compression Plant Prior to each of the two recent foaming incidents, there were upsets in the upstream GCP where gas flow through the sub-sea pipeline to BGP ceased, Figs. 5 and 6. No flow into the sub-sea segment of the pipeline and continuous withdrawal of gas by BGP caused the pipeline pressure to 30 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 Fig. 8. Amine contactor temperature profile during January 18 foaming incident. decrease. Due to the retrograde nature of the gas, pressure reduction leads to an increase in the gas dew point temperature11. Therefore, low ambient temperature caused the stagnant gas to reach the dew point temperature and resulted in condensation in the pipeline. Looking at the two foaming incidents, there was a time lag between the shutdown of GCP and the onset of foaming in the HP amine system. This is due to the fact that gases travel faster than the bulk liquids accumulation due to condensation. Operating Gas Plant Facility Berri Shedgum Sour Gas Rate, MMSCFD 270 440 Hydrogen Sulfide Content, Mol% 2.2 3.2 Carbon Dioxide Content, Mol% 2.8 3.7 Pressure, psig 550 990 2,100 3,400 Process Variables Amine Circulation Rate, GPM Lean Amine Solution Analyses Amine, wt% 39 34 Water, wt% 58 52 Degradation Products, wt% 3 15 Organic Acids, ppmw 50 80 Inorganic Acids, ppmw 15 20 HSS Salt Anions, ppmw 65 100 Lean Loading, mol/mol 0.08 0.07 99 98 Sample Recovery, % Table 1. Berri and Shedgum Gas Plant data Gas residence time in the HP gas pipeline is 13-16 hours; however liquids will travel slower depending on their quantities. This also explains the time difference in observing the shutdown impact in the form of foaming between the two incidents. The November 26 foaming took place two days after GCP shutdown while the January 18 foaming was observed five days after the shutdown. This is attributed to longer shutdown duration during the January 18 case that resulted in more liquid condensation and accumulation. • Contactor Temperature Profile The temperature profile inside the contactor during both foaming incidents showed an increasing trend as we moved upward in the column, Figs. 7 and 8. The reaction between amine and sour gas is exothermic and usually the first contact trays have the highest temperatures. In foaming systems, major reactions take place at the interface of the foam due to the hold up of amine by the foam. As the foam moves upward, the exothermic reaction will move upward and will be reflected by higher temperatures on the upper trays. Such a trend appeared during the foaming incidents, which indicates that sour feed gas has introduced foaming promoters to the system. • BGP HP System Operating Experience Operating experience in BGP HP amine plant showed no foaming tendencies during summer time. High temperature is the best environment for inducing foaming as it reduces the amine surface tension and makes it susceptible to foaming. Trouble free operation during summer operations proves that the HP DGA system should be adequate to handle normal operating conditions during cold weather seasons if the same sour gas feed quality is maintained. • Amine Quality Amine quality has not been a problem in BGP HP DGA. The plant was able to operate adequately during summer operations. In addition, the HP amine system is equipped with the recommended conventional filtration system of mechanical and activated carbon which are designed to maintain high amine quality. The good amine quality was confirmed by detailed analyses as shown in Table 1. What is Recommended to Alleviate Foaming Reoccurrence? Troubleshooting the amine foaming problem and operational experience revealed that this problem is periodic and could be controlled without any major modification to the exiting system. Therefore, it was decided to stop the continuous anti-foam injection practice. It was found that the most cost-effective method to abate foaming is to have better coordination between the upstream facilities and the gas processing plant. Producing facilities should alarm the gas plant to take the proper action whenever upsets occur in any of the following systems: gas refrigeration, gas dehydration and gas compression. Implementing this practice will allow gas treatment operations personnel to take the corrective action of injecting anti-foam (batch) to the amine solution and closely monitor plant operation. In addition, added benefits could be attained by installing a gap action control valve in the slug catcher liquid drainage system to prevent high liquid build up. TROUBLESHOOTING GUIDE Effective troubleshooting of foaming is a vital step in achieving a resolution to amine foaming. Operations engineers should be aware of several things in order to provide effective troubleshooting: • Understand the foaming concept, symptoms, and potential causes. • Check amine quality and treatment methods that include filtration and/or reclamation. • Examine sour gas quality and pretreatment equipment. • Review operation practices of the amine sweetening plant. • Respond proactively to the activities in upstream facilities that have the potential to cause problems in the amine system. SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 31 CONCLUSION Foaming in amine absorber columns has been a major concern in HP gas sweetening facilities in Saudi Aramco. Therefore, continuous anti-foam injection to suppress foaming has been the most popular remedial method. Investigation and troubleshooting of the foaming in two amine sweetening facilities reduced the reliance on the continuous anti-foam injection at Berri Gas Plant by identifying the main source of the problem; however, economics dictated continuing the anti-foam injection at Shedgum Gas Plant. Both case studies revealed that liquid hydrocarbon carry over with sour feed gas was the main foam promoter. A lesson learned from these two cases was to focus on defining the foaming problem. This allowed a better understanding of the problems and provided the least expensive solution to abate the foaming or reduce its severity. ACKNOWLEDGEMENTS This paper was previously published in the Oil & Gas Journal, August 27, 2007, under the title “Identifying Sources Key to Detailed Troubleshooting of Amine Foaming.” REFERENCES 1. Linga, H., Hinderaker, G. and Tykhelle, B.: “The Effect of Hydrocarbon Condensate and Anti-foaming Agents on the Performance of CO2 Absorption with Activated MDEA,” presented at the 52nd annual Lawrence Reid Gas Conditioning Conference, Norman, Oklahoma, February 24-27, 2002. 2. Pauley, C.R., Hashemi, R. and Caothien, S.: “Analysis of Foaming Mechanisms in Amine Plants,” presented at the 39th annual Lawrence Reid Gas Conditioning Conference, Norman, Oklahoma, March 6-8, 1989. 3. Al-Ghamdi, A.M.: “Study Underscores Effectiveness of Anti-foaming Agent in DGA Sweetening Process,” Oil and Gas Journal, May 20, 2000, pp. 62-69. 4. Pauley, C.R., Hashemi, R. and Caothien, S.: “Ways to Control Amine Unit Foaming Offered,” Oil and Gas Journal, December 11, 1989, pp. 67-75. 32 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 5. Khull, A. and Nielsen, R., Gas Purification, 5th Edition, Gulf Publishing Company. 6. Pauley, C.R.: “Face the Facts about Amine Foaming,” Chemical Engineering Progress, July 1991, pp. 33-38. 7. von Phul, S.A.: “Sweetening Process Foaming and Abatement,” presented at the 51st annual Lawrence Reid Gas Conditioning Conference, Norman, Oklahoma, February 25-28, 2001. 8. von Phul, S.A.: “Sweetening Process Foaming and Abatement Part II: Case Studies,” poster session in the 52nd annual Lawrence Reid Gas Conditioning Conference, Norman, Oklahoma, February 24-27, 2002. 9. Khatib, Z.I.: “Reduction of Entrainment of Aerosols in Gas Streams,” presented at the 47th annual Lawrence Reid Gas Conditioning Conference, Norman, Oklahoma, March 2-5, 1997. 10. Harruff, L.G.: “Saudi Arabian Experience with DGA Units and Related Sulfur Plants,” presented at the 48th annual Lawrence Reid Gas Conditioning Conference, Norman, Oklahoma, March 1-4, 1998. 11. Katz, D.L.: “Retrograde Condensate in Natural Gas Pipelines,” presented at the 23rd annual Lawrence Reid Gas Conditioning Conference, Norman, Oklahoma, 1973. SmartWell Completion Utilizes Natural Reservoir Energy to Produce High Water-Cut and Low Productivity Index Well in Abqaiq Field Nashi Al-Otaibi Abdulwafi A. Al-Gamber Michael Konopczynski Suresh Jacob Nashi Al-Otaibi is a Senior Engineer with the Abqaiq Production Engineering Division of Saudi Aramco’s Southern Area Production Engineering Department (APED/SAPED). Nashi holds a B.S. in Petroleum Engineering from King Fahd University of Petroleum and Minerals (KFUPM), Saudi Arabia. He has worked in several petroleum engineering departments within Saudi Aramco, including production engineering, and reservoir management and the EXPEC Advance Research Center (EXPEC ARC). Nashi is an active member with the Society of Petroleum Engineers (SPE). Abdulwafi A. Al-Gamber is the Superintendent of the North Ghawar Well Services Division of the Southern Area Production Services Department. Previously, he held supervisory positions in the Abqaiq Production Engineering Division. Abdulwafi has a B.S. degree in Petroleum Engineering from King Fahd University of Petroleum and Minerals (KFUPM), Saudi Arabia. He has more than 20 years of experience in production engineering, reservoir engineering, drilling and workover engineering/operations, and producing operations. Michael Konopczynski is the Manager of Reservoir Solutions and Commercialization at WellDynamics International Ltd., where he is responsible for providing petroleum engineering support for the application of SmartWell technology. Prior to joining WellDynamics in 2001, Michael was an employee of Shell Canada Ltd. in a variety of production engineering and technology roles for close to 20 years. His assignments with Shell included projects for steam assisted thermal recovery, CO2 enhanced recovery, deep sour gas development, and gas-condensate developments in Canada, the United States and the Sultanate of Oman. Suresh Jacob is the Country Manager for WellDynamics in Saudi Arabia, where he is responsible for the technical and commercial support for WellDynamics’ operation in the Kingdom. He has over 10 years experience in well completion and has worked on several projects comprising the planning, installation and operation of SmartWell completions. Suresh received a B.S. in Mechanical Engineering from the University of Kerala, India in 1993 and a M.S. degree in Petroleum Engineering from the University of Texas A&M, College Station, TX in 2001. This application eliminates the need for artificial lift infrastructure at the surface and operational expenditures. Using gas cap energy basically is providing free energy. This article discusses selection criteria of smartwell application to naturally lift an oil producer by utilizing energy from an overlying gas cap, completion and operation experiences and production optimization. Results show the applicability of natural gas-lift dependent upon standoff (with respect to the initial gas-oil and water-oil contacts) and target production rate. It will also address design considerations for natural gas-lift applications and reports the operational experience gained in the Abqaiq field with gas cap gas-lift applications. INTRODUCTION ABSTRACT Reservoir Background Innovations and smartwell technology applications have helped overcome the challenges of complex and mature fields such as the Abqaiq field. This article presents the application of SmartWell technology in utilizing “free energy” from an overlying gas cap to produce high watercut and low productivity wells completed in underlying reservoirs. The smartwell completion was implemented in the Abqaiq field to naturally gas lift an intermittent well (a well which cannot continuously flow to the surface), completed in the low permeability Hanifa reservoir. The well is drilled through the gas cap having a 40 ft gas column in the upper section of the Arab-D reservoir. In this application, the smartwell completion consists of a surface controlled, hydraulically operated downhole choke valve that regulates the gas inflow from the gas cap into the production tubing. Abqaiq field was the first super giant field developed in Saudi Arabia. It is located at the North-Eastern tip of the Ghawar field in the Eastern Province of Saudi Arabia. The field was discovered in 1940, but full scale development did not begin until 1946. The field consists of a high relief south dome and a low relief north dome. The Abqaiq field produces from two main reservoirs, the Jurassic Arab-D and Hanifa reservoirs, separated by the 450 ft thick, nonreservoir Jubaila formation. The Arab-D (upper) reservoir is prolific throughout the whole field with an average permeability of 400 millidarcies (mD). The Hanifa oil reservoir (lower) is only present in the South Dome region. The matrix permeability of this lower reservoir is low (1 mD - 2 mD) with well productivity controlled by near wellbore fracturing. The oil in the Abqaiq field Arab-D and Hanifa reservoirs is Arabian Extra Light with an average API of 37° and Gas Oil Ratio (GOR) of 860 SCF/STB. First commercial production began in 1946 from ArabD. The field was initially produced in a primary depletion mode. In the time period from 1954-78, a crestal gas injection pressure support program was carried out in the primary Arab-D reservoir at the crest of the high relief South Dome. Water injection was started from 1956. After almost 60 years of production, the field watercut is still very low. Hanifa reservoir production started in 1954. Reservoir development and production picked up slightly in 1975 with implementation of gravity water injection. Production from Hanifa was limited and full development was slow due to the complex behavior of this fractured reservoir. Vertical communication between the two reservoirs is evident from production data, and is believed to be caused by faults and extensive fractures that cut through Jubaila1, 2. Figure 1 shows the gas cap in the top of Abqaiq field Arab-D reservoir. Fig. 1. Abqaiq field map and the gas cap is shown in red. 34 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 Hanifa Productivity The Hanifa oil reservoir is separated from the overlaying giant Arab-D reservoir by over 450 ft of the Jubaila formation. These two reservoirs are in pressure-fluid communication via a network of fractures through Jubaila impermeable carbonates. This reservoir communication together with the reservoir heterogeneity of the Hanifa, in the form of micro-pores and associated fractures, provides a challenge for reservoir geology and reservoir engineering to formulate a development plan, involving horizontal producers, to mitigate reservoir communication and to efficiently and effectively extract the reserves within the Abqaiq Hanifa reservoir. The low permeability (1-2 md) of Hanifa rock adversely impacts the wells productivity index and injectivity index (PI/II), which causes the Hanifa producers and injectors that are not in contact with big fractures to have very low rates1. In the case of the producers, the wells tend to flow below bubble point pressure. Moreover, these types of wells usually die at less than 40% water cut. On the injection side, the tightness of Hanifa makes it challenging on the flank injectors to provide adequate pressure support to the crestal producers. I N C E N T I V E S F O R N AT U R A L G A S L I F T UTILIZING FREE ENERGY Fig. 2. Abqaiq Well A completion schematic. To overcome the challenges of this complex reservoir, Saudi Aramco has carried out many projects, studies and field trials for new technologies to achieve the ultimate goal of enhancing oil recovery. An auto gas lift smartwell completion system was selected in AB-A as an alternative to conventional artificial lift methods, like an electric submersible pump (ESP). The concept of natural gas lift or auto gas lift has been discussed by Kumar, et al.3, Glandt described the application of intelligent wells to natural gas lift4, and others have described the application and benefits of intelligent well auto gas lift in the North Sea and in Brunei5, 6. The smartwell option utilizes the energy from the gas cap to lift the oil and eliminates the need for artificial lift infrastructure at the surface. The advantages of smartwells were the low operating cost and reduction in well intervention compared to conventional artificial lift methods like ESP. CONCEPTUAL DESIGN OF NATURAL GAS LIFT The design of natural gas lift with smartwell technology is different from the standard gas lift techniques that inject gas in the annulus and produce from the tubing through gas lift valves in side pocket mandrels. In the smartwell design, the gas from the Arab-D gas cap is produced into the production tubing to gas lift the oil from the Hanifa intermittent well. The gas is controlled through a hydraulically actuated, remotely operated downhole flow control device. The valve is installed between two packers to isolate the individual zones along the well path. The interval control valve enables choking or shutting different zones according to the well performance like drawdown, GOR, water cut, etc. The control lines are used to hydraulically actuate the downhole interval control valve from the surface. Three conditions must exist to effectively implement sustainable auto gas lift in a well: 1. The pressure of the gas reservoir must be greater than the hydrostatic pressure of the column of fluid in the production tubing (to the depth of gas entry), plus the line-pack under static conditions, to “kick-off” the well. 2. The productivity of the gas reservoir must be great enough to produce sufficient gas for effective lift at moderate drawdown pressures. 3. The volume of gas reserves associated with the gas source must be large enough to maintain sufficient pressure and productivity throughout the life of the well and under a variety of producing conditions as the oil zone is depleted and water cut increases. SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 35 Fig. 3. Interval control valve. flow trim to be accurately moved through up to 11 predetermined positions. Accu-Pulse may communicate with either side of the ICV piston; it may drive the ICV open or closed. This allows incremental positioning in one direction8. In this application, the Accu-Pulse module was placed in the open side so that the valve may be cycled in incremental positions towards full opening. This configuration allows the choke to be directly closed from any open position without having to open any further. By matching Accu-Pulse with a specific ICV flow trim design, the system can be optimized for gas injection requirement. The ICV valve was designed with this in mind and provides a customizable flow trim element allowing Accu-Pulse and the valve to be matched to gas lift requirements. GAS TRIM CHOKE DESIGN Fig. 4. Accu-Pulse control system. Figure 2 shows the well completion and the different downhole components of the smart auto gas lift completion. I N T E R N A L C O N T R O L VA LV E ( I C V ) The Interval Control Valve (ICV) was used to control lift gas from the Arab-D gas cap to the lower Hanifa reservoir. This ICV has 11 positions, including fully open and fully closed. The ICV is hydraulically operated from the surface through ¼” control lines. A minimum control line differential pressure of 250 psi is needed to unlock the metal-to-metal seal in the choke. This feature prevents inadvertent opening of the choke by the friction of the fluid. Once unlocked, the choke can then be fully or partially opened to any position by applying pressure on the open line. The choke may be returned to the closed position by applying pressure to the close line8. The ICV is shown in Fig. 3. The design process for an auto-gaslift application must consider the range of possible uncertainties related to reservoir and well performance throughout the life of the well. The following key parameters must be considered in the design process, including the range of values of these parameters representative of both reservoir uncertainty and expected changes over the functional life of the well: 1. Gas zone productivity index. 2. Gas zone reservoir pressure (including future depletion). 3. Gas zone fluid composition. 4. Oil zone reservoir pressure (including future depletion). 5. Oil zone productivity index. 6. Oil zone fluid composition (particularly water cut and natural GOR). The evaluation and design process is based on nodal analysis to determine the viability and sustainability of the auto-gaslift application, to establish the optimum completion geometry (production conduit size), and to specify the ICV choke Cv profile to provide optimum gas ACCU-PULSE™ CONTROL SYSTEM The Accu-Pulse Control System, shown in Fig. 4, is used in conjunction with the SmartWell Control System to incrementally open a multi-position ICV. Accu-Pulse provides incremental movement of a suitable ICV flow trim by exhausting a predetermined amount of control fluid from the ICV piston. The capability to recharge and exhaust the same amount of fluid repeatedly allows the ICV 36 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 Fig. 5. Gas lift performance curves. Fig. 6. Flowing bottom hole pressure. Fig. 8. CV profile for gas zone chokes. Fig. 7. Gas zone IPR. Fig. 9. Types of flow control valve choke trims. lift controllability over the range of reservoir uncertainties and changes in future operations7. The evaluation and analysis process is as follows: 1. Gas lift performance curves (gross flow rate and flowing bottom-hole pressure vs. lift gas injection rate) for the oil zone with a fixed flowing tubing head pressure are generated using nodal analysis software/wellbore simulator. Curves are generated for the anticipated range of oil zone productivity indices, oil zone reservoir pressures, and water cuts, Fig. 5. From these curves, the lift gas rate resulting in maximum productivity (minimum flowing bottomhole pressure (FBHP)) and the lift gas rate resulting in a flowing bottom-hole pressure equivalent to the minimum desired inflow pressure are identified, Fig. 6. 2. Using the gas lift performance curves, the flowing production conduit pressure at the point of lift gas injection is calculated based on tubing outflow performance as a function of gas injection rate. This pressure comprises the “downstream” pressure of the auto gas lift flow control valve. 3. Inflow performance curves for the gas zone are generated, resulting in gas zone inflow pressure as a function of flow rate. These pressures comprise the “upstream” pressure of the auto-gaslift flow control valve, Fig. 7. 4. At any particular lift gas flow rate, the difference between the pressure established in Step 3 (gas zone inflow pressure) and the pressure established in Step 2 (production conduit flowing pressure at gas injection depth) as a function of lift gas injection rate constitutes the pressure drop required across the autogaslift control valve. Based on this relationship between lift gas rate and pressure drop across the control valve, the Cv profile for the control valve can be established, Fig. 8, and the physical geometry of the choke trim can be designed. 5. The process is repeated for the range of reservoir and productivity parameters expected. Using the optimum lift gas rates identified in Step 1, the corresponding flowing bottom-hole pressures for the gas reservoir are established. The best choke Cv profile which satisfies the majority of production scenarios and offers good lift gas control over the range is selected. Based on well data and choke modeling an equal SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 37 percentage type choke was selected for this application. Figure 9 shows the performance of an equal percentage type in comparison to the other designs. The ICV in combination with the Accu-Pulse choking system will provide 11 choke settings with a flow capability of 0-20 MMscfd through the choke. The equal percentage type of choke trim is the best solution for this type of application because it is well suited for flow control applications where the entire system (inflow – outflow) absorbs a large pressure drop as a function of flow rate. In a reservoir/wellbore system, the friction pressure drop through the permeable reservoir rock surrounding the wellbore (inflow), and the friction pressure drop in the production tubing to surface (outflow) absorb a large percentage of the controlling pressure drop, hence the equal percentage type of flow trim is the most applicable for downhole flow control design. The other benefit of this design is that it permits a “soft start” of the lift gas addition, avoiding potential slugging and inlet separator destabilization, and easing lift gas optimization for variable well flow conditions. The hydraulic control lines transmit the hydraulic pressure necessary to manipulate and control the downhole ICV8. There are two hydraulic lines connected to the open and close side of the control valve. The lines are encapsulated in wear resistant plastic as shown in Fig. 11 and securely clamped to the outside of the production tubing. I S O L AT I N G PA C K E R S S U R FA C E H Y D R A U L I C S Y S T E M Two HF-1 hydraulically set retrievable packers were used to isolate the perforated interval of the Arab-D gas cap from the Hanifa reservoir. The packer is designed for smartwell applications and has the facility for bypass of electrical and hydraulic control lines without the requirement for splicing. The HF-1 packer can be used as both the top production packer and as one of many lower packers isolating adjacent zones8. Its design enables all tubing loads to be transmitted to the casing and prevents movement of the production tubing and control lines. The HF-1 packer is shown in Fig. 10. The Surface Hydraulic System is a critical component of any smartwell completion. The system cleans, pressurizes and distributes the hydraulic control fluid required to operate the downhole valve8. A typical hydraulic unit was used to actuate the downhole ICV. It has a built-in hydraulic pump and accumulator as well as all required gauges on the inlet and outlet to monitor and operate the ICV, Fig. 12. Fig. 11. Hydraulic control lines encapsulated in wear resistant plastic. HYDRAULIC CONTROL LINES WELLHEAD OUTLETS REQUIREMENTS A special modified tubing hanger and bonnet were used, Fig. 13. This tubing hanger and bonnet were equipped with feed- Fig. 10. Control lines going through the HF-1 Packer. 38 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 Fig. 12. ICV Surface Hydraulic Control unit. Fig. 14. Well performance before starting natural gas lift. Fig. 13. Tubing hanger modifications. through ports for the control lines in the smartwell completion system and for the subsurface safety valve. The lines were isolated outside the wellhead using needle valves. The surface hydraulic panel was connected to the downhole lines to control the downhole valves and subsurface safety valve. SELECTION CRITERIA In most cases, multiple options are evaluated to select the candidate well. The concept of gas lifting the Hanifa with the Arab-D gas cap was our primary goal. After evaluating many options, AB-A was selected because it is located in the middle of the south dome which has the gas cap on top of the Arab-D reservoir. The well was drilled and completed as a highly deviated open hole Hanifa producer in May 1998. The well was drilled through the Arab-D gas cap, which was isolated by a 7” liner. The well was put on production in October 1998 and has been flowing at low bottom-hole pressure since then. It was an intermittent producer because it must be shut-in when its FBHP comes close to the bubble point pressure. The rate of the well has been declining since it was put on production in October 1998 even after the stimulation treatment. The decline became more severe when the well started producing water in September 1999. well. Diagnostics conducted by the vendor found the control line damaged below the wellhead. This does not affect the functioning of the downhole valves and it is fully functional. WELL PERFORMANCE Figure 14 shows a plot of the production performance of the well. The plot shows the rate the well has been declining since it was put in production in October 1998. The well was initially producing 4,000 barrels per day (BPD) dry oil at 50/64” choke. That rate started declining shortly after the initial production of the well and the well was still dry at that time. This decline became more severe when the well started producing water in September 1999. To compensate for the sharp decline in rate, the choke was gradually relaxed until it was fully opened in May 2001. The well was shut-in several times to build up the pressure when the pressure surveys showed that the well flowing bottom-hole pressure was close to bubble point pressure. This behavior continued even after the acid stimulation performed in April 2002 when its productivity index (PI) improved from 1.6 BPD/psi to 5.6 BPD/psi. The well was worked over in December 2004 to install the smart completion with natural gas lift. The ICV was function tested after completion and was found functioning properly. The ICV was cycled several times successfully to all WELL COMPLETION AND SYSTEM DEPLOYMENT A 40 ft section of gas cap was perforated in the Arab-D during the workover to convert to gas lift smartwell. The two packers straddle the gas cap and the downhole choke valve was placed in the gas cap to control the gas rate flowing into the 4½” production tubing. A permanent monitoring system consisting of a Venturi flow meter and downhole gauges were installed as part of the completion. Though these were functional at the time of completion, they were not working at the time of commissioning the Fig. 15. Well performance after starting natural gas lift. SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 39 positions. After installing and commissioning the ICV surface hydraulic control system, another function test for the ICV was conducted and found satisfactory. When the well tie-in work was completed, the well was unable to flow. The ICV was opened to help unload the well and bring it back to production. At ICV position 5, the well was successfully unloaded and the initial oil production was at 3,700 BPD at 36% water cut on 68/64” choke. Long-term production rates have averaged approximately 1,700 BPD with 35% water cut on 43/64” choke. The rate was optimized after several tests performed at different ICV positions. During these tests FBHP was monitored to make sure that the well is flowing at pressure higher than the bubble point pressure. Production data in Fig. 15 shows that the smart gas lift completion has enabled the well to sustain production at higher water cut than before. Figure 15 is a chart showing Well A production using the natural gas lift option from February 2005 to August 2006. CONCLUSIONS Natural gas lift has achieved the objectives to sustain production from an intermittent well. The natural gas lift application in Abqaiq Well A has demonstrated the feasibility and benefit of using intelligent well technology. In particular, the project has shown that surface controlled downhole variable flow control valves are beneficial for control of the gas source zone in applications where there is a high degree of uncertainty for the production performance of the oil and gas zones. ACKNOWLEDGEMENT The authors would like to thank the management of Saudi Aramco and WellDynamics for their permission to publish this paper. N O M E N C L AT U R E FBHP Cv ESP ICV BPD GOR PDHMS MMscfd Flowing Bottom-Hole Pressure Coefficient of Variation Electric Submersible Pump Interval Control Valve Barrels Per Day Gas Oil Ratio Permanent Downhole Monitoring System Million standard cubic feet per day REFERENCES 1. Grover Jr., G.A.: “Abqaiq Hanifa Reservoir: Geologic Attributes Controlling Hydrocarbon Production and Water Injection,” SPE paper 20607, presented at the SPE Middle East Oil Technical Conference and Exhibition held in Bahrain, April 3-6, 1993. 2. Al-Garni, S.A., et al.: “Optimizing Production/Injection and Accelerating Recovery of Mature Field through Fracture Simulation Model,” IPTC paper 10433, presented at the International Petroleum Technology Conference held in Doha, Qatar, November 21-23, 2005. 3. Kumar, A., Telang, J.K. and De, S.K.: “Innovative Techniques to Maintain Production from a Problematic Indian Offshore Field – A Case History,” presented at the 1999 SPE Latin American and Caribbean Petroleum Engineering Conference, Caracas, Venezuela, April 2123, 1999. 4. Glandt, C.A.: “Reservoir Aspects of SmartWells,” SPE paper 81107, presented at the SPE Latin American and Caribbean Petroleum Engineering Conference, Port-ofSpain, Trinidad, April 27-30, 2003. 5. Betancourt, S., Dahlberg, K., Hovde, O. and Jalali, Y.: “Natural Gas-Lift: Theory and Practice,” SPE paper 74391 presented at the SPE International Petroleum Conference and Exhibition, Villahermosa, Mexico, February 10-12, 2002. 6. Jin, L., Sommerauer, G., Abdul-Rahman, S. and Yong, Y.C.: “Smart Completion Design with Internal Gas Lifting Proven Economical for an Oil Development Project,” SPE paper 92891, presented at the 2005 Asia Pacific Oil & Gas Conference and Exhibition, Jakarta, Indonesia, April 5-7, 2005. 7. Konopczynski, M.R. and Ajayi, A.: “Design of Intelligent Well Downhole Valves for Adjustable Flow Control,” SPE paper 90664, presented at SPE ATCE 2004, Houston, Texas, September 26-29, 2004. 8. WellDynamics library: “Library_section/pdfs/smartwell systems,” via (http://www.welldynamics.com). S I M E T R I C C O N V E R S I O N FA C T O R S ft x 3.048* E-01 psi x 6.894757 E+00 bbl/d x 1.589873 E-01 in x 2.54* E+01 * Conversion factor is exact 40 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 m kPa m3/d mm Shaft Misalignment and Vibration - A Model Dr. Irvin Redmond Dr. Irvin Redmond re-joined Saudi Aramco in 1998 and is currently an Engineering Specialist in the Rotating Equipment Division of Consulting Services Department. Irvin completed his B.Sc. (with honors) in 1974 and M.Sc. in Mechanical Engineering in 1981 at Strathclyde University, Glasgow, later returning to obtain a Ph.D. in Vibration Control of Rotating Machinery in 1985. Before joining Saudi Aramco, he worked extensively in the design, development and troubleshooting of a variety of rotating equipment. Dr. Redmond has published a number of technical papers and presented at international conferences in the field of machinery vibration. He is a Chartered Engineer (UK) and a corporate member of the Institution of Mechanical Engineers. ABSTRACT Misalignment of coupled rotating machinery shafts is a frequently occurring problem which can have a substantial influence on equipment reliability. Experience has shown that diagnosis of misalignment through vibration analysis can be extremely difficult due in large part to the observed substantial variability in the character of machinery vibration even when apparently identical alignment states exist. This article presents the results of a theoretical study on a simple linear rotordynamic model, capable of simulating the effects of parallel and angular misalignment across a flexible-element coupling connecting drive and driven rotors. In contrast to other works the complex system forces and motions are derived by application of the Lagrange Method without the imposition of specific harmonicexcitation assumptions. The model results confirm that a system having purely linear properties when subjected to parallel misalignment can exhibit complex multiharmonic vibration response. Support stiffness anisotropy is shown to be an important parameter in determining the presence and level of first (1X) and secondharmonic (2X) vibration response. Coupling of the lateral-torsional motions is demonstrated as being key to the production of multi-harmonic system response. The results provide significant insight into some of the major controlling elements of the vibration-misalignment relationship in a linear system. N O M E N C L AT U R E a, b Shaft dimensions c Load torque constant Cx, Cy, Ct, Cz Damping constants (x and y lateral, torsional and axial) ft, fz Dimensionless frequencies (torsional and axial) g Gravitational constant h Dimension defining mass/inertia location on shaft I1, I2 Rotor Polar Moments of Inertia k1 kx, ky, kt kz, kc Dimensionless support stiffness ratio (= kx/ky) Stiffness constants (x and y lateral and coupling torsional, axial and angular) L Shaft Length m r1, r2 t Ti, TL Rotor mass Rotor radii of gyration Time Time Input Torque, Load Torque X1, X2, Y1, Y2 Shaft linear displacements at bearings 1 and 2 on rotor 2 z Axial displacement α αo Shaft angular displacement about x axis Angular misalignment about x’-axis Shaft angular displacement about y-axis Angular misalignment about y’-axis β βo δ ζx, ζy, ζz, ζt, Shaft Parallel offset (misalignment) Damping Ratios (x and y lateral, axial and torsional) ψ φ θ Rotor 1 rotational displacement Rotor 2 rotational displacement Parallel misalignment reference angle ωnT, ωnY, ωnZ Natural Frequencies – Torsional, y-Lateral & Axial INTRODUCTION Shaft misalignment has major implications for modern day rotating equipment reliability. Although effective alignment techniques have been applied successfully on a wide range of equipment for some time, deterioration of the alignment state can frequently occur due to, for example, changes in equipment operating conditions, foundation settlement and piping strain1. This situation can lead to the imposition of excessive forces on the equipment rotating and static elements, most commonly resulting in bearing or coupling failure. In extreme circumstances contact between rotating and stationary components can be expected to occur. 42 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 The presence of shaft misalignment can greatly influence machinery vibration response2. It’s detection through vibration diagnostics is not a straightforward matter due to the lack of a clear understanding of the physical mechanism relating shaft misalignment to vibration. Published work in this area is extremely limited. For instance, frequent reference is made to the appearance of a second-harmonic (2X) vibration component as a possible indication of shaft misalignment, though there does not appear to be any definitive work demonstrating analytically how or when this phenomenon would be expected to occur. Dewell and Mitchell3 investigated the vibration spectrums produced by a misaligned flexible disk coupling and showed that (2X) and (4X) frequency components could be used to detect the presence of misalignment. Jackson4 described the emergence of a (2X) vibration component resulting from the nonlinear properties of oil-film bearings when preloaded due to misalignment forces. Simon5 modeled misalignment in a large turbo-machinery and computed the vibration response based on assumed values for the coupling reaction forces, the form of which was not disclosed. Xu and Marangoni6, 7 studied, analytically and experimentally, the vibration response of a misaligned motor-driven system. The coupling was assumed to exhibit Hooke’s-joint characteristics, thereby leading to even frequency shaft speed fluctuations resulting in (2X) rotor response. Sekhar et al.8 and Arumugam et al.9 predicted multi-harmonic response from rotordynamic systems subjected to angular and parallel misalignment by assuming coupling transmitted forces to be represented by a half-sinusoid function having fundamental frequency equal to twice the rotational speed. Prabhakar10 applied the same coupling force assumptions and investigated the transient response of a misaligned rotor system. They reported success in identifying the presence of coupling misalignment through the application of wavelet techniques. Redmond and Hussain11 analyzed the vibration resulting from a simple linear rotor model on isotropic supports and showed the dominant response to be similar to that resulting from a shaft bow. The predicted vibration response did not contain any second-harmonic content. Hussain and Redmond12 extended the model to include torsional flexibility and demonstrated the influence of lateral-torsional coupling. Shaft lateral response was shown to occur at frequencies corresponding to shaft running speed and torsional natural frequency. No double frequency response was observed. It is clear from the literature that the relationship between shaft misalignment and machinery vibration is still not fully understood. There is a real need for a simple mathematical misalignment model which would exhibit the basic characteristics of real rotordynamic Fig. 1. Flexible Element Coupling a) Schematic, and b) Coupling model. systems and thereby enable investigation of this common but complex phenomenon. This article presents such a model and investigates the influence of a number of system parameters on the vibration response resulting from misalignment. MISALIGNMENT MODEL Model Requirements In this article, the main objective is to produce a model which helps explain the complex misalignment-vibration relationship in rotordynamic systems. More specifically, the model is intended to address the mystery of the source of (2X) vibration, commonly cited as proof of misalignment in rotating equipment. To gain an understanding of this unexplained phenomenon it is important that the selected model be simple in nature to aid in transparency. As a first step towards this, the system dynamic motions should preferably be derived without recourse to assumptions of component (e.g., coupling) nonlinear behavior. With this in mind, the study presented within is confined to that of a rotor system having purely linear properties. Only shaft misalignment is considered and other excitation sources such as mechanical unbalance are not considered at this stage. Additionally, axi-symmetry is assumed throughout the rotating elements. Coupling Model The coupling model employed here was selected to reflect the characteristics commonly attributed to flexible element couplings, namely radial-rigidity and angular, axial and torsional flexibility. The coupling has one articulation point, Fig. 1a. The shaft ends are considered to be connected by a frictionless pinned-joint across which a linear rotational spring, kc, exerts a moment proportional to the relative angular displacement at the coupling, Fig. 1b. Since axi-symmetry is assumed, then kc is a constant. The coupling allows for relative axial and torsional motions of the shafts through the respective stiffnesses kz and kt. Corresponding axial and torsional damping is provided by the coefficients Cz and Ct. Fig. 2. a) Double-rotor misalignment model, and b) Coupling angular offset schematic. System Model The model consists of two coupled rigid rotors as shown in Fig. 2a. For simplicity, rotor 1, considered the drive rotor, is restrained by rigid supports while rotor 2 is supported on flexible damped supports having anisotropic properties. The model has 5 degrees of freedom. The torsional displacements of rotor 1 and rotor 2 are defined by ψ and ϕ respectively. Variables α and β denote the rotational displacements of the driven end of rotor 2 about the x’ and y’ axes, respectively, while z represents the axial displacement of rotor 2. The model is shown in Fig. 2a with parallel misalignment, δ, greatly exaggerated for clarity purposes. In these circumstances, the shaft system is initially in an “unstressed state” before rotation begins. In contrast, when angular misalignment α0 and β0 is present, rotor 2 supports will be subjected to an induced preload even before rotation – it’s value dependent upon the amount of misalignment and the relative stiffnesses of the coupling and supports. SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 43 In the case where the shafts are aligned but coupling halves are non-concentric with the shafts, the system response can also be computed considering parallel misalignment as presented within. When a coupling-half is mounted on it’s shaft with an angular offset, τ, as in Fig. 2b, then the situation is quite different from conventional shaft angular misalignment and needs to be accounted for separately in the system equations. Therefore this angular offset effect is included in the model equations presented within. (7) Defining the following dimensionless parameters: (8) Where (9) The dimensionless system matrices become: Dimensionless Mass matrix: Derivation of Model Equations The equations of motion for the coupled system are derived from application of the Lagrange equations to the system energy functions. (10) Energy Expressions Dimensionless Damping matrix: The system generalized coordinate is described by: (1) (11) The system kinetic energy, T, can be written as: Dimensionless Stiffness matrix: (2) The system potential energy, V, can be written as: (12) (3) and the Dimensionless Force Vector is: where the symbol (‘ ) denotes differentiation with respect to time. Nondimensional Equations of Motion Upon substituting the kinetic and potential energy expressions into Lagranges’s equation and introducing nonconservative damping forces from work done considerations, the system equations of motion may be obtained and nondimensionalized by dividing through by mω2nyL 2 to give: (13) (4) For clarity purposes, the system excitation force terms in equation (13) have been separated into static and dynamic components. The system equations are clearly nonlinear and the model degrees of freedom are both statically and dynamically coupled. It is notable that parallel misalignment dynamically couples the lateral and torsional system motions (eqns. 10, 11 and 13) in addition to introducing static “preload” forces (rows 1 and 2 of eqn. 13). In contrast, angular misalignment alone provides only static forcing of shaft lateral motions (rows 1 and 2 of eqn. 13). Where the dimensionless system generalized displacement, velocity and acceleration vectors are defined as follows: (5) (6) 44 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 More importantly, equation (13) very clearly shows that parallel misalignment produces both first (1X) and second (2X) harmonic torsional excitation forces. The magnitude of the fundamental forcing term is proportional to the support stiffness values while that of the double-frequency term increases in proportion to the x–y support stiffness anisotropy, k1. This is a very important feature as most real rotor systems incorporate bearings whose stiffness increases with increasing static loading. The equations already show that the presence of misalignment leads to the imposition of static bearing or support loading so it is clear that in such systems increasing the misalignment would produce a greater static preload thereby augmenting the bearingsupport anisotropy leading to further reinforcement of the (2X) torsional excitation. It is evident that the character of the resulting vibration response, particularly in relation to the presence of (1X) and (2X) components, will be dependent upon numerous system parameters, not least the proximity of the system lateral, torsional and axial natural frequencies to the system main excitation frequencies. This probably explains the substantial variability in observed vibration response in apparently similarly aligned rotating machinery trains. This situation is even more understandable when one takes into account the other numerous potential sources of (1X) and (2X) vibration. Finally, referring to equation (13), the introduction of coupling angular offset results in lateral excitation of rotor 2 at a frequency corresponding to the fundamental rotational frequency (1X). Where (16), (17) Therefore, shaft angular misalignment produces only a static displacement and system vibration does not occur. Note that rotating-element asymmetry, which can be present in some systems, has been ignored in this analysis. Its presence, for example in a disc coupling3, would lead to oscillatory system motions. The above equations are used to create Figs. 3a and 3b. These Figures show the influence of coupling angular stiffness and transmitted torque on rotor 2 displacement when isotropic supports are assumed (k1=1.0) and α* is set to a realistic value of 0.1. It is seen that at low coupling stiffness (kc*→ 0) the shafts tend to rotate at a misalignment angle equal to the original misalignment (α0) with minimum load transferred to the bearings, while for high coupling stiffness (kc*→∝) the shafts rotate at a reduced misalignment angle since the bearings become preloaded to counter the increased coupling transferred moment. The Figures also demonstrate how increasing the transmitted torque leads to a decrease in the misalignment angle, Fig. 3a, in the y-z plane but induces misalignment of the shafts in the orthogonal x-z plane, Fig. 3b, leading to an increase in the bearing static loading. A N A LY S I S Shaft Angular Misalignment Only The influence of angular misalignment is most easily demonstrated by simplifying the system dimensionless equations of motion (eqn. 4) through removal of terms related to the model axial degree of freedom, z*. Then consider rotor 2 mass to be concentrated at the right-hand end of the shaft (h*=1.0) and eliminate parallel misalignment (θ=0.; p=0) and coupling angular offset (τ=0) effects. Only the equations related to α and β degrees of freedom are coupled. When these equations are combined and the shafts are assumed to be initially angularly misaligned by an amount α0 about the x-axis (β0=0) the resulting shaft angular displacements α and β can be shown to be time-invariant and are determined from: (14), (15) Fig. 3. Influence of Coupling Stiffness, and Transmitted Torque, a) b) v’s TL*. v’s TL* ; SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 45 Fig. 4a. β vs. rotor 2 speed. Fig. 4c. Axial displacement frequency response. Fig. 4b. Rotor 2 displacement orbits. Fig. 4d. Support/Coupling load frequency response. Interestingly, the torque-induced β displacement is seen to have zero value at zero transmitted torque, TL*and low values at high torque, but reaches a peak at some intermediate torque value, in this case at TL*=1. It is important to note that the introduction of these static displacements will also lead to the creation of alternating stresses in the rotating elements. (h* =0.55). The shaft support configuration remains as defined above in section 3.1.1 (i.e., a* = 0.1) and gravity, shaft angular and shaft parallel misalignment effects are ignored (g* = 0; α0 = 0; β0 = 0; p = 0; θ=0). The dimensionless drive torque, Ti* is assumed constant at 5.0e5 and the related load torque, TL* is defined by the square-law relationship TL*= c.φ’*2 where c = 2.22e-5, so as to provide a nominal rotor 2 dimensionless final running speed of φ’*=1.5. The dimensionless critical speed in line with the y-axis, of course, occurs at a frequency corresponding to φ’*=1.0. System damping parameters are selected as ζx = ζy = .03; ζz = .01; ζT = .002. Dimensionless coupling stiffness, kc* = 0.1. The dimensionless axial and torsional natural frequencies were chosen as fz = 0.1 and ft = 1.0, respectively. Figures 4a, 4b, 4c and 4d shows the computed system responses for a range of Angular Offset Coupling Considering the case where the coupling is angularly skewed on the shaft, Fig. 2b, the dimensionless equations of motion (eqn. 4) are solved numerically using a 4th order Runge-Kutte algorithm to determine the system transient and steady-state response. The dimensionless time step is set at Δt*=.03. For simplicity, the drive rotor inertia is considered large (r1 = 0.1) compared to the driven rotor (r2 = .01). Rotor 2 mass is assumed to be located at center span 46 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 Fig. 5a. Rotor speed transient at startup. Fig. 5b. System transient torques at startup. support anisotropy values, k1 = 1.0 to 4.0, when the coupling skew angle is set at τ = 0.003. In Fig. 4a the β transient response is presented from startup to full speed. The rotor angular response β occurs at rotor rotational frequency (1X). The critical speed in the x-direction increases with increasing anisotropy parameter k1. The resulting full speed shaft synchronous displacement orbits (at RH support) are shown in Fig. 4b. The orbits become elliptical when support anisotropy is present, i.e., when k1 ≠ 1.0. When support anisotropy is present, it is seen that shaft axial motion is also induced, Fig. 4c. In this case the frequency of vibration corresponds to (2X) rotor rotational frequency. The vibration is relatively small and results from the axial inertia forces produced by small axial displacements linked to rigid-body shaft rotation. Figure 4d shows the frequency character of the dimensionless moment loads experienced by the coupling and rotor 2 flexible supports. The support loads are seen to Fig. 5c. Steady-state rotor speed spectrum. Fig. 5d. Rotor steady-state displacement plots. occur at (1X) shaft rotational frequency. The nondimensional support load, Mβ*, which occurs in the direction of the x-axis increases with increasing support anisotropy while the corresponding orthogonal support load, Mα*, is not a function of support anisotropy owing to the definition of k1. Referring to the coupling dimensionless load, Mc* frequency spectrum, Fig. 4d, it is interesting to note that when support anisotropy is present the rotating components experience alternating loading at a frequency corresponding to (2X) shaft rotational frequency while for isotropic supports only steady loading is experienced by the rotating elements. Shaft Parallel Misalignment Only The case of parallel misalignment is addressed by analyzing the model described above for different support anisotropy, coupling stiffness and misalignment values, through numerical analysis of equation (4). Figures 5a and 5b show the transient plots of rotor speed and transmitted torque SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 47 Fig. 5e. Steady-state Y2 displacement spectrum. Fig. 5g. Steady-state axial displacement. Fig. 5f. Steady-state X2 displacement spectrum. Fig. 5h. Steady-state support/Cplg forces. during startup when a steady drive torque, Ti* = 5.e-5, is applied and isotropic supports are assumed. The parallel misalignment parameter p is set at .003 and the dimensionless steady-state rotor speed is chosen as φ’ = 0.5. The fluctuation in steady-state rotor speed resulting from parallel misalignment is evident in Fig. 5a. The system is subjected to an alternating “resistance torque,” Tr* (Fig. 5b) emanating from the parallel offset. This dynamic torque is balanced, at full speed, by the fluctuating load torque TL*. These fluctuations are seen to occur at a frequency corresponding to rotor speed and it’s harmonics, Fig. 5c. Of particular interest is the presence of a significant secondharmonic response component. This is to be expected since any (2X) torsional excitation will coincide with the torsional and y-lateral natural frequencies. It is seen that increasing the support anisotropy (i.e., increasing k1) has a marked effect in increasing the magnitude of the (2X) speed oscillation, due to the proximity of (2X) excitation. 48 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 The dimensionless rotor displacements, X2 and Y2, are computed at the right hand supports of rotor 2 for a range of support anisotropy values and the results are presented in Fig. 5d. Circular shaft orbit occurs when the supports have equal stiffness along the x and y axes. The orbit centers, of course, do not coincide with the axes origin but take up a position between this point and the initial offset point thereby leading to static loading of the supports and coupling. This is particularly true when the support stiffness in the x-direction is increased (k1 > 1) where it is evident that the shaft is then forced to take up a static position closer to the x-y origin and further from it’s initial position. In addition, the shaft displacement orbits become less circular and more distorted as the x-y support stiffnesses diverge. The influence of support anisotropy on the spectral content of the shaft displacement responses X2 and Y2 is demonstrated in Figs. 5e and 5f, respectively. Shaft displacement response along the y-axis, Y2, occurs at the fundamental rotor frequency and second-harmonic and is generally increased with increasing support anisotropy, Fig. 5e. In contrast, displacement X2 also exhibits (3X) response and, as expected, all frequency components reduce in magnitude with increasing x-direction support stiffness. The frequency content of rotor 2 axial vibration response is displayed in Fig. 5g where it can be seen that, as with the other model coordinates, axial response is dominated by fundamental frequency activity along with significant double-frequency response. All frequency components are observed to be increased in magnitude when support anisotropy is augmented. A similar situation exists in relation to the dynamic support (or bearing) and coupling forces, Fig. 5h. The support dynamic forces in a direction in line with the misalignment plane also show a (3X) frequency component in addition to (1X) and (2X) frequency responses, at increased k1 values. The coupling experiences only (1X) dynamic forcing when isotropic supports are employed. When support anisotropy is introduced (2X), (3X) and (4X) components are observed to emerge. Increasing the parallel offset, p, has the effect of increasing the (1X) and (2X) vibration components as clearly shown in Fig. 6a and Fig. 6b, where k1 is set at 3. The increased offset produces a larger alternating resistance torque consisting mainly of (1X) and (2X) components, as observed in the steady-state speed waveform shown in Fig. 6c. This torsional excitation couples through to the lateral shaft motions to produce the distorted shaft displacement motion highlighted in Fig. 6d. The influence of dimensionless coupling angular stiffness, kc, in the presence of shaft parallel misalignment is clearly demonstrated in Figs. 7a and 7b. In this case, the support anisotropy parameter k1 = 3, parallel offset, p =.003 and all Fig. 6a. Steady-state α v β plots. Fig. 6c. Shaft Speed vs. Time (k1 = 3.). Fig. 6b. Shaft angular response, α and β. Fig. 6d. Rotor steady-state displacement plots. SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 49 CONCLUSIONS Fig. 7a. Shaft Speed vs. Time (k1 = 3). Fig. 7b. Rotor steady-state displacement plots. other parameters are as before. As would be expected, the rotor 2 displacements increase with increasing coupling stiffness. Referring to Fig. 7a, at low coupling stiffness values the shaft response is governed more by the support stiffness due to the enhanced coupling flexibility. This situation reverses as the coupling stiffness increases leading to increased transfer of the initial misalignment across the coupling. In these circumstances Fig. 7b shows the X2 shaft displacement response to be dominated by (1X) vibration along with significant (2X) and (3X) components. All of the frequency components are increased by increasing coupling stiffness. In the preceding parallel misalignment analysis the important system parameters, ft = 1.0 and φ’* = .05, were deliberately selected with a view to focusing on the emergence of system (2X) vibration response. More work will therefore be necessary to investigate system response for a wider range of controlling parameters. 50 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 A simple five degree-of-freedom linear rotor-system model, consisting of two flexibly-coupled rigid rotors, is presented to enable assessment of the relationship between shaft vibration and misalignment. The model is selected to display some of the important characteristics of present-day rotating machinery. Anisotropic flexible-damped supports and coupling torsional and axial flexibility are considered and the impact of shaft angular and parallel misalignment investigated. The resulting system coupled nondimensionalized equations of motion are shown to be nonlinear in nature. The individual lateral, axial and torsional responses are coupled and the relative response magnitudes will depend upon the degree of coupling and the proximity of the excitation frequencies with the system natural frequencies. The equations provide insight to the situation where only shaft angular misalignment is present and, surprisingly, demonstrate that in these circumstances system vibration does not occur. The resulting static displacements lead to static loading of the supports and dynamic loading of the rotating elements. The presence of coupling skew, or rotating angular misalignment, leads to the introduction of an angular displacement-forcing function at a frequency corresponding to the rotor speed. The system equations show clearly that parallel misalignment introduces a static displacement in addition to fundamental-frequency (1X) lateral and torsional excitation components. A discrete second-harmonic (2X) torsional excitation term is also evident in the system force vector. The magnitude of this term is directly proportional to the support anisotropy and disappears for isotropic supports. The above effects are demonstrated through numerical analysis of the equations of motion for a range of model parameters where it is confirmed that: • Both angular and parallel misalignment introduce a static loading, or preload, to the system. • Angular misalignment alone produces only static system displacements, in the absence of rotor and coupling asymmetry. The introduction of transmitted torque reduces the shaft misalignment angle leading to greater imposed static forces. • The presence of an angularly skewed coupling produces (1X) shaft lateral response when isotropic supports are employed. The introduction of support anisotropy leads to (2X) shaft axial response and (2X) loading of the rotating elements. • Parallel misalignment alone produces both static and dynamic, multi-harmonic (i.e., 1X, 2X and 3X) system responses. The presence of parallel offset introduces torsional response occurring mainly at fundamental and second-harmonic frequencies. The resulting speed oscillations couple through to the system lateral motions and produce multi-frequency support and rotating element forces. Parallel misalignment also induces shaft axial motion which is dominated by (1X) and (2X) response. Support anisotropy plays a major role in determining system dynamic response, with greater divergence of support orthogonal stiffness values leading to increased dynamic response. Increasing the parallel offset results in an increase of the (1X) and (2X) system dynamic response. The coupling stiffness is very influential in controlling the system response, as would be expected, so that a reduction in this parameter leads to reduced dynamic response, for a given parallel offset. As far as the author is aware there is nothing in the literature outlining the relationship between shaft misalignment and rotor vibration as demonstrated in this paper, particularly with respect to the importance of support anisotropy and lateral-torsional coupling in producing parallel misalignment related (2X) vibration and the inability of angular misalignment alone to produce shaft vibration. The model described within has already been developed to enable investigation of interaction of shaft misalignment with mechanical unbalance, nonlinear supports and rotating element asymmetry. Work is currently underway to expand the current investigations to assess the influence of these other “real world” rotordynamic influences. ACKNOWLEDGEMENTS The author acknowledges the support of Saudi Aramco, Saudi Arabia. REFERENCES 1. Piotrowski, J.: “Shaft Alignment Handbook,” Marcel Dekker Inc., New York, 2nd Ed., 1995. 2. Piotrowski, J.: “Why Shaft Misalignment Continues to Befuddle and Undermine Even the Best CBM and ProActive Maintenance Programs,” Proc. of the Predictive Maintenance Technology National Conference, Indianapolis, Indiana, 5:18-23, December 3-6, 1996. 4. Jackson, C.: “Considerations in Hot and Cold Alignment and Couplings,” Proc. 7th Intl. Pump Users Symposium, Texas A&M University, Texas, 1990, pp. 27-38. 5. Simon, G.: “Prediction of Vibration Behavior of Large Turbo-Machinery on Elastic Foundations Due to Unbalance and Coupling Misalignment,” Proc. Instn Mech Engrs, ImechE, Vol. 206, pp. 29-39, 1992. 6. Xu, M. and Marangoni, R.D.: “Vibration Analysis of a Motor-Flexible Coupling-Rotor System Subject to Misalignment and Unbalance, Part I: Theoretical Model and Analysis,” Journal of Sound and Vibration, Vol. 176(5), pp. 663-679, 1994. 7. Xu, M. and Marangoni, R.D.: “Vibration Analysis of a Motor-Flexible Coupling-Rotor System Subject to Misalignment and Unbalance, Part II: Experimental Validation,” Journal of Sound and Vibration, Vol. 176(5), pp. 663-691, 1994. 8. Sekhar, A.S. and Prabhu, B.S.: “Effects of Coupling Misalignment on Vibrations of Rotating Machinery,” Journal of Sound and Vibration, Vol. 185(4), pp. 655671, 1995. 9. Arumugam, S., Swarnamani, S. and Prabhu, B.S.: “Effects of Coupling Misalignment on the Vibration Characteristics of a Two Stage Turbine Rotor,” ASME Design Engineering Technical Conference, Vol. 3, Part B, 1995. 10. Prabhakar, S., Sekhar, A.S. and Mohanty, A.R.: “Vibration Analysis of a Misaligned Rotor-Coupling Bearing System Passing Through the Critical Speed,” Proc. Instn. Mech. Engrs., Vol. 215, Part C, 2001. 11. Redmond, I. and Hussain, K.M.: “Misalignment as a Source of Vibration in Rotating Shaft Systems,” Proc. Intl. Model Analysis Conf. (IMAC) XIX, Orlando, Florida, February 2001. 12. Hussain, K.M. and Redmond, I.: “Dynamic Response of Two Rotors Connected by Rigid Type Mechanical Coupling with Parallel Misalignment,” Journal of Sound and Vibration, Vol. 249(3), pp. 483-498, 2002. 3. Dewell, D.L. and Mitchell, L.D.: “Detection of a Misaligned Disk Coupling Using Spectrum Analysis,” Trans. ASME, Journal of Vibration, Acoustics, Stress and Reliability in Design, Vol. 106, pp. 9-18, January 1984. SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 51 New Coating Generations Offer Effective Solutions for Rehabilitation of Buried Pipelines Dr. Moufaq I. Jafar Dr. Fikry F. Barouky Faisal M. Melibari Dr. Moufaq I. Jafar is a Corrosion Specialist in Saudi Aramco’s Research and Development Center in Dhahran. He is an expert in coatings, cathodic protection and corrosion monitoring. Dr. Jafar has a Ph.D. in Corrosion Science and Engineering from the University of Manchester Institute of Science and Technology, Manchester, UK. He has written over 30 technical papers in the field of corrosion. Dr. Jafar is a Chartered Engineer (UK), a Professional Member of the Institute of Corrosion (UK), a Professional Member of the Institute of Materials, Minerals and Mining (UK), and a Member of the National Association of Corrosion Engineers (NACE, USA). He has served as Vice-chairman and Chairman of NACE, Saudi Arabian Section. Dr. Fikry F. Barouky is an Engineering Specialist in Saudi Aramco’s Consulting Services Department in Dhahran. He is the Chairman of Saudi Aramco Engineering Standards Committee for Paints & Coatings. Dr. Barouky has more than 33 years experience in the materials selection and corrosion control in the oil and gas industry, power generation, water desalination, and mining. He received a Ph.D. in Materials Engineering & Corrosion Science from Murdoch University, Australia. Faisal M. Melibari is a Laboratory Technical Specialist in Saudi Aramco’s Research and Development Center in Dhahran. He has 15 years of experience in the field of corrosion and non-metallic materials. Faisal has a B.Sc. in Chemistry from Surrey University, Guildford, UK. He has been involved with numerous technical projects in the field of coatings/non-metallic materials. 52 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 Dr. Barouky has written 36 technical papers in the field of protective coatings and corrosion. He is an active member of several professional and engineering associations, such as NACE, SSPC, ACA, Institute of Corrosion and the Institute of Materials. Coating Thickness Color System #1 2.6 mm Light Synthetic polyolefin with green PVC wrapping band System #2 2.0 mm Black Rubberized bitumen with geotextile fabric Black A two-component elastomeric system of polymer modified bitumen ABS T R AC T System #3 1.6 mm Description Saudi Aramco operates thousands of kilometers of buried pipelines, which require external corrosion protection, particularly in high water table areas known as “subkha” (salty) ground. Protective coatings have been the most costeffective passive corrosion control method utilized for the last five decades as the first line of defense against corrosion. The use of liquid coatings on new pipelines has not been successful compared to fusion bonded epoxy (FBE) in subkha ground. Also, for rehabilitation of buried pipelines, achieving good surface preparation is still one of the main factors, which causes premature failures of liquid coatings. A few years ago, Saudi Aramco started investigating alternative coating systems that are surface tolerant and having reliable chemical and mechanical properties for the external protection of pipelines in subkha ground. Visco-elastic coatings from different generic materials have been tested, qualified and successfully used as stand-alone coatings for external protection of buried pipelines. This article presents the results obtained from laboratory and field testing of three new coating systems. One coating system has been used in the field for 7 years without problems, whereas the other coating systems have been applied in the field for 1 year and are still being evaluated. Key words: corrosion, visco-elastic coatings, subkha, pipelines. Recently two more coatings (systems #2 and #3) were successfully evaluated in the laboratory and currently being evaluated in the field. Visco-elastic coatings are non-curable coatings with self-recovering characteristics. This type of coating adheres to the steel substrate, with little surface preparation and allows cold application on under and above ground facilities. There is no need for priming or high surface preparation (such as grit blasting to near-white finish), but the surface must be free of grease, dirt and loose materials. Coating system #1 comprise of the visco-elastic coating and a black PVC wrapping band. The corrosion protection is provided by the “paste” coating, whereas the PVC wrap is designed to apply pressure on the coating to enhance its adhesion to the steel substrate and to protect it from soil stresses. The two recently evaluated coating systems #2 and #3 are of a different generic type to coating system #1, Table 1. The two coatings have some properties, which are similar to those of system #1. These properties include self-recovery, visco-elasticity and the need for little surface preparation. All the coatings can be applied manually or with a wrapping machine. INTRODUCTION TEST PROGRAM Saudi Aramco operates thousands of kilometers of buried pipelines, which require external corrosion protection, particularly in subkha ground. The use of liquid epoxy coatings has not been successful in subkha ground compared to FBE coatings. Also, for rehabilitation of buried pipelines, good surface preparation is required and this is costly and time consuming. Therefore, there is a need for coatings, which require little surface preparation. Saudi Aramco has been investigating alternative coating systems for the external protection of buried pipelines in subkha ground. A few years ago, Saudi Aramco identified one visco-elastic coating (system #1), which has been used for the external protection of pipelines buried in subkha ground. Table 1. Details of the coating systems Holiday Detection A sample of each coating system was placed on a steel panel and tested in accordance with ASTM G62 to establish the presence of holidays, using a holiday detector (model Elcometer 236 Holiday Detector). The tests, which were carried out at 3,000 volts, showed no holidays in the coatings. Impact Resistance Impact resistance tests were carried out on the coatings to check the self-recovering characteristics of the coatings. The tests were performed at two different energy levels of 5 and 10 Joules, at room temperature (~ 23 °C). After testing, the SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 53 Coating 5 Joules (Self-recovery) 10 Joules (Self-recovery) System #1 Pass (good) Pass (good) System #2 Pass (good) Pass (good) System #3 Pass (v. good) Pass (good) Table 2. Impact resistance tests and self-recovery Coating Self-recovery/Elasticity System #1 Good System #2 Good System #3 Very Good Fig. 1. Temperature limitation test. Table 3. Self-recovery/elasticity properties of the coatings impact areas (dents) were visually examined for damage and tested using a low voltage (90 Volt) holiday tester. The three coating systems passed the impact test at 5 Joules and exhibited good to very good self-recovery of the impact area (dent disappeared). Each coating was subjected to holiday testing, and the results were all negative (no holidays in the coatings). At 10 Joules, the three coating systems passed the impact resistance test and exhibited good self-recovery. In all cases, coating system #3 exhibited the quickest recovery, whereas coating system #2 exhibited the slowest recovery, which may be due to the presence of the geotextile fabric on the back of the coating. The results of impact resistance tests are shown in Table 2. In addition to the observation of the coatings behavior after impact resistance testing, a small square sample of each coating system was pulled from one corner and released to check its self-recovery/elasticity. The coatings exhibited a good level of elasticity as summarized in Table 3. Coating system #3 exhibited the best self-recovery/elasticity. Chemical Resistance Small samples (approximately 5 cm2) of the coating systems were subjected to chemical resistance tests in acidic, neutral and alkaline solutions. One sample of each coating was immersed in each of the three solutions (initially pH 3, 7 and 10) at room temperature. The solutions were made up with deionized water and the pH was adjusted using a hydrochloric acid (HCl) solution to obtain pH 3, or a sodium hydroxide (NaOH) solution to obtain pH 10. The test cells were checked regularly for any change in the coatings or solutions. After two weeks of immersion in the test solutions, there was no change in the coating systems or solution. The pH of the solutions was adjusted to pH 2, pH 7 and pH 12, and the test was continued for another five months, during which there was no change in the coatings or solutions. 54 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 The three coating systems exhibited good performance in the three test solutions. The results suggest that the coatings are chemically stable, which is desirable for longterm corrosion protection. Any coating, in which chemical reactions take place, would not be stable and would change its properties/corrosion resistance in the long-term. Temperature Limitation The coatings were subjected to temperature limitation tests to obtain information on the thermal behavior of the coating and to establish the maximum operating temperature for each coating. A sample of each coating system (approximately 5 cm x 8 cm) was placed on a steel panel and weighed before being placed in an oven initially maintained at 60 °C. The panels were placed against the wall of the ovens (approximately a 60° angle, Fig. 1) to see if sagging of the coating would take place at the test temperature. The panels were exposed at 60 °C for 28 days, during which the coatings were unaffected. The test temperature was increased to 70 °C and maintained at this temperature for 90 days (a total of 118 days or 2,832 hours exposure at the two temperatures) to see the effect of higher temperature on the coatings. The test panels were examined regularly for any sign of sagging or increased stickiness/tackiness. At the end of the test period the panels were visually examined and weighed to see if Coating At 60 °C At 70 °C % wt. Loss System #1 No change Increased tackiness and stickiness 0.44 System #2 No change Increased tackiness and stickiness 0.18 System #3 No change Increased tackiness and stickiness 0.29 Table 4. Properties of coatings after heating to 60 °C and 70 °C Coating Initial After 1 Month After 4 Months After 8 After 12 Months Months System 1.75E+11 9.42E+10 7.52E+10 8.40E+10 6.62E+10 #1 System 1.35E+11 7.59E+10 9.70E+10 6.85E+10 6.72E+10 #2 System 1.64E+11 9.63E+10 5.47E+10 5.31E+10 3.26E+10 #3 Table 5. Electrochemical impedance results Fig. 2. Electrochemical impedance test cell and equipment. there has been any weight loss. At 70 °C the three coatings showed some increase in tackiness and stickiness, but no sign of sagging. The weight loss results from the coatings were very low, Table 4. The weight loss may be due to loss of moisture and light (a volatile) ingredient in the coatings. Upon completion of the temperature limitation test, the coatings were placed back in the ovens and the temperature was increased to 80 °C for one week to establish the maximum operating temperature for the coatings. The three coatings exhibited increasing stickiness, tackiness and some sagging. In summary, the results demonstrated that the maximum operating temperature for the coatings is 70 °C. Operating the coatings at a higher temperature would adversely affect their properties and performance. after 1 month showed a slight reduction in the electrochemical impedance of the coatings, which may be attributed to water uptake by the coatings. The reduction in the electrochemical impedance was very slow with increasing exposure time. The coatings continued to exhibit high electrochemical impedance (>1E+10 Ohm-cm2). Cathodic Disbondment Cathodic disbondment tests were carried out on the coatings to obtain information on the performance of the coatings under cathodic protection condition. Coated samples were exposed to the test solution (3% NaCl) after making a 6 mm hole in each coating. A stainless steel tube was used as the anode and a saturated calomel electrode was used as a reference electrode. A Solartron 1480 multistat was used to polarize the coated panels to –1.5 Volts for a period of 30 days at room temperature. Upon completion of the cathodic disbondment test, the coated panels were subjected to visual examination to establish the level of cathodic disbondment. The examination showed that there was no disbondment of the coatings around the hole, or undercreep corrosion. The coatings were adherent to the steel substrate and it was difficult to pull off the coatings from the steel substrate, Fig. 3. The high adhesion helped to prevent undercreep corrosion and coating disbondment. Field Trials An important part of the evaluation of any coating system in Saudi Aramco is field trials. Coating system #1 has been applied to several sections of pipelines buried in subkha ground with a high water table, Fig. 4. The coated sections were excavated at different intervals and visually inspected for any sign of coating degradation. Also, windows were cut in the coating to inspect the steel substrate, Fig. 5. All Electrochemical Impedance A computer controlled EG&G Frequency Response Analyzer (Model 1025) in conjunction with an EG&G potentiostat/galvanostat (Model 283) were used to conduct EIS measurements, Fig. 2. The test solution was sodium chloride (3% by wt). The impedance results obtained from EIS measurements are summarized in Table 5. The results showed that the initial impedance for all the coatings was very high (>1E+11 Ohm-cm2). The results Fig. 3. Appearance of hole after cathodic disbondment and removal of coating system #1. SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 55 Fig. 4. Excavation of coating system #1. Fig. 7. Inspection of coating system #2. Fig. 5. Inspection of coating system #1. Fig. 8. Coating system #3 before backfilling. Fig. 6. Coating system #2 before backfilling. Fig. 9. Inspection of coating system #3. the inspected coated pipelines were found to be in good condition with no sign of degradation, such as change in color or physical condition after 7 years of burial in subkha ground. Coating system #1 is currently being used by Saudi 56 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 Aramco for coating pipelines operating at temperatures up to 70 °C. The two other coating systems (#2 and #3) were applied last year to a pipeline buried in subkha ground, Figs. 6 to 9. The coated sections were visually inspected after six months, and windows were cut in the coatings to inspect the surface of the pipe. The inspection of system #2 showed that the coating was damaged at the bottom of the pipe (around the 6 O’clock position), which led to water ingress and corrosion of the pipe. The failure appeared to be due to poor application of the coating in this area, where the overlap of the coating was inadequate. There was no corrosion on the pipe surface in other areas where windows were cut in the coating. For coating system #3, the result of the visual inspection was better. There was no damage of the coating at the bottom or other areas of the pipe. There was good adhesion between the coating and the pipe and there was no corrosion on the pipe surface in areas where the window was cut in the coating. The overlap areas were intact. The field trial is still ongoing. CONCLUSIONS The results obtained from the test program have demonstrated the following: • The coatings are chemically stable and resistant to a wide range of pH levels (2-12). • The coatings have good self-recovering characteristics, which is important if the coatings are subjected to damage during installation or due to soil stresses. • The coatings have excellent electrochemical impedance. • The coatings have excellent cathodic disbondment resistance. • The coatings can be used for the corrosion protection of pipelines operating at temperatures up to 70 °C. ACKNOWLEDGEMENT The authors acknowledge the support of Saudi Aramco and the help provided by the staff of the R&D Center, Consulting Service Department and Pipelines Department during the course of this project. SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 57 Production Optimization Through Utilization of Innovative Technologies in an Offshore Field Environment Konstantinos I. Zormpalas Khalid Al-Omaireen Karam Sami Al-Yateem Konstantinos I. Zormpalas joined Saudi Aramco in July 2006 and has been working with the Safaniya Production Engineering Unit in NAPED. His focus on the Safaniya field activities are in production monitoring, well testing, the performance of wells equipped with Electric Submersible Pumps (ESP) and a selection of candidate wells for remedial work to enhance overall production. Prior to joining Saudi Aramco, he was the Production Engineer of a field in the Sahara desert in Algeria and worked throughout the project from the commissioning phase of the Central Processing Facility for oil and gas, to startup for the first oil and to full field development. His background includes 15 years of broad production engineering experience in the oil and gas industry with international postings in eight countries and four continents. Khalid Al-Omaireen is the General Supervisor for Safaniya Production with diverse and deep involvements in plant operation, plant maintenance, well services and field services. In 1986, he received his B.S. degree in Petroleum Engineering from the University of Southwestern Louisiana, LA. During his career with Saudi Aramco, he worked as a division head for different plant complexes that include gas/oil separation, gas compression, seawater distillation and oil stabilization facilities. In offshore fields, he has a long experience supporting rig operations and dealing with offshore barges/boats conducting different surveillance activities with a focus on improving asset safety and streamlining. Karam Sami Al-Yateem graduated with a B.S. degree in Petroleum Engineering with honors from King Fahd 58 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 University of Petroleum and Minerals (KFUPM), Saudi Arabia in 2005. Karam started as a Production Engineer in NAPED covering the Safaniya field. Since then he has gone on several field assignments to various locations onshore and offshore in the Tanajib area. Currently, Karam works as a Reservoir Engineer in the Safaniya field for the Northern Area Reservoir Management Department as a part of the company’s Professional Development Program. Author and co-author of several technical papers, Karam has also worked with the Computational Modeling Technology Team as a summer student in 2004. ABSTRACT Several innovative techniques and practices have been recently implemented to improve well production performance in offshore assets in the Arabian Gulf. The challenges which followed past practices were identified and intensive work was focused on enhancements to existing well completions to increase well productivity and prevent premature water or gas encroachment. This article describes several innovative concepts implemented in three major offshore fields in Saudi Aramco. The methodologies of four technologies which were tested and implemented in the recent years are presented. These technologies are the practice of sidetracking horizontal wells and completed with passive inflow screens, the use of reservoir gas cap for artificial lift of oil wells, the Tornado technique for sand fill clean out and the chemical treatment of wells which endured formation damage. All these technologies proved to be successful and their combined application added value to Saudi Aramco’s operations. As a result, the production targets for 2006 were met and the positive results obtained from the implementation of these technologies will lead to the optimization and improvement of future operational practices. BACKGROUND Saudi Aramco operates three major offshore fields in the North part of the Arabian Gulf. Horizontal drilling in these three fields dates back more than a decade. The company has been prudent in evaluating the technology of drilling and completing horizontal wells as it has progressed with time; and constantly improving the designs of horizontal completions to maximize reservoir recovery. As the number of horizontal wells increase in the fields, the reservoir sweep efficiency is improved with time and higher production rates were accomplished on a per well basis when compared Fig. 1. Typical sandstone reservoir log section. Fig. 2. Example of advancement of the OWC. to vertical producers. The geology in one of the fields is rather complicated with the existence of stringer sand bodies which are usually separated from the main sand by an impermeable shale break, Fig. 1. The stringer sands were deposited uncontrollably in the subsurface and pose enormous challenges in the well placement and deciding on the direction of the wells when it comes to horizontal drilling. The three major offshore fields were discovered in the mid-fifties and have been on production since. Their SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 59 (OWC) moves upwards slowly with time due to the strong aquifer drive in a piston-like movement until producing zones are swept, Fig. 2. In some areas, the advancement of the formation water towards the vicinity of the downhole perforations has as a consequence the increase in water production. The increasing water cut in the well affects adversely the production of oil since the well has no longer sufficient energy to produce naturally and it starts to produce in an intermittent status. Horizontal sidetracking is a solution to deal with problematic wells in terms of their productivity, following a rigorous and thorough evaluation to select the most promising candidate wells that would yield the most optimum results. By sidetracking intermittent wells utilizing a workover rig in all three offshore fields, the average production gain from the sidetracked wells in 2006 was 3 thousand barrels of oil per day (MBOPD) per well. U S E O F PA S S I V E I N F L O W S C R E E N S I N H O R I Z O N TA L W E L L C O M P L E T I O N S Fig. 3. Nonuniform inflow profile in a horizontal well. petrophysical properties are characterized by clean coarse sands with very good permeability in the range of 3-5 darcies (D). The recovery mechanism is by natural water drive and in some areas it is complemented by a gas cap drive. The sandstone reservoirs have pressure support by a strong water aquifer, which underlay the sand bodies. In general, the most common type of downhole water encroachment seen in Saudi Aramco’s offshore fields is bottom water movement. In this case, the oil water contact Fig. 4. Internal view of passive inflow screen device. 60 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 Saudi Aramco carried out internal appraisals of the performance of horizontal completions. The evaluation of production logging campaigns using Production Logging Tools (PLT) indicated that the implementation of horizontal wells in the offshore fields demonstrated an excellent sweep performance of the reservoirs. The studies also identified that in some horizontal producers, the flow was predominantly coming from only certain perforations in the horizontal section or even from a part of single perforated intervals due to permeability variations or formation damage during perforation operations. Figure 3 shows a flow profile of the preferential entry of oil from perforated intervals in the horizontal section of such a well. This nonuniform profile often results to premature water breakthrough or gas Fig. 5. Open hole mechanical packer shown in “Run in hole” position above and “Set” position below. Fig. 6. Production performance from first candidate horizontal well equipped with passive inflow screens. Fig. 8. Inflow profile comparison between horizontal wells with and without passive inflow screens. Fig. 7. Even distribution of inflow from first candidate horizontal well equipped with passive inflow screens. coning, which directly influences the productivity of the well and typically leads to its production decline. Evaluation of new technologies led to the evolution of the horizontal completion design with targets to achieve a uniform inflow profile in the horizontal section which will enhance well productivity and reservoir sweep. Saudi Aramco introduced the open hole completion combined with a stand alone premium screen with passive inflow screens, or otherwise called inflow control devices (ICD). The implementation of the passive inflow screen technology in the horizontal section was to prolong well life by avoiding an uneven flow as seen from the previous example, thus delaying gas or water breakthrough in horizontal wells. An additional advantage of the open hole completion was the overall cost reduction of well drilling mainly due to rig time savings. The passive inflow screen system is supposed to “equalize” the flow and even out the reservoir contribution along the horizontal section of a well. The passive inflow screens divert production from toe to heel through a spiral channel in the horizontal section, Fig. 4. The horizontal section can be divided in individual compartments with the use of mechanical open hole packers, which could seal washouts up to 2.5” higher than the run-in outer diameter of pipe (OD) of the completion string, Fig. 5. The combined use of mechanical open hole packers with passive inflow screens prevents the initiation of an acute channel of gas from the gas cap above or water from the water aquifer below the oil rim. The first pilot installation of the passive inflow system was in the main sand (Khafji formation) in one of the three offshore fields in December 2002. The performance of this well equipped with passive inflow screens is shown in Fig. SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 61 Fig. 10. Completion design schematic for natural gas cap lift. Fig. 9. Flow profile and performance plot of salvaged intermittent well. 6, where the well was put on production in February 2003 with an initial oil rate of 8 MBOPD and it sustained the production rate with zero water cut until today. After the installation of the passive inflow screens, a PLT was run which confirmed the even distribution of inflow in the horizontal wellbore, Fig. 7. The superiority of the completion design equipped with passive inflow screens is evident when this well is compared to two offset wells, also horizontal producers completed prior to 2002 and without passive inflow screens, with production rates of less than 5 MBOPD as opposed to 8 MBOPD of the first candidate well with passive inflow screens, Fig. 8. Several installations of passive inflow screens followed the initial pilot run since 2002. As of the end of 2006, there were 87 passive inflow screen completions in the three offshore fields. During the 4 years since the first implementation of the passive inflow screens, the horizontal wells equipped with this completion design when put on production, demonstrated an increase between 2-4 MBOPD compared with nearby horizontal wells which already had signs of increased water cut or gas oil ratio (GOR). A distinct advantage of the passive inflow screen system in the offshore fields of Saudi Aramco is the salvaging of intermittent flow wells due to increased water production. Figure 9 shows an example of a conventional vertical producer which flowed at 1 MBOPD and had reduced production after water breakthrough. The well was sidetracked with 50 ft of oil column remaining under the gas cap and underlain by water. The well was completed with passive inflow screens in the horizontal section and after it was put online, it had a stable production of more than 3 MBOPD and with only 5% water cut (WC) as seen in Fig. 9. 62 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 N AT U R A L G A S C A P A RT I F I C I A L L I F T Another innovation which was implemented in the major offshore fields is the successful integration of natural gas cap lift with the passive inflow screens. This innovation is again part of the continued evolution of the horizontal completions to enhance sweep efficiency or target reservoir locations partially swept by aquifer water. Coupling the two technologies together, allowed supplemental energy provided by the lifting source, in this case the reservoir gas cap, to be distributed equally in the wellbore through the passive inflow screens since the best zones along the horizontal section will not dominate the inflow in the wellbore. In one of the three fields, the hydrostatic pressure of the produced fluids with even relatively a low WC range of below 30% exceeds the production energy of the reservoir and reduces the well flow. Since there is a gas cap above the oil zone, a natural gas lift system was used as the energy source for lifting the oil. The method allows continued production from the well after the well had stopped or reduced production, due to water breakthrough. After review for the best candidate well, the new completion design was implemented utilizing the combined concepts, which are the use of passive inflow screens installed in the oil zone in the reservoir and natural gas lift entry from the gas cap above. The well is selectively perforated at the gas cap and allows the gas to flow in the annular space. The gas is then introduced into the wellbore through an orifice to assist lifting the column of fluid from the oil zone. Three choke settings of the orifice downhole can be controlled via slick line to optimize drawdown and production rates from the well. This completion design can be seen in Fig. 10. The success of this completion design in the pilot well paved the way for workovers in other wells of the field where they Fig. 11. Intervention jobs breakdown by production gain utilizing a barge vessel. would benefit from the existing natural gas cap allowing higher sustainable production and longer well life. SAND FILL CLEAN OUT USING TORNADO TECHNIQUE The Tornado technique utilizes Coiled Tubing (CT) and a special jetting nozzle tool for the purpose of sand fill clean out. While the CT with the jetting tool at the end cleans the wellbore in the first direct run from debris and sand which has blocked healthy perforations (penetration stage), the tool has the ability to invert circulation from its nozzles to the opposite direction and while pulling out of the hole with the CT there is a second clean out run which removes sand that has been re-deposited after the first run (clean out stage). This technique ensures that unwanted sand which was not circulated properly and cleaned from the wellbore during the first run, is now effectively removed especially from sections of slanted or highly deviated sections of wells where the gravity is assisting the decantation of sand after the penetration stage. A total of 13 wells were cleaned out in 2006 using this technique to facilitate logging operations and/or for production increase by cleaning blocked perforations. The implementation of the Tornado technique resulted in cost savings of $20,000 per job primarily by eliminating the chemicals required during previously adopted clean out operations. The production gain by cleaning perforations in four wells using the Tornado method in 2006 amounted to 2.75 MBOPD per well. The sand fill clean out on the remaining nine wells was to facilitate running a PulseNeutron Log (PNL) and it did not attribute to any production gain. F O R M AT I O N D A M A G E C H E M I C A L T R E AT M E N T Oil wells in the three major offshore fields are subjected to formation damage during drilling or workover operations due to calcium carbonate and clay minerals that invade the pay zone upon well completion. A chemical treatment process called “Iron Check Pellet” (ICP) was developed and perfected in Saudi Aramco Research & Development Center prior to its applicability to the field. It was initially pilot tested in 2005 for use in wells that had suffered formation damage and did not flow, or flowed with rates below expectations. The aim of the ICP chemical treatment was to restore well potential and directly remove formation damage caused by drilling fluids while drilling, or by the use of limestone chips through killing the well during workover operations. During 2006 and because of the positive results obtained from the pilot test in 2005, the ICP treatment technique had a wider use in the offshore fields and 14 ICP chemical treatment jobs were performed. The average production gain per well from chemical treatment amounted to 3.2 MBOPD. As seen in Fig. 11, the ICP chemical treatment proved to be the most advantageous when it comes to production gain among intervention jobs to restore well productivity by utilizing a barge vessel, as it contributed 44% to the overall production gain among rigless intervention jobs in 2006. CONCLUSIONS 1. Iron Check Pellet chemical treatment was the technique that provided the highest production gain among all intervention job types by utilizing a barge vessel (rigless interventions) instead of a workover rig. 2. The availability of proper log data is paramount for the design of the passive inflow screen system with the correct horizontal length of compartments and number of screens per compartment. The decision making of the proper placement of the passive inflow screens is facilitated with the acquisition of formation data utilizing logging while drilling (LWD) formation evaluation technology. 3. The success realized from the implementation of passive inflow screens in the three offshore fields will trigger a new generation of completion systems in Saudi Aramco. These systems will involve running ICDs, with mechanical open hole packers, combined with downhole monitoring systems, in multilateral level 4 completions. This completion type will be able to exploit more than one zone (multiple stringer sands), and provide real-time downhole pressure and temperature monitoring for individual laterals. 4. During 2006, a total of 17 workovers utilizing rigs and 62 intervention jobs utilizing barge vessels (rigless) were conducted in Saudi Aramco’s three major offshore fields, which provided substantial production gains to sustain overall field productivity and meet the annual targets. SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 63 T H E WAY F O RWA R D The innovative technologies which are presented in this article have been trial tested and evaluated in the recent years in Saudi Aramco’s offshore fields and proved to be very effective in improving sustainable well productivity. Several of these applications will be perfected for future use and others have been identified and will be evaluated for use in the three major offshore fields. The next generation of completion design with open hole packers in conjunction with the passive inflow screens will utilize swellable packers. These packers are made of a solid rubber element which is capable to expand up to 200% of its original OD when it comes in contact with reservoir crude. Current completion designs utilize compartment sizes of 800 ft to 1,000 ft based on open hole log interpretation, whereas the use of swellable packers could allow individual compartments every 100 ft in the open hole section. The increase of the number of compartments created by the swellable packers along the horizontal section will improve the system efficiency because the impact on production flow rates if one or more of the compartments will experience severe water or gas breakthrough will be minimized. ACKNOWLEDGEMENTS The authors acknowledge the support of Saudi Aramco management for their permission to publish the information contained in this paper. Our sincere thanks go to AbdulHameed Aborshaid for his insights and input. Additionally, the achievements mentioned herein are a collective effort of several individuals and groups and could not have materialized without the insight of people who have a passion for the advancement of technology. Their direct or indirect contribution to this work is highly appreciated. N O M E N C L AT U R E CT D ft GOR ICD ICP OD PLT WC Coil Tubing Darcy (unit for permeability) Feet Gas Oil Ratio Inflow Control Device Iron Check Pellet Outer Diameter of Pipe Production Logging Tool Water Cut 64 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 Crosswell Electromagnetic Tomography in Haradh Field: Modeling to Measurements Dr. Alberto F. Marsala Dr. Saleh Al-Ruwaili Dr. Shouxiang Mark Ma Modiu Sanni Zaki Al-Ali Jean-Marc Donadille Dr. Michael Wilt Dr. Alberto F. Marsala has more than 17 years of oil industry experience and is currently working in Saudi Aramco’s EXPEC Advanced Research Center (EXPEC ARC). Previously in Eni and Agip, he covered several upstream disciplines, including 4D seismic, reservoir characterization, petrophysics, geomechanics, drilling, and construction in environmentally sensitive areas. Dr. Marsala worked in the Technology Planning and R&D committee of Eni E&P. He was the head of Performance Improvement of the KCO Joint Venture (Shell, ExxonMobil, Total, and others) for the development of giant fields in the northern Caspian Sea. Dr. Marsala, who has authored several technical papers and international patents, holds a Ph.D. in Nuclear Physics from the University of Milan, Italy, an MBA in Quality Management from the University of Pisa, Italy, and a specialization in Innovation Management. He served for several years on the Board of Directors of SPE Italian Section and is currently a Quality System Manager of the European Organization for Quality. Dr. Saleh Al-Ruwaili is a Petroleum Engineer specializing in petrophysics and formation evaluation. He received his B.S. degree in 1989 and a M.S. degree in 1992, both from King Fahd University of Petroleum and Minerals (KFUPM), Saudi Arabia. In 1995, Dr. Ruwaili received his Ph.D. in Computational and Applied Mathematics from Rice University, Houston, TX. During his 15 years with Saudi Aramco, he has worked in a number of upstream areas like reservoir engineering and simulation, reservoir description, reservoir characterization, reserves assessment and reservoir engineering technology. Dr. Ruwaili has filed one patent and authored numerous geoscience and engineering papers, which were published in international journals of AAPG, SPWLA and SPE. Currently, he is the technology champion of the Deep Diagnostics Focus Area for the Reservoir Engineering Technology Team in the EXPEC Advanced Research Center (EXPEC ARC). Dr. Shouxiang Mark Ma is a Petroleum Engineering Specialist and a Technologist Development Program mentor at the Petroleum Engineering organization, Saudi Aramco. Mark received a Ph.D. degree in Petroleum Engineering and has published more than 30 papers in log/core petrophysics. Before joining Saudi Aramco in 2000, he worked 20 years in the industry and academia including PRRC/New Mexico Tech, WRI/University of Wyoming, and Exxon Production Research Company. Mark is a member of SPE and SCA. Modiu Sanni is a Petroleum Engineering Specialist with the Reservoir Engineering Technology Team (RETT) of the EXPEC Advanced Research Center (EXPEC ARC). Prior to joining Saudi Aramco in 2004, Modiu worked for Shell for approximately 15 years in Nigeria, The Netherlands and Sultanate of Oman. He has experience in formation evaluation, reservoir characterization and description, integrated multidisciplinary field studies, field development and enhanced oil recovery. Modiu has authored and coauthored papers published in SPE and SPWLA conference proceedings. He received his B.Sc. in 1987 and a M.Sc. in 1990, both in Mechanical Engineering from the University of Ibadan, Nigeria. Zaki Al-Ali holds a M.S. degree in Petroleum Engineering from King Fahd University of Petroleum and Minerals (KFUPM), Saudi Arabia. He was a Senior Petroleum Engineer with the Reservoir Simulation Division before joining ‘Udhailiyah Reservoir Management Division. Zaki worked for the Ministry of Petroleum and Minerals for 4 years prior to joining Saudi Aramco in 1987. Jean-Marc Donadille has been working for 6 years for Schlumberger in the Paris and Beijing offices. He is currently a Senior Research Engineer in the Schlumberger Dhahran Carbonate Research Center in Saudi Arabia. JeanMarc received a joint M.S. degree in 2000 from ENSIMAG (French Top National School of Computer Science and Applied Mathematics, Grenoble) and the University of Waterloo, Ontario, Canada. His interests include modeling and inversion, electromagnetics, geophysics and petrophysics. Dr. Michael Wilt received his B.S. in 1973 and M.S. in 1975 in Geophysics from the University of California, Riverside, CA. He received his Ph.D. from the University of California at Berkeley, CA in 1991. Dr. Wilt was employed as a staff scientist at Lawrence Berkeley Laboratory between 1977 and 1984 and he was a program 66 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 leader at Lawrence Livermore National Laboratory between 1989 and 1997. In these roles he applied electrical, electromagnetic (EM) and potential field methods for oil and geothermal field characterization and steam flood monitoring. In 1997 Dr. Wilt joined Electromagnetic Instruments Inc. (EMI) where he led research and development projects in crosshole EM and extended induction logging. EMI joined Schlumberger in 2001 and he led the development effort in deep reading EM technologies, which continues today. He is currently the Schlumberger Business Development Manager for deep reading EM technologies in the Middle East and Asia and he is stationed at the Schlumberger Regional Technology center in Abu Dhabi. ABSTRACT Crosswell electromagnetic (EM) resistivity is emerging as an intriguing technology for reservoir surveillance. It provides a cross-sectional resistivity image between two wells and has the potential to provide fluid distribution at an interwell scale. It can be used for identifying bypassed hydrocarbons, monitoring macroscopic sweep efficiency, planning infill drilling, and improving effectiveness of reservoir simulation. It can be deployed for one-time or time-lapse surveys. A crosswell EM technology trial project is being conducted in an Upper Jurassic carbonate reservoir, at the Ghawar field in Saudi Arabia, to monitor the movement of injected water flood front and map the fluid distribution. The project site is in Ghawar’s southern region, Haradh field, and consists of three wells in the oil-water contact zone where peripheral injection water may have produced an uneven flood front distribution. Significant drilling and well deepening were required prior to the deployment of tools in the three-well triangle. In fact, one new well was drilled and two other wells were deepened by more than 200 m, so that good volumetric coverage could be obtained at the oil-water contact zone. Extensive logs, core and formation tests were also acquired to provide deterministic saturation profiles at the near wellbore region. Formation evaluation in the project area indicates that one of the wells was fully swept while a second well, some 400 m away, was not. In July 2007, crosswell EM surveys were acquired across the three Haradh wells. In spite of the large well separations, the acquired EM data had good quality, and good stations repeatability. Preliminary processing has revealed a structure consistent with the background structure but a clear image of the oil-water contact is yet to be made. INTRODUCTION The Haradh field is in the southernmost part of the greater Ghawar field – the largest single oil field in the world, Fig. 1. Arab-D is a 100 m thick, highly prolific, upper Jurassic reservoir comprising a carbonate sequence of grainstones, packstones and wackestones1. The original sedimentary textures have been altered in many places by leaching, recrystallization, cementation, dolomitization and fracturing, which have caused a variety of pore types2 to coexist in Arab-D. Flood-front movement can be uneven in some parts of the reservoir. Reservoir porosity ranges from less than 10% at the base to over 30% at the top while permeability ranges from a few millidarcies to more than one Darcy. The Arab-D reservoir in Ghawar has historically been operated at relatively low depletion rates. Flank water injection is being carried out to maintain pressure and to improve sweep efficiency in this reservoir. With current inter-well spacing, about 1 km, determining fluid distribution behind the flood front is a key challenge to maximizing recovery from this reservoir. Traditional reservoir fluid monitoring techniques, e.g., pulsed-neutron logs (PNL) and resistivity logs have investigation depths ranging from a few inches, for PNL logs, to about 3 m for the deepest resistivity logs3. Therefore, they cannot be used effectively for flood-front monitoring at the inter-well scale. Of the deeper technologies investigated, the crosswell EM method seems to have potential value for reservoir surveillance applications. It has been used in other fields for reservoir characterization4 and for mapping oil recovery in thermal enhanced oil recovery (EOR) applications. It has also been used in time-lapse mode as an indirect means of waterflood monitoring5. We note, however, that these surveys were acquired at a modest inter-well spacing, < 300 m, which Fig. 1. Arabian Peninsula and Ghawar field. The area of interest lies in the southwestern flank of Ghawar, within Haradh. is not available at the Ghawar field. Previous trials of 4D seismics at Ghawar have produced inconclusive results, indicating that the method is not viable for reservoir surveillance in the Ghawar field. These results were likely due to the high rigidity of the limestone-dolomite reservoir rock matrix and the small acoustic impedance contrast between the pore fluids6 in Ghawar field. CROSSWELL EM PROJECT A joint research project between Saudi Aramco and Schlumberger was initiated to investigate the applicability of crosswell EM resistivity technology for studying the Arab-D formation at Ghawar. Haradh field was selected because it is deemed to be partially invaded by injection water from nearby injectors. The objective was to evaluate fluid distribution between wells using crosswell EM resistivity tomography in combination with a sophisticated suite of Fig. 2a. Surface location of the project. Fig. 2b. Relative locations of the three wells for the X-well EM. SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 67 Fig. 3a. Resistivity model for a case having water flood, extending up to onefourth of the two-well separation (500 m). phase it was assumed that a new well, A, could be drilled and the open hole sections of existing wells B and C could be used for measurements. Several scenarios of flood-front movement such as edge water due to super-K or fracture swarms, bottom water encroachment, coning, and cusping were modeled (see Figs. 3a and 3b)7. The modeling showed that in almost all cases the crosswell system would provide adequate signal but the lateral resolution of images is degraded if the aspect ratio (vertical logging interval relative to inter-well distance) is too low. Experimentation with a range of aspect ratios was conducted and it was found that an aspect ratio of 0.25 or more is required to achieve reasonable results. In addition, it was found that measurements need to be made above and below the reservoir to accomplish plausible results. To satisfy these requirements, well A was drilled to 200 m below the reservoir. Additionally, wells B and C were deepened by approximately 200 m. Consequently, the open hole intervals for crosswell logging in the three wells enabled having aspect ratios ranging from 0.3 to 0.65. In addition, a segment of nonmagnetic (chrome) casing was used in well A to extend measurements into the section above the reservoir. Compared to conventional casings, Fig. 3b. Inversion of synthetic crosswell EM data for the water flood case shown in Fig. 3a. wireline logs and formation evaluation tools. These technologies combined have the potential to monitor macroscopic sweep efficiency, identify current fluid contacts, and locate bypassed oil, thus enabling effective infill-well placement. PREACQUISITION MODELING Prior to field acquisition, an extensive search was made to locate suitable wells at the oil-water contact, Fig. 2a. Once the site was selected then pre-job forward modeling was carried out6 to investigate the feasibility of obtaining useful results from the measurements, with special considerations to the large well separation and existing completions in wells B and C to be surveyed, Fig. 2b. During the modeling 68 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 Fig. 4. Interpretation of historical well logs in well B. Fig. 5. Interpretation of historical well logs in well C. chrome pipe has little effect on EM data. Such nonmagnetic casing would allow EM measurements to be extended across a cased section of well A. Otherwise, EM data needs to be obtained in the open hole with possible risk to well integrity. These new drilling and completion activities were accompanied by coring in well A and logging in the three wells. Comparing newly acquired logs to the older open hole suite of logs, it is possible to obtain near-well formation evaluation in time-lapse mode; see next section. F O R M AT I O N E VA L U AT I O N Well B was drilled vertically in 1994; see a composite of recent and older logs in Fig. 4. Track 1 shows the original formation resistivity and track 4 the interpreted volumetric oil and water. A productivity index (PI) test performed in 1996 indicated that the near-wellbore formation was slightly damaged with a skin of 3. The first production log (PL) run in 1996 showed that well B was producing dry oil uniformly from the 100 m reservoir. Water broke through in 2001. From a PL run in 2003 (track 5), the main oil and water producing intervals were around 660 ft. Until recently well B was in production. Prior to deepening well B, a carbon-oxygen (C-O) log was run, using reservoir saturation tool (RST™), to evaluate oil and water distribution near the wellbore8. After the tubing was removed we ran conventional open hole logs of triple combo; the resistivity logs are plotted in track 2. Comparing the 1994 and 2007 resistivity logs indicate that the invading water has almost reached the top of the reservoir, track 3. This is consistent with the C-O log results, track 6. The 2007 resistivity log was interpreted using the Archie equation with formation water salinity of 120 ppk total dissolved salts (TDS); see results in track 6 of Fig. 4. The 2007 results of C-O (shaded blue) and resistivity (yellow curve) are in good agreement, which is important since the well data will be used to anchor the crosswell EM results. A formation tester (FT) job was run and a reservoir fluid sample was taken at a depth of 652 ft, (track 6). After pumping out for more than nine hours, this sample had an 85% water cut, indicating that water had reached the top of the reservoir. Well C was drilled vertically in 1996; the logs are shown in Fig. 5. Track 1 shows the original formation resistivity and track 6 the interpreted volumetric oil and water. A PI test performed in 1996 indicated that near wellbore formation was slightly damaged with a skin of 3. Another PI tested in 1999 indicated more severe formation damage, with a skin of 9. According to the 1996 PL, the well was producing dry oil and the reservoir contribution to production was roughly uniform. Water broke through in June 1999. From a PL run in May 2001 (track 7), the main oil producing interval was about 670 ft and water breakthrough interval was near 672 ft. Well C was also deepened for the crosswell EM work. We used this opportunity to acquire a C-O (RST™), slimhole array induction tool (SAIT™), and conventional triple combo. The regular array induction tool (AIT™) resistivity logs are plotted in track 3. The comparison, in track 4, between the 1996 original resistivity, track 1, and the 2007 rigless SAIT, track 2, and rig AIT resistivities indicates that the invading water had reached a depth of 685 ft. The following observations can be drawn from Fig. 5: 1. Different logging runs may not be on depth. In average, a 3½ ft depth shift was required to put the newly acquired logs on depth with the original open hole logs, track 4. 2. The workover fluid may have deep water invasion that reduces the AIT™ readings. Depth of invasion SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 69 volumetrics are plotted in tracks 4 and 5, respectively. Using image log calipers, a 2D borehole shape is constructed in track 1. From Fig. 6, the following observations can be drawn: 1. The borehole washout (track 1) across the anhydrite interval, just below casing, is very typical of anhydrite-water interaction. This enlargement affects log data quality, especially shallow-depth logs. 2. Track 3 shows water-based mud invasion profile. For formation evaluation, deep reading logs should be used. 3. The open hole logs interpretation, using a formation water salinity of 90 ppk TDS, indicates that the water front has advanced to about 736 ft (track 5); this is consistent with FT pressure data and sampling results. 4. Similar to well C, some dry oil was sampled in well A across the thin oil zone at 844 ft. 5. Comparing reservoir porosity, track 5, and NMR pore-body size distribution, track 6, higher porosity rocks (above 760 ft) can have bigger pores. 6. From the static image, track 8, it is obvious that there Fig. 6. Well logging interpretations for well A. depends on rock properties and workover operation practices. 3. After depth shifting, time-lapse porosity logs (track 5) showed little change from 1996 to 2007. 4. Track 8 shows the C-O results (shaded blue) and the SAIT™ data (yellow curve) interpreted using Saudi Aramco best practices of interpreting SAIT™ logs9 and using water salinity of 60 ppk TDS. The C-O and SAIT™ logs (track 8) are in good agreement. 5. An FT job sampled reservoir fluids. After more than seven hours of pump-out, the sample at depth 645 ft contained about 95% oil (5% water cut). Then, after more than 10 hours of pump-out, for the sample at depth 692 ft, it showed a water cut of 80%. To our surprise, some dry oil was sampled across the thin zone at 821 ft. Well A was drilled specifically for this crosswell EM project and this opportunity was utilized to collect cores across the reservoir. A complete set of logs was also run in this well, see Fig. 6. Triple combo logs are shown in tracks 1-3, an NMR log in track 6, image logs in tracks 7-8, and FT in track 5. Logging interpretations for lithology and 70 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 Fig. 7. Water volume as fraction of total space on the B-C-A wells section. Scenario obtained from open hole logs. is a low porosity, or high resistivity, streak at 730 ft that may have helped to slow down water advancement. FLUID DISTRIBUTION SCENARIO From the recent formation evaluations discussed, we found that the near-wellbore conditions in wells A, B and C are quite variable in spite of their close proximity. In particular, variations in the fluid level, in the saturation of the various zones, and in the salinity of the formation water were observed. Near-wellbore water saturation was estimated from recently acquired porosity and resistivity logs using the Archie equation with water resistivity (Rw) of 0.035 ohmm. In the following modeling scenarios, the water volume is considered a fraction of the total space, which equals water saturation multiplied by porosity: This quantity is represented for the three wells, in Fig. 7, by blue color crossing the porosities in the displayed horizons between wells. Well B has been producing for a number of years; consequently it shows a large volume of water in the high porosity section at the upper half of the reservoir. Well C has also produced for several years; it shows intermediate water content at the bottom of the highporosity section and low content at the top. In well A, the water content is low everywhere except at the bottom of the high-porosity, where it has water in a 3 m zone. Nonetheless, it is not obvious whether the water in this wet zone is caused by production in nearby wells or by peripheral water injection. In absence of any other inter-well information, the most plausible way to create scenarios of water distribution between wells is to interpolate the values at the wells. The image of Fig. 7 was obtained by interpolating the water volume fraction computed from eight wells in the area. Each cell value is an average of the water volume fraction at nearby wells weighted by the inverse of the distance from the cell to the nearby well data point. The method accounts for structural information and reservoir zonation; in addition it favors horizontal continuity. Considering the proximity of these wells, this image is showing surprising variations. Because it is based on interpolation, rather than measurements, its results are questionable. For example, it is not clear whether the continuous path of water leading to Z1-A originates from Z1-B, Z2-B, or both. Likewise, the extent of the water present between Z3-B (mainly wet) and Z3-A (dry) is not well defined. Similar questions about the distribution of the Fig. 8. Crosswell EM tomography. water between well A and well C may not be answered with certainty. It is expected that the resistivity images, obtainable from crosswell EM surveys, will better define the inter-well fluids distribution. CROSSWELL EM TECHNOLOGY Crosswell EM uses the principles of electromagnetic induction and tomography to provide an image of the resistivity distribution between boreholes. Figure 8 illustrates a field application of crosswell EM. Two boreholes are spaced a distance (x) apart and have a depth range (z), over which inter-well measurements can be made. The transmitter (T), placed in the first well, broadcasts EM signals throughout the medium. At the second well, the signals are detected using an array of induction coil (magnetic field) receivers (R). Whenever possible, the sources and receivers are placed at regularly spaced intervals below, within, and above the depth range of interest. The data collected are used to image the interwell space. In practice, the adjacent source and receiver stations are spaced 2% - 5% of the inter-well distance (x). The ideal measurement range in depth (z) is at least equal, if not greater, to the well separation such that the aperture (z/x in Fig. 8.) of the tomographic imaging experiment is equal to or greater than unity. There have been, however, successful SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 71 fit within a specified tolerance for acceptance. The computational engine that drives the sensitivity and inversion algorithms is a numerical method that calculates the electromagnetic fields within a 2D (or 3D) rectangular grid. A number of these solutions have been developed over the past 20 years and these will not be described here. Presently, finite difference algorithm10 is used. It is well known that the inversion process results in non-unique models for resistivity maps in the inter-well space investigated. In practice, this condition is usually managed by applying the previously known data, e.g., logs, formation tests, well performance history, and exercising reasonable model constraints for fitting the data. C R O S S W E L L E M S U RV E Y I N H A R A D H Fig. 9. Sample crosswell EM raw data; profile and repeat. imaging examples where the aperture was much less than unity; in such cases the problem is usually fairly constrained. The data set normally constitutes several thousand measurements, which are interpreted together to provide the inter-well resistivity map. Field data is collected using standard wireline logging conveyance with the source and receiver systems connected by hardwire. The transmitter tools have an electronics cartridge and a fairly large antenna, typically 8 cm - 10 cm in diameter and 4 m - 5 m long. This size is required to generate a sufficient moment to transmit the signal across large distances. The receivers can be slimmer but are often multilevel coil strings; thus they can be quite long. The acquisition strategy involves fixing the receiver(s) at a certain depth in one well and acquiring data while the transmitter sonde is moving continuously in a second well. After a specified depth interval is logged, the receiver is moved to a new depth and the process is repeated until the logging interval is covered by both source and receiver. A data point usually consists of stacking a monochromatic sine-wave hundreds or thousands of times. An entire data set consists of 30-60 separate receiver positions covering the depth range of interest; therefore using a string of receivers is essential to manage the data acquisition time. An entire data set typically requires from 12 to 36 hours depending on the tools used, well conditions, and well separation. Field data are interpreted by fitting the measurements to calculated data from a numerical model, using an inversion procedure. We begin with a resistivity model, usually derived from prior knowledge of the field area including logs, geologic and seismic data. Using this model and a forward EM code, the inversion calculates the forward EM response and then adjusts the model parameters, under certain constraints, until the observed and calculated data 72 SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 Key challenges facing crosswell EM data acquisition at Haradh are the large well spacing and the variable resistivity sections. Although, in theory, EM tomography is useful at well separations of 1 km or more, this is so far the largest well separation tried by crosswell EM. Crosswell EM work in Haradh field was conducted in July 2007. The three well pair required about seven days for rig-up and data collection. A sample field profile, Fig. 9, reveals that although the signals were low (as expected), the data are repeatable. In addition, the background noise level was found to be very low, which bodes well for future surveys. Each of the three surveys consisted of 3,000-4,000 measurements which will be processed jointly to provide the 2D inter-well resistivity maps. In addition to the tomography data, we also collected background noise data to evaluate the influence of steel and chrome casing on the ambient noise. The next step in the process is to complete the data inversions and compare the inter-well resistivity maps to the initial well derived resistivity realizations. CONCLUSIONS This initial crosswell EM survey in Saudi Arabia has produced interesting and useful results. The technique has demonstrated adequate range and sensitivity for reservoir monitoring and likely has a bright future in the Kingdom. We look at this project as an early test of deep diagnostic technology. The newly acquired crosswell EM surveys and their interpretations will help in anchoring on effective reservoir surveillance strategies, which will enhance the production plans leading to improved recovery. N O M E N C L AT U R E EM PNL PL PI C-O RST™ SAIT™ AIT™ TDS FT 2D, 3D, 4D m n Rw Rt Vwater,frac φ Electromagnetic Pulsed neutron logs Production log Productivity index Carbon-oxygen Reservoir Saturation Tool Slimhole Array Induction Tool Array Induction Tool Total dissolved salts Formation tester 2-, 3-, 4-dimensional; 4D is a 3D repeated at different time (time lapsed) Archie cementation exponent Archie saturation exponent Water resistivity – ohm-m Formation (true) resistivity – ohm-m Water volume, fraction of total space – m3/m3 Porosity - m3/m3 ACKNOWLEDGEMENTS The authors are thankful to Saudi Aramco and Schlumberger for their permission to publish this paper. Special gratitude extended to S. Neaim, N. Afaleg, O. Ukaegbu, M. Badri and B. Miller for their constant support to this work. Similar thanks are extended to S. Ghamdi for the geological description, to R. Akkurt, A. Ibrahim, I. Ariwodo, M. Zeybek and S. Crary for logging data acquisition and interpretation, to C. Levesque for the crosswell EM modeling, to S. Hussain for the Petrel modeling, and to M. Buali for the wells operations. REFERENCES 1. Cantrell, D.L., Swart, P.K., Handford, R.C., Hendall, C.G. and Westphal, H., “Geology and Production Significance of Dolomite, Arab-D Reservoir Ghawar Field, Saudi Arabia,” GeoArabia, Vol. 6, No. 1, 2001, pp. 45-59. 4. Wilt, M.J., Morrison H., Becker A. and Lee, K.: “Cross Borehole Electromagnetic Induction for Reservoir Characterization,” SPE paper 23623, 1992. 5. Patzek, T., Wilt, M.J. and Hoversten, G.M.: “Using Electromagnetics (EM) for Reservoir Characterization and Waterflood Monitoring,” SPE paper 59529, 2000. 6. Dasgupta, S.N.: “Monitoring Reservoir Fluids Alternatives to 4D Seismic,” 68th Meeting, EAGE, Expanded Abstracts, E027, 2006. 7. Sanni, M.L., Yeh, N., Afaleg, N.I., Kaabi, A.O., Ma, S.M., Levesque, C. and Donadille, J.M.: “Electromagnetic Resistivity Tomography: Pushing the Limits,” SPE paper 105353, 2007. 8. Kelder, O., Al-Hajari, A., Eyvazzadeh, R., Ma, S.M. and Al-Behair, A.M.: “Expanding the Operating Envelope of Carbon-Oxygen Saturation Monitoring Technology,” IPTC paper 10458, November 2005. 9. Al-Sunbul, A., Ma, S.M., Al-Hajari, A., Srivastava, A. and Ramamoorthy, R.: “Quantifying Remaining Oil by Use of Slimhole Resistivity Measurement in Mixed Salinity Environments – A Pilot Field Test,” SPE paper 97489, International IOR Conference in Asia Pacific, December 5-6, 2005, and Kuala-Lumpur, Malaysia. Saudi Aramco Journal of Technology, Winter 2005. 10. Abubakar, A., Habashy, T.M., Druskin, V.L., Alumbaugh, D., Zhang, P., Wilt, M.J., Denclara, H. and Nichols, E.: “A Fast and Rigorous 2.5D Inversion Algorithm for Crosswell Electromagnetic Data,” 75th annual International Meeting 2005, SEG, Expanded Abstracts, 534-537. S I M E T R I C C O N V E R S I O N FA C T O R S feet x 3.048* E-01 psi x 6.894757 E+00 bbl/d x 1.589873 E-01 inch x 2.54* E+01 m kPa m3/d mm * Conversion factor is exact 2. Clarke, E.A.: “Miles to Microns – Analysis of the Ghawar Arab-D Pore Systems,” Internal Saudi Aramco Report, 2006. 3. Ma, S.M., Al-Hajari, A.A., Berberian, G. and Rammamorthy, R.: “Casedhole Reservoir Saturation Monitoring in Mixed Salinity Environments; A New Integrated Approach,” SPE paper 92426, 2005. SAUDI ARAMCO JOURNAL OF TECHNOLOGY WINTER 2007 73 SUBSCRIPTION ORDER FORM To begin receiving The Saudi Aramco Journal of Technology at no charge, please complete this form. Please print clearly. 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