uh-1h main rotor blade fatigue
Transcription
uh-1h main rotor blade fatigue
UH-1H MAIN ROTOR BLADE FATIGUE by Patrick Conor, Alan James, Michael Hollis Defence Technology Agency New Zealand Defence Force Auckland PRESENTATION OUTLINE • BACKGROUND • BLADE CRACKING • GRIP PAD DISBONDING • BLADE INSPECTION • NDI RESULTS • CAUSAL FACTORS • IN-SERVICE MANAGEMENT UH-1H MAIN ROTOR BLADE (MRB) FATIGUE BACKGROUND • RNZAF AIRFRAME AVERAGE TSN APPROX 10,000 HRS • US ARMY HOLD TYPE CERTIFICATE • MAIN ROTOR BLADE SAFE LIFE 2,500 HRS (US ARMY SPECTRUM) • RNZAF MAINTENANCE iaw US ARMY MANUALS • RNZAF FREE OF SERIOUS MRB PROBLEMS SINCE 1965 "# " $ MEDIUM UTILITY HELICOPTER ROLE Location of flight operations in 2000 - 2001: • NEW ZEALAND • • EAST TIMOR • BOUGAINVILLE • ANTARCTICA ! DEFECT INDICATION – NZ3816, EAST TIMOR 2001 BLADE CONSTRUCTION ADHESIVELY BONDED METAL LAMINATE STRUCTURE D-spar Grip Plate (Aluminium) Toughened epoxy adhesive Grip Pad (Steel) Bushing % $ ' '( FRACTURE SURFACE Fatigue crack limits CHORDWISE C/S & GRIP PAD DISBONDING UNDER-SURFACE OF CRACKED BLADE SAW CUT GRIP PAD REMOVED AND BLADE CUT UP FOR FRACTURE SURFACE ANALYSIS FATIGUE CRACK TIP L.E. ) $ + RESULTS OF DESTRUCTIVE TESTS TWO MRB CLASSES Early-Model Blades - MODERATE DISBONDS AT 2,500 HRS Recent Blades - SIGNIFICANT DISBONDS AT 1,000 HRS - MANY BLADES IN SERVICE * DAMAGE ASSESSMENT GRIP PLATE CRACK GROWTH RATE WAS RAPID CRACKS CONCEALED BY GRIP PAD CRACKING PRECEDED BY GRIP PAD DISBONDING SAFETY PREDICATED BY DISBONDING SO, MANAGE SAFETY BY MONITORING DISBOND ONSET (SAFETY BY INSPECTION) PRESCRIBED INSPECTION – CAREFUL VISUAL CHECK , DISBONDING FOUND IN A BLADE REJECTED FOR OTHER REASONS AFTER 1100 HRS IN SERVICE - $ ' Grip Pad (Steel) - LARGE DEFECT WAS NOT DETECTED BY EITHER: • BONDLINE VISUAL INSPECTION (IN A LAB ENVIRONMENT) OR, • COIN TAP-TESTING Grip Plate (Aluminum) PERFORMANCE OF AVAILABLE INSPECTION METHODS FOR MEASURING GRIP PAD DISBONDING METHOD RESULT VISUAL - UNRELIABLE DYE PENETRANT - UNRELIABLE COIN TAP TEST - FAILED ULTRASONIC TEST - DIFFICULT TO INTERPRET EXISTING INSPECTION METHODS DID NOT PROVIDE ADEQUATE MEASUREMENT CAPABILITY NEW INSPECTION TECHNIQUE - BONDLINE COMPLIANCE - ' STRAIN GAUGE $ ' MECHANICAL DISPLACEMENT BONDLINE LOAD BONDLINE COMPLIANCE 700 500 400 RESULT WITH MULTIPLE STRAIN GAUGES 300 200 Microstrain 600 100 1 0 54.45 Bending Mom ent (metre.kg) 95.975 0 2 3 4 5 6 7 8 9 10 Strain Gauge Number ! $ ' BLADE GRIP PAD EDGE STRAIN vs TIME SINCE NEW 1600 Max. Strain (uS) 1400 1200 1000 800 600 400 200 0 0 500 1000 1500 TIME SINCE NEW (Flying Hours) 2000 2500 OPTIONS TO KEEP FLYING 1. BUY MANY NEW BLADES AND REPLACE VERY EARLY - VERY EXPENSIVE - IMPOSSIBLE SUPPLY PROBLEM 2. ADOPT SAFETY BY INSPECTION - DEFINE SAFE DISBOND SIZE - DETECT AND MONITOR SUB-CRITICAL DEFECTS - USING THE STRAIN NDI METHOD % - " $ 1400 DISBOND RUNAWAY LIMIT Max TE Strain (uS) 1200 1000 800 600 BLADE QUARANTINE LIMIT 400 200 0 0 20 40 60 80 100 120 140 Delaminated Area (cm 2) & CAUSAL FACTORS ) A-FS11396 A-FS11421 A-FS11423 A-FS12014 A-11392 A-FS11365 A-FS11068 A-FS11416 A-FS11413 A-7619 A-6715 A-FS11343 A-6712 A-FS11347 A-FS12062 A-FS11415 A-11376 A-FS11271 A-FS11243 A-FS11449 A-FS11385 A-FS11419 A-11928 A-FS12026 A-FS12061 A-FS12584 A-9144 A-FS11349 A-FS12008 A-FS12768 A-FS12767 A-FS12007 A-FS12708 A-FS12874 A-FS12060 A-11389 A-FS12769 A-FS12051 A-FS12869 AMR01288 A-FS12797 A-FS12890 A-FS12921 A-5031 A-FS12866 A-FS12770 A-FS12828 A-FS12923 Blade TSN (hours) # . / 0 11 /2 . $ 3 4 25 26 2 4 2500 2000 RNZAF DATA 1500 1000 800 1000 600 500 0 Blade Strain -> ' , 7.1 5 1600 1400 Ice Hrs 1200 Hrs NZ 400 Hot & Wet Hrs Strain 1 200 0 Analysis by S/Ldr M Going * MAIN ROTOR BLADE ATTACHMENT FITTING - LOAD TRANSFER Resultant Horizontal Shear Outboard Up MB P Aluminium Grip Plate ADHESIVE PEEL Steel Grip Pad Resultant Horizontal Shear Adhesive Bond Line FATIGUE? • HIGH PEEL STRESS IN THE ADHESIVE • DEMANDING LOADS SPECTRUM? FEA: ADHESIVE STRAIN IN Z-AXIS Analysis by S K Campbell (DTA) # , ' SAFETY BY INSPECTION • STRAIN NDI FOR DISBOND MONITORING • CONTINUOUS ANALYSIS OF RESULTS • REDUCED BLADE LIFE CONFIRMED • INSPECTION METHOD IMPOSES AN UNAVOIDABLE MAINTENANCE PENALTY SUMMARY THE BLADE WAS AFFECTED BY AN EXCEPTIONALLY LARGE FATIGUE CRACK - THE HELICOPTER WAS SAVED BY CONSERVATIVE DESIGN - MULTIPLE LOAD PATHS - REDUNDANT STRUCTURAL ELEMENTS - FLIGHT SAFETY IS NOW MAINTAINED BY BONDLINE STRAIN INSPECTION - THE INSPECTION IS BASED ON EXHAUSTIVE ANALYSIS OF IN-SERVICE DEFECTS Acknowledgements RNZAF Wing Commander D C Howard No. 3 Squadron Maintenance Flight RNZAF Base Auckland Technical Support Unit (ATSU) RNZAF Base Ohakea Technical Support Unit (OTSU) DTA Mr S K Campbell Mr I P Gatehouse Bell Helicopter Textron Incorporated !