Final Report
Transcription
Final Report
The Application of Woodward’s Diesel Burner System to a Low-Temperature Duty Cycle Application Using Tenneco’s ELIM-NOx SCR System Final Report for: New Technology Research and Development Program N-16 Submitted to: Houston Advanced Research Center Submitted by: Woodward Governor Company Principal Investigators: Dr. Michael B. Riley Ed VanDyne February 28, 2009 The preparation of this report is based on work funded by the State of Texas through a grant from the Texas Environmental Research Consortium, with funding provided by the Texas Commission on Environmental Quality Table of Contents 1. Executive Summary................................................................................................................. 6 2. Introduction ............................................................................................................................. 8 3. Project Objectives/Technical Approach ................................................................................ 11 3.1. 4. Exhaust Temperature Limitations and the Exhaust Heat Exchanger ............................. 13 Tasks ...................................................................................................................................... 17 4.1. Phase 1............................................................................................................................ 17 4.1.1. Phase 1 Task 1 NOx Aftertreatment Alternatives ................................................... 17 4.1.2. Task 2 Fuel Economy Effects of Thermal Regulation Approaches ....................... 18 4.1.3. Task 3 Possible Hydrocarbon Poisoning of SCR at Low Exhaust Temperatures .. 18 4.2. Phase 2............................................................................................................................ 19 4.2.1. Task 1 Selection of Candidate Engine .................................................................... 19 4.2.2. Task 2 Procurement of SCR System Components ................................................. 20 4.2.3. Task 3 Computational Fluid Dynamics (CFD) Analysis ........................................ 21 4.2.4. Task 4 Burner Control Software Development ...................................................... 22 4.2.5. Task 5 Proof-of-Concept System Fabrication......................................................... 23 4.2.6. Task 6 Engine Testing ............................................................................................ 27 5. Finance and Schedule ............................................................................................................ 42 6. Discussion/Observations ....................................................................................................... 45 6.1. Objectives vs. Results .................................................................................................... 45 6.2. Critical Issues ................................................................................................................. 46 6.3. Technical and Commercial Viability of the Proposed Approach .................................. 46 6.4. Scope for Future Work ................................................................................................... 46 7. Intellectual Properties/Publications/Presentations ................................................................. 48 8. Summary/Conclusions ........................................................................................................... 49 9. Acknowledgements ............................................................................................................... 50 10. References .......................................................................................................................... 51 11. Appendices ......................................................................................................................... 52 11.1. Appendix 1: Comparison of NOx reduction technologies, report from project N-1252 Final Report NTRD Program N-16 Woodward Page 2 11.2. Appendix 2: Poisoning in SCR Systems ................................................................... 68 11.3. Appendix 3: SwRI Testing Report of Woodward’s Burner System ......................... 74 Table of Figures Figure 1: Technologies Used by US Heavy Duty Engine Manufacturers in the 1980’s to 1990’s 8 Figure 2: Profile of exhaust temperatures in a trash truck with a diesel engine over an urban cycle ......................................................................................................................................................... 9 Figure 3: Exhaust temperature occurrence levels in a trash truck with a diesel engine over an urban cycle ...................................................................................................................................... 9 Figure 4: NOx conversion efficiency as a function of exhaust gas temperature at two different ratios of NO to NO2 (and ammonia) ............................................................................................ 10 Figure 5: Light-off with ionization signal and temperature in burner ......................................... 11 Figure 6: Flame-out with ionization signal and temperatures in burner ....................................... 12 Figure 7: Woodward burner system for control of DPF ............................................................... 13 Figure 8: Engine exhaust temperatures into heat exchanger as tested in Loveland, Colorado ..... 14 Figure 9: Schematic of double-sided heat exchanger showing flow paths ................................... 14 Figure 10: Double-sided heat exchanger on test in Loveland, CO ............................................... 15 Figure 11: Measured test engine exhaust outlet temperatures after heat exchanger ..................... 16 Figure 12: Schematic of test setup ................................................................................................ 24 Figure 13: Burner system on test engine at Woodward ................................................................ 25 Figure 14: Burner system on test engine at SwRI......................................................................... 26 Figure 15: Woodward test engine performance characteristics and SCR test points ................... 27 Figure 16: Burner inlet temperatures (left) and SCR inlet temperatures (right) from SCR testing at Woodward, October 2008 ......................................................................................................... 28 Figure 17: NOx levels entering SCR (left) and exiting SCR (right) from SCR testing at Woodward, October 2008 ............................................................................................................. 29 Figure 18: NOx reduction percentages with burner preheating exhaust prior to SCR from testing at Woodward, October 2008 ......................................................................................................... 29 Figure 19: Schematic representation (left) and graphic representation (right) of energy input and losses between burner inlet and SCR inlet. ................................................................................... 30 Figure 20: Energy balance between burner inlet and SCR inlet from testing at Woodward, October 2008 ................................................................................................................................. 31 Figure 21: Ideal consumption of diesel fuel into the burner to raise exhaust temperatures to 300°C. Heat losses and heating of burner fuel and air ignored. .................................................. 32 Figure 22: Scaled, measured flow rates of diesel fuel into the burner to raise exhaust temperatures to 300°C. Heat losses and heating of burner fuel and air included. ....................... 33 Final Report NTRD Program N-16 Woodward Page 3 Figure 23: Impact on fuel economy of heating exhaust flow to 300°C at the inlet of the SCR. Data scaled from measured data with slightly varying burner outlet temperature. Thermal and other losses included. .................................................................................................................... 34 Figure 24: Impact on fuel economy of heating exhaust flow to 300°C at the inlet of the SCR. Data calculated only. Thermal and other losses are not included. ............................................... 35 Figure 25: Torque curve of Detroit Diesel Series 60 engine with speed/load points at which SCR testing was conducted. .................................................................................................................. 36 Figure 26: Exhaust temperatures during SwRI testing for the inlet and outlet of the exhaust heat exchanger. ..................................................................................................................................... 36 Figure 27: SCR inlet temperatures with burner on during SwRI testing of Woodward burner system ........................................................................................................................................... 38 Figure 28: NOx levels entering and exiting the SCR with burner on during SwRI testing of Woodward burner system ............................................................................................................. 39 Figure 29: NOx reduction efficiencies with burner on during SwRI testing of Woodward burner system ........................................................................................................................................... 39 Figure 30: Ratio of NO2 to NOx at SCR inlet with the burner off (left) and on (right) during SwRI testing of Woodward burner system. .................................................................................. 40 Figure 31: Ammonia slip from SCR with burner on during SwRI testing of Woodward burner system. Actual test data shown in white squares ......................................................................... 41 Figure 32: Monthly project costs for N-16 ................................................................................... 42 Figure 33: Cumulative project costs for N-16 .............................................................................. 43 Figure 34: Transient performance of a burner system during Woodward testing (different system than reported here.) ....................................................................................................................... 47 Final Report NTRD Program N-16 Woodward Page 4 Table of Tables Table 1: Tube diameters to fabricate double-sided heat exchanger .............................................. 15 Table 2: Speed and load points for testing burner and SCR system at SwRI ............................... 37 Final Report NTRD Program N-16 Woodward Page 5 1. Executive Summary Diesel NOx emissions have been the subject of intense research over the past two decades. Approaches have concentrated on either in-cylinder reductions or aftertreatment. Of the aftertreatment approaches SCR systems have gained the greatest support, promising NOx mitigation up to 90% in certain circumstances. An added benefit with aftertreatment systems is that the base engine is not affected, and a wide range of engines can be serviced by a relatively small number of sizes of SCR systems. The downside of this strategy is that occasional maintenance by the engine owner is required to ensure an uninterrupted urea supply, and the engine owner must bear that cost. SCR systems work very effectively when the exhaust gases are in the range of 300°C to 450°C. When exhaust gas temperatures are below this range some form of thermal regulation is required. Woodward has developed proprietary technology around combustion ion-feedback sensing with a controller and a burner that can provide the degree of thermal regulation required to ensure the temperatures of exhaust gases are elevated to the range of efficient operation of the SCR, while simultaneously promising to minimize ammonia slip while providing high levels of NOx reduction. The Engine Systems Research group within Woodward has been developing a diesel burner for use in exhaust systems to facilitate regeneration of particulate traps. In RFGA-06 the Texas Environmental Research Consortium (TERC) was seeking technologies that would allow diesel engines operating on low-temperature duty cycles to reduce NOx effectively. The requirements for low exhaust temperatures presented a key challenge for lab testing and evaluation of the burner. For testing purposes only, a custom-design air-to-air heat exchanger was added to the exhaust system upstream of the burner to simulate the low-temperature duty cycles. This method of achieving low exhaust temperatures was selected solely to demonstrate the capabilities of the burner, not to optimize the system for fuel economy. The heat exchanger would never be included in a real-world burner system design. Woodward has demonstrated a practical diesel exhaust burner system that is capable of heating low-temperature exhaust to 300°C from idle to rated speed and 50% load. (Beyond these levels the exhaust gas temperatures exceeded 300°C even with the heat exchanger.) Selective catalyst reduction (SCR) systems are effective in reducing NOx in diesel exhaust systems only if the exhaust temperature is sufficiently high, typically above 250 - 275°C. Woodward’s burner was designed to elevate exhaust temperatures up to 650°C to allow diesel particulate filters (DPFs) to regenerate. This system was modified to operate continuously at 300°C for efficient SCR operation while allowing the higher temperatures required for DPF regeneration. An air-to-air heat exchanger was designed and fabricated to ensure exhaust temperatures reaching the burner were sufficiently reduced to be representative of low-temperature duty cycles. The duty cycles that TERC references are usually the result of transient operation, where the vehicle is driven in such a way that there is significant idle time between periods of reasonably high load. Examples include school buses and trash trucks. Under this mode of Final Report NTRD Program N-16 Woodward Page 6 operation the exhaust temperature may rarely exceed 225°C, preventing SCR systems from operating effectively. Duplicating such an operating cycle in the laboratory would be challenging for developing a burner, so the approach used was to operate at steady-state speed and load points, and remove sufficient heat from the exhaust gases to fall below 225°C. The focus of the program was to prove the capability of the burner to maintain close to 300°C at the inlet of the SCR, so the heat exchanger subsystem was operated at a high rate of heat rejection. The subsequent effects on fuel economy must not be taken as a measure of the performance of the burner in real-world applications. The correlation between engine speed and load, exhaust mass flow and exhaust temperature would require measurement in real-world applications to understand the fuel economy impacts more thoroughly. A proof-of-concept system was assembled and tested on a 12.6 L diesel engine at Woodward’s Loveland test facility with Woodward’s burner heating the now-cooled exhaust into a Tenneco ELIM-NOx SCR system. The system was calibrated and debugged, and testing was conducted over a wide range of speeds and loads where the temperatures into the burner were at or below 225°C. The exhaust was heated with the burner so that exhaust temperatures into the SCR were maintained between 297°C and 335°C. Urea dosing levels were conservative as Woodward does not have the capability to measure ammonia emissions. Overall NOx reduction under these conditions was approximately 55%. After testing at Woodward the complete system was shipped to SwRI where it was installed on a Detroit Diesel Series 60 engine. The burner controller and SCR system were recalibrated for the different engine and the engine was run with and without the burner at a number of steady-state test points, comparing the NOx reduction in both cases. The overall NOx reduction from the Detroit Diesel Series 60 engine when operating with temperatures below 225°C was 75%. Ammonia slip was below 10 ppm for 16 of the 21 test points, with higher speed and load points showing slip between 10 and 21 ppm. Tenneco engineers on-site during part of the SwRI testing indicated that the SCR catalyst was undersized. More refinement of the calibrations and an appropriately sized catalyst would allow ammonia slip levels to be reduced below 10 ppm while maintaining a NOx reduction efficiency in the 75% range. Final Report NTRD Program N-16 Woodward Page 7 2. Introduction NOx emissions are directly linked to ground-level ozone, one of the principal components in smog [1]. The high efficiencies of diesel engines, resulting from high combustion temperatures, make them one of the major sources of NOx emissions. Over the past twenty years a number of new technologies have been introduced to meet ever-tightening emissions standards, as shown below [2]. Figure 1: Technologies Used by US Heavy Duty Engine Manufacturers in the 1980’s to 1990’s The general trend of the technologies listed in Figure 1 is to reduce engine-out emissions, that is, emissions that are generated in-cylinder. There are several new and existing technologies that are effective in reducing NOx from diesel engines. Techniques for reducing NOx in-cylinder that use conventional diesel combustion include charge-air cooling, retarded injection timing (with variable injection timing (VIT) for minimal fuel economy impact) and cooled exhaust gas recirculation (EGR.) More sophisticated approaches modify the combustion modes, including homogeneous charge combustion ignition (HCCI) and low temperature combustion (LTC.) These latter approaches are still being researched and have not made it into widespread use at this stage. The alternative to in-cylinder NOx reduction approaches is to treat the exhaust gas after it has been released from the cylinder. Aftertreatment approaches include lean NOx traps (LNT) and selective catalyst reduction (SCR.) Particulates are reduced with aftertreatment using diesel particulate filters (DPF). Significant reductions in NOx in diesel engine exhausts can be achieved with an SCR system, but this requires exhaust temperatures above certain thresholds for effective operation. If the temperature of the exhaust stream is too low then heat addition is required. This implies the need to control the heat added, as well as the quantity of urea injected. Heat addition may be accomplished via electric resistance heating elements (not regarded seriously at this stage), with a diesel oxidation catalyst (DOC) provided exhaust temperatures are sufficiently high, or with burners. Using burners implies the need for accurate delivery of fuel and air, especially through transient operation. Final Report NTRD Program N-16 Woodward Page 8 An example of anticipated exhaust system temperatures from urban-cycle driving is shown in Figure 2 [3]. Figure 2: Profile of exhaust temperatures in a trash truck with a diesel engine over an urban cycle The frequency with which the temperatures in Figure 2 are exceeded is shown in Figure 3. Figure 3: Exhaust temperature occurrence levels in a trash truck with a diesel engine over an urban cycle In this case the exhaust temperatures were below 225 C over 80% of the time. NOx is made up of NO and NO2. Catalyst performance depends on the ratio of NO and NO2, exhaust gas temperature and catalyst formulation. SCR systems require exhaust temperatures to be above certain levels for efficient operation. Figure 4 shows the effects of varying temperature and NO:NO2 ratio on the reduction of NOx [4] for a particular catalyst formulation. The implication is that a higher proportion of NO2 in the exhaust allows catalyst function to be more efficient at lower inlet temperatures. Conversion of NO to NO2 facilitates this process. Final Report NTRD Program N-16 Woodward Page 9 Figure 4: NOx conversion efficiency as a function of exhaust gas temperature at two different ratios of NO to NO2 (and ammonia) DPFs for reduction of particulate emissions also require thermal regulation to ensure that temperatures are high enough to burn the trapped particulates during their intermittent regeneration cycles. In the case of diesel fueled burners, diesel fuel and air are supplied to the burner, which is located just before the DPF. Accurate control of the fuel quantity injected and air delivered is essential to control combustion in the burner for a low emission flame, to generate temperatures that both minimize fuel consumption and optimize emissions, and to be independent of the condition of the exhaust stream. Woodward’s development of ion sensing for combustion feedback provides the instantaneous control required. Where control of both particulates and NOx is required, a DPF and an SCR system may be used sequentially. The thermal characteristics of the two systems are different. An SCR system operates between 300 C and 700 C and is endothermic, while the DPF operates between 600 C and 900 C without a catalyst, or 450 C to 900 C with a catalyst, and is exothermic. The temperatures achieved at the output of a DPF may exceed the maximum operating temperatures of an SCR system, so tight control over burner outlet temperatures is required to regulate both processes with only one burner over a wide range of engine operating conditions. The control logic developed by Woodward allows accurate control of the exit temperatures to protect the SCR catalyst. There are still several challenges remaining to make this system viable for retrofit applications. These include cost reductions and more compact air sources, both of which are being addressed aggressively. Final Report NTRD Program N-16 Woodward Page 10 3. Project Objectives/Technical Approach The objective of this project was to demonstrate the combination of a diesel burner and controller capable of elevating the temperature of sub-225°C diesel exhaust to 300°C within a small margin. Woodward has developed a proprietary ion sensing technology for application to both compression- and spark-ignited engines for a variety of combustion diagnostics and control. The ion sensing system is well suited for application to a diesel burner in engine exhausts to control temperatures, allowing optimal operation of catalysts and/or DPFs. The ability of the ion sensing system to provide accurate feedback of the combustion process means that hydrocarbon spikes due to delayed light-off of the burner, unstable combustion or failing to identify a flame-out are essentially eliminated. This tight control over the combustion process ensures the inlet temperature to the SCR is maintained at appropriate levels, providing high levels of NOx reduction. Figure 5 shows temperatures and the ionization signal in a burner developed by Woodward for a diesel application. The plot shows burner light-off, and how the ion signal reacts almost instantaneously to the start of combustion, while the thermocouples take an additional half a second to register any change. This demonstrates the advantage of measuring ionization in combustion over temperature, which is a consequence of combustion. Further, in transient applications exhaust temperatures change with engine load, making it difficult to separate the effects of combustion from those of engine load change. Figure 5: Light-off with ionization signal and temperature in burner The process is similar when the flame is extinguished. Figure 6 shows this phenomenon in the same diesel burner. Again the lag between flame-out and the thermocouple reaction is significantly longer than that with the ionization signal. Final Report NTRD Program N-16 Woodward Page 11 Figure 6: Flame-out with ionization signal and temperatures in burner It is obvious from the traces in Figure 5 and Figure 6 that the ionization signal is a more immediate measure of combustion than temperature measurement, so when used in conjunction with a burner and an SCR, the ion sensing system would reduce the risks of a hydrocarbon spike both at the start and end of combustion. Woodward has developed this system to work with a burner as a temperature controller for a DPF. Figure 7 shows a schematic of such a system, although with a DPF. Final Report NTRD Program N-16 Woodward Page 12 Figure 7: Woodward burner system for control of DPF 3.1. Exhaust Temperature Limitations and the Exhaust Heat Exchanger The overriding requirement for this project was to test the capabilities of the Woodward burner with exhaust temperatures below 225°C over a significant portion of the operating map of the test engine. To achieve these low temperatures Woodward designed and fabricated an air-to-air heat exchanger. The space limitations of test cells at both Woodward and SwRI dictated that a double-sided heat exchanger of limited length be used. Sizing of the heat exchanger was estimated knowing the exhaust temperature range and the exhaust mass flow rates at different conditions. A fixed air flow using blower fans was selected, and the exhaust temperatures were allowed to find their equilibrium level at each speed and load point. Figure 8 shows the normal exhaust temperatures for the 12.6 L test engine operating over its speed and load range as tested in Woodward’s Loveland dyno facility. The area of the curve with temperatures below 225°C is only a very small fraction of the operating map. Final Report NTRD Program N-16 Woodward Page 13 Figure 8: Engine exhaust temperatures into heat exchanger as tested in Loveland, Colorado Commercially available blowers were used to pipe cooling air into the heat exchanger, flowing either side of, and in the opposite direction to the exhaust flow. (Two blowers with combined flow of approximately 1000 CFM were used.) Figure 9 shows a schematic of the cooling passages of the heat exchanger. Figure 9: Schematic of double-sided heat exchanger showing flow paths Final Report NTRD Program N-16 Woodward Page 14 Diameters of the constituent pipe sections making up the plug, exhaust flow area and cooling flow areas were evaluated to determine the effects on exhaust temperature out and pressure drop in the exhaust. Detailed optimization was not carried out as it was not felt to be necessary. The following table lists the tube diameters for commercially available stainless steel tubing, which were considered to be a reasonable compromise between cooling capacity and overall system bulk: Table 1: Tube diameters to fabricate double-sided heat exchanger Description Outermost tube Outside of exhaust section Inside of exhaust section Innermost tube Tube OD 9” 8” 7” 6” Figure 10 shows a photo of the heat exchanger on-engine during testing at Woodward’s Loveland, CO facility. Figure 10: Double-sided heat exchanger on test in Loveland, CO The additional piping required to duct the exhaust gas to and from the heat exchanger was also helpful in reducing overall exhaust temperatures. Figure 11 shows the measured exhaust outlet temperatures with an overall heat exchanger length of 2.0 m. Final Report NTRD Program N-16 Woodward Page 15 Figure 11: Measured test engine exhaust outlet temperatures after heat exchanger Final Report NTRD Program N-16 Woodward Page 16 4. Tasks The following list of phases and tasks was produced at the start of the project. Phase 1: NOx aftertreatment alternatives, fuel economy consequences of heating exhaust gases, and potential SCR poisoning Task 1: NOx aftertreatment alternatives Task 2: Fuel economy effects of thermal regulation approaches Task: Possible hydrocarbon poisoning of SCR at low exhaust temperatures Phase 2: Construct proof-of-concept NOx reduction system and perform preliminary testing Task 1: Selection of candidate engine Task 2: Procurement of SCR system components Task 3: Computational fluid dynamics (CFD) analysis Task 4: Burner control software development Task 5: Proof-of-concept system fabrication Task 6: Engine testing 4.1.Phase 1 4.1.1. Phase 1 Task 1 NOx Aftertreatment Alternatives 4.1.1.1. Phase 1 Task 1 Objective The goal of this task was to outline the different alternatives available to engine manufacturers to reduce NOx levels from diesel engines. 4.1.1.2. Phase 1 Task 1 Technical Details This task had already been completed by one of the principal investigators for project N-12. The report included in-cylinder and aftertreatment approaches used by many researchers investigating methods to reduce NOx levels. Emphasis was given to the in-cylinder effects of variable injection timing, as that was one of the main thrusts of project N-12. SCR systems appear to offer the best option of NOx reduction, especially when fuel consumption was considered. The studies referenced in this report were not specifically for engine duty cycles with low-temperature exhaust entering the SCR, so the fuel economy benefits may not relate directly to this project. Final Report NTRD Program N-16 Woodward Page 17 4.1.1.3. Phase 1 Task 1 Major Issues/Critical Paths This task was a literature study. There were no major issues or critical paths. 4.1.1.4. Phase 1 Task 1 Deliverables The deliverable from this task is the report given in Appendix 1. 4.1.2. Task 2 Fuel Economy Effects of Thermal Regulation Approaches 4.1.2.1. Phase 1 Task 2 Objective The goal of this task was to investigate the effects of providing heat by combustion and electric resistance methods on fuel economy. 4.1.2.2. Phase 1 Task 2 Technical Details Discussions were held with HARC personnel about this task after the program was awarded. It was agreed that there was little benefit in carrying out this task. Combustion systems deliver almost 100% of the energy value of the fuel as heat into the exhaust, as where electricity produced by the engine’s electrical system delivers around 30% of the energy as heat in optimal circumstances. In addition this approach appears to have attracted little interest from manufacturers, so it was agreed to delete this task. 4.1.2.3. Phase 1 Task 2 Major Issues/Critical Paths 4.1.2.4. Phase 1 Task 2 Deliverables None. None. 4.1.3. Task 3 Possible Hydrocarbon Poisoning of SCR at Low Exhaust Temperatures 4.1.3.1. Phase 1 Task 3 Objective Final Report NTRD Program N-16 Woodward Page 18 The goal of this task was to conduct a literature survey to investigate mechanisms by which SCR performance is degraded during operation. 4.1.3.2. Phase 1 Task 3 Technical Details A literature study was undertaken to review work performed by others in investigation of reduced SCR performance Mechanisms for performance degradation include contamination by sulfur, hydrocarbons, minerals in blow-by oil, crystallized urea, as well as thermal aging. Both contamination by hydrocarbons (exiting the burner) and thermal aging (if the SCR is located after an SCR in the exhaust) are potential hazards to SCR systems with a burner. 4.1.3.3. Phase 1 Task 3 Major Issues/Critical Paths This task was a literature study, so there were no major issues or critical paths. 4.1.3.4. Phase 1 Task 3 Deliverables The deliverable from this task is the report given in Appendix 2. 4.2.Phase 2 4.2.1. Task 1 Selection of Candidate Engine 4.2.1.1. Phase 2 Task 1 Objective The goal of this task was to select an appropriate candidate engine to demonstrate the effectiveness of the burner to maintain a 300°C outlet temperature from sub-225°C exhaust temperatures. This task turned out to require two engines, one for testing at Woodward in Colorado, and the other at SwRI in San Antonio, Texas. 4.2.1.2. Phase 2 Task 1 Technical Details The choice of engine (size, power, NOx levels) determined the size of burner to be designed and built. Woodward has been working with a manufacturer who provided an engine of suitable size for burner development, but who would prefer to remain anonymous. This engine is a 2004 model, 6-cylinder, turbocharged diesel engine of 12.6 L swept capacity. The engine selected for testing at SwRI was a 1998-calibration Detroit Diesel Series 60 engine. It is also a 6-cylinder, turbocharged diesel engine of 12.7 L swept capacity. Final Report NTRD Program N-16 Woodward Page 19 4.2.1.3. Phase 2 Task 1 Major Issues/Critical Paths Testing at Woodward was uneventful in terms of communications of the burner controller with the engine controller. Testing at SwRI was delayed for a short period due to the inability to communicate over the CAN bus to read speed and load settings on the engine. These values were entered manually into the controller software to ensure correct burner operation. This process was acceptable during the steady-state testing conducted, but would not be practical for transient testing. 4.2.1.4. Phase 2 Task 1 Deliverables The deliverables for testing purposes were a suitable engine for burner and SCR installation at Woodward’s test facility in Colorado, and the Detroit Diesel Series 60 engine at SwRI in Texas. 4.2.2. Task 2 Procurement of SCR System Components 4.2.2.1. Phase 2 Task 2 Objective The goal of this task was to select and procure a suitable SCR system to apply to the candidate engine(s). A mandatory requirement of this equipment is the ability to program the SCR system to achieve correct urea dosing under all engine operating conditions. 4.2.2.2. Phase 2 Task 2 Technical Details Woodward’s partner in the development of the burner system, Tenneco, markets the ELIM-NOx SCR system, so the choice of SCR system was obvious. The ELIM-NOxTM SCR system is designed to reduce NOx emission from on-road and non-road construction equipment. It meters precise amounts of the urea solution into the exhaust stream of the diesel engine. Once in the exhaust, the reagent vaporizes, mixes with the oxides of nitrogen and passes over a catalyst to turn the ozone-forming oxides of nitrogen (NOx) into water, nitrogen, and CO2. The system includes a reagent storage tank, pump, motor and filter, a patented return flow urea injector, SCR catalyst, dedicated electronic control unit (ECU) and various sensors to monitor and control the process. The system is modular, compact and packaged for quick retrofit installation. Final Report NTRD Program N-16 Woodward Page 20 4.2.2.3. Phase 2 Task 2 Major Issues/Critical Paths During testing at SwRI there was agreement between Tenneco and SwRI engineers familiar with SCR systems that the catalyst used on this program was undersized for the engines tested. The recommended catalyst size would be approximately twice the volume of the catalyst used for testing. This size difference was thought to contribute to ammonia slip in some test conditions. The catalyst sizing was not considered to be an impediment for this program however. Maximum exhaust flow during testing for peak torque output for the engine tested at Woodward’s facility in Colorado was approximately 450 g/s, while the peak flow during SCR testing was 207 g/s, under 50% of the peak flow. 4.2.2.4. Phase 2 Task 2 Deliverables The deliverable for this task was a complete ELIM-NOx SCR system from Tenneco for installation on the test engines. 4.2.3. Task 3 Computational Fluid Dynamics (CFD) Analysis 4.2.3.1. Phase 2 Task 3 Objective The goal of this task was to determine the appropriate mixing length for location of the urea injection nozzle in the entry pipe to the SCR. 4.2.3.2. Phase 2 Task 3 Technical Details Urea injected into the inlet pipe of the SCR must be uniformly distributed, and preferably fully evaporated before it enters the SCR. Failure to achieve either of these objectives may result in underutilizing the reaction sites of the SCR. Prior to identifying the Tenneco ELIM-NOx system as the preferred solution it was thought that several CFD models would have to be investigated to determine the optimal location of the nozzle. Discussions with a Tenneco engineer familiar with the system resulted in recommendations for placement that obviated the need for this analysis. The recommendations for mixing length were: 18” for adequate mixing, 24” for good and 30” for complete mixing. 4.2.3.3. Phase 2 Task 3 Major Issues/Critical Paths None. Final Report NTRD Program N-16 Woodward Page 21 4.2.3.4. Phase 2 Task 3 Deliverables The deliverable for this task was a recommended mixing length for the location of the urea injector nozzle. The range of acceptable locations was decided from discussions with an experienced Tenneco engineer rather than CFD analysis. That recommendation was that the injector should be located at least 18” from the inlet of the SCR. The test installation included locating the injector approximately 42” from the SCR inlet. 4.2.4. Task 4 Burner Control Software Development 4.2.4.1. Phase 2 Task 4 Objective The goal of this task was to develop control software to allow the burner to maintain a prescribed temperature to the inlet of the SCR. 4.2.4.2. Phase 2 Task 4 Technical Details At the start of project N-16 Woodward had developed the basic software to control the burner for light-off, ramp-up to temperature, temperature control, ramp-down and shut-off. The software monitored engine speed and load, several temperatures and the pressure drop across the DPF. Numerous set points and ramp rates were controllable in the user interface for the development work. The primary difference between controller operation for DPF regeneration and SCR operation was the desired outlet temperature. This was set initially at the outlet of the burner, but later was set to the inlet to the SCR for tighter control. Testing in this phase was at steady state only. The software has been developed for DPF regeneration to handle engine transients, but this feature was not exercised during SCR testing either at Woodward or SwRI. 4.2.4.3. Phase 2 Task 4 Major Issues/Critical Paths Testing at Woodward was conducted with correct communications between the control module for the burner and the engine ECU. The engine used CANbus communications for speed and load between the controllers. Communications between the Detroit Diesel at SwRI and the burner ECU were not feasible over the early CANbus on that engine. Scheduled testing was for steady-state points, so the decision was made not to install speed and load sensors to deliver that information to the burner ECU. As a consequence the control software interface was modified to allow user input of speed and load. Final Report NTRD Program N-16 Woodward Page 22 For future activities the effects of the thermal mass of a diesel exhaust with a DPF should be modeled and evaluated experimentally. This may require modifications to the control algorithms to ensure sufficiently accurate temperature tracking at the SCR inlet. 4.2.4.4. Phase 2 Task 4 Deliverables The deliverable for this task was control software to allow the burner to provide the required inlet temperatures to the SCR. In addition the software allowed manual entry of engine speed and load for steady-state testing. 4.2.5. Task 5 Proof-of-Concept System Fabrication 4.2.5.1. Phase 2 Task 5 Objective The goal of this task was to assemble the complete exhaust system, including air-to-air heat exchanger, burner, DPF and SCR systems, along with all the required sensors, controller, mounting hardware and data acquisition system. 4.2.5.2. Phase 2 Task 5 Technical Details A 2004 model 12.6 L test engine was mounted on a dynamometer at Woodward’s Loveland test facility. The engine was fitted with the exhaust air-to-air heat exchanger described above. The burner was installed after the heat exchanger, and DPF and SCR systems were installed after the burner. The installation was instrumented to record temperatures into the burner and SCR, and NOx emissions entering and exiting the SCR. There was no facility to measure ammonia slip. A schematic of the installation is shown in Figure 12. (The ammonia sensor is shown here, although it was not installed until the system was tested at SwRI.) As is obvious from the photo in Figure 10 there is a substantial length of exhaust pipe both before and after the heat exchanger, further contributing to reducing the exhaust temperatures entering the burner. Final Report NTRD Program N-16 Woodward Page 23 Figure 12: Schematic of test setup The exhaust system is shown on-engine during Woodward testing in Figure 13. The engine is on the lower right. Final Report NTRD Program N-16 Woodward Page 24 Figure 13: Burner system on test engine at Woodward The exhaust system was assembled in a modular fashion so that it could be shipped to SwRI for installation on a 1998 Detroit Diesel Series 60 engine. The layout could be modified somewhat for the geometry of the test cell, but the components and distances between them remained the same. The SwRI installation is shown in Figure 14. Final Report NTRD Program N-16 Woodward Page 25 Figure 14: Burner system on test engine at SwRI 4.2.5.3. Phase 2 Task 5 Major Issues/Critical Paths Incorporating the air-to-air heat exchanger in the exhaust created some issues with the volume it occupied in the dyno cell during the fabrication/installation stage. 4.2.5.4. Phase 2 Task 5 Deliverables The deliverable for this task was a complete exhaust system that included the air-to-air heat exchanger, burner and controller, DPF, SCR system and all sensors. This system was modular to allow disassembly after testing at Woodward, and reassembly for testing on a different engine at SwRI. Final Report NTRD Program N-16 Woodward Page 26 4.2.6. Task 6 Engine Testing 4.2.6.1. Phase 2 Task 6 Objective The goal of this task was to demonstrate that the Woodward burner could heat incoming exhaust gases below 225°C into a burner to 300°C at the inlet of an SCR. All testing at this stage is steady-state. 4.2.6.2. Phase 2 Task 6 Technical Details 4.2.6.2.1. Engine Performance Characteristics and Data Points for SCR Operation During Testing At Woodward Figure 15 shows the torque curve for the test engine used at Woodward. The curve show peak torque from the manufacturer. The filled circles show the speeds and torques at which SCR testing was performed. The shaded area shows the bounding box of subsequent contour plots. Figure 15: Woodward test engine performance characteristics and SCR test points Final Report NTRD Program N-16 Woodward Page 27 4.2.6.2.2. Control of Exhaust Temperatures During Testing At Woodward The temperatures into the SCR inlet were maintained within a tight range around 300°C. Figure 16 shows the temperature into the burner on the left, and into the SCR on the right. Figure 16: Burner inlet temperatures (left) and SCR inlet temperatures (right) from SCR testing at Woodward, October 2008 The burner was able to hold inlet temperatures at the SCR within a close margin over the entire test range with exhaust temperatures considerably lower than most engine applications. Testing was performed with control on the burner-out temperature. At higher speeds and loads the SCR inlet temperature drifted upwards because thermal losses from the DPF and piping did not increase as rapidly as the exhaust enthalpy. 4.2.6.2.3. Performance of ELIM-NOx System During Testing At Woodward The calibration of the urea injection system was carried out with an awareness of the lack of ammonia measurement capability. Accordingly NOx reduction levels were kept well below the maximum achievable. Figure 17 shows NOx levels before and after the SCR catalyst. Final Report NTRD Program N-16 Woodward Page 28 Figure 17: NOx levels entering SCR (left) and exiting SCR (right) from SCR testing at Woodward, October 2008 The overall NOx percentage reduction is shown in Figure 18. Figure 18: NOx reduction percentages with burner preheating exhaust prior to SCR from testing at Woodward, October 2008 Final Report NTRD Program N-16 Woodward Page 29 The use of a more appropriately sized injector at low speeds and loads would improve NOx reduction. 4.2.6.2.4. Energy Balance on Burner System During Testing At Woodward The additional fuel consumed in the burner must be compared to the heat addition to raise the exhaust temperature to the required level for efficient SCR operation. Figure 19 shows a schematic representation of the heat exchanger-burner-piping-DPF system, from the inlet of the burner to the inlet of the SCR, with the sources of energy input and thermal losses. The input and losses are also shown qualitatively in the accompanying bar graph. Figure 20 shows the actual gains/losses at the different test points. The energy (rate) balance on the burner system is split into five components: : fuel energy (rate) added to the burner : energy (rate) to raise the temperature of the air and fuel delivered to the burner to the SCR inlet temperature : heat losses (rate) from the outside of the piping, burner and DPF : thermal energy (rate) to vaporize the urea : energy (rate) to raise the exhaust temperature to the SCR inlet temperature. Figure 19: Schematic representation (left) and graphic representation (right) of energy input and losses between burner inlet and SCR inlet. Final Report NTRD Program N-16 Woodward Page 30 Energy Balance between Burner and SCR Project N-16, Low Temperature NOx Reduction, October 2008 40000 35000 30000 Power (W) 25000 Q urea 20000 Q loss 15000 Q into air, fuel Q into exhaust 10000 5000 0 RPM/Torque (ft-lb) Figure 20: Energy balance between burner inlet and SCR inlet from testing at Woodward, October 2008 It is evident from Figure 20 that reducing thermal losses from the system is critical to minimizing the fuel consumption increase. 4.2.6.2.5. Correlation Between Exhaust Temperature and Mass Flow for Heat Addition The thermal input required to raise exhaust temperature to 300°C is a function of the exhaust mass flow rate and its temperature. Figure 21 shows this relationship for the ideal case of no thermal or other losses. Final Report NTRD Program N-16 Woodward Page 31 Figure 21: Ideal consumption of diesel fuel into the burner to raise exhaust temperatures to 300°C. Heat losses and heating of burner fuel and air ignored. Real systems will have thermal losses between the inlet of the burner and the inlet of the SCR, so the thermal input will be higher than this theoretical figure. In addition the different rates of heat transfer from the exhaust gases inside the piping and DPF relative to the outside will skew the shape of the contours. Figure 22 shows the fuel flow to the burner from measured data during experimentation at Woodward, scaled to an inlet temperature of 300°C at the SCR. Final Report NTRD Program N-16 Woodward Page 32 Figure 22: Scaled, measured flow rates of diesel fuel into the burner to raise exhaust temperatures to 300°C. Heat losses and heating of burner fuel and air included. 4.2.6.2.6. Fuel Economy Impact to Raise Exhaust Temperature to 300°C The thermal input required to raise exhaust temperature to 300°C is a function of the exhaust mass flow and the exhaust temperature into the burner. The exhaust cooling system employed for this project was designed to remove more heat from the exhaust than absolutely necessary to ensure sub-225°C temperatures into the burner. This design overkill imposes an additional fuel economy penalty on the burner system. Figure 23 shows the impact on overall fuel economy of the burner operating with the system tested at Woodward. The increase ranges from a low of 2.9% at high speed, high load, to a maximum of 47% at idle over the engine speeds and loads tested and for the rate of exhaust heat removal achieved with the exhaust heat exchanger. Final Report NTRD Program N-16 Woodward Page 33 Figure 23: Impact on fuel economy of heating exhaust flow to 300°C at the inlet of the SCR. Data scaled from measured data with slightly varying burner outlet temperature. Thermal and other losses included. The effects of thermal losses as well as the heating of the air and fuel supplied to the burner obviously increase fuel consumption. To gauge the impact of thermal and other losses on fuel economy, an ideal burner system is shown in Figure 24. Final Report NTRD Program N-16 Woodward Page 34 Figure 24: Impact on fuel economy of heating exhaust flow to 300°C at the inlet of the SCR. Data calculated only. Thermal and other losses are not included. 4.2.6.2.7. Burner and SCR Testing at SwRI The entire exhaust system comprised of the heat exchanger, burner, DPF and SCR were shipped to SwRI for installation on a Detroit Diesel Series 60 engine, vintage 1998. The engine performance was mapped for basic characteristics, and to ensure that exhaust temperatures were similar to testing at Woodward. A plot of the engine peak torque curve, overlaid with the test points selected for evaluating the SCR system is shown in Figure 25. Final Report NTRD Program N-16 Woodward Page 35 Figure 25: Torque curve of Detroit Diesel Series 60 engine with speed/load points at which SCR testing was conducted. 4.2.6.2.8. Control of Exhaust Temperatures During Testing at SwRI The heat exchanger and piping were installed on the Detroit Diesel engine, and the burner controller was recalibrated to hold tighter values at the SCR inlet. The exhaust temperatures were mapped with and without the burner operating. The results are shown in Figure 26. Figure 26: Exhaust temperatures during SwRI testing for the inlet and outlet of the exhaust heat exchanger. Final Report NTRD Program N-16 Woodward Page 36 The range of speed and load values over which the exhaust temperatures are below 225°C is broader than for testing at Woodward. A range of engine speeds and loads was selected for testing the burner and SCR system. These points are shown in Table 2. Table 2: Speed and load points for testing burner and SCR system at SwRI Operation of the burner during steady-state testing at the points in Table 2 produced inlet temperatures to the SCR that were close to the 300°C target, as shown in Figure 27. Final Report NTRD Program N-16 Woodward Page 37 Figure 27: SCR inlet temperatures with burner on during SwRI testing of Woodward burner system 4.2.6.2.9. NOx Reduction with Woodward Burner System During Testing at SwRI Tenneco’s ElimNOx system was recalibrated for operation on the Detroit Diesel engine. The engine was then operated over the range of speed and load points in Table 2, and the NOx emissions before and after the SCR were measured. The emissions levels are shown in Figure 28. Final Report NTRD Program N-16 Woodward Page 38 Figure 28: NOx levels entering and exiting the SCR with burner on during SwRI testing of Woodward burner system NOx reduction efficiency is shown in Figure 29. Figure 29: NOx reduction efficiencies with burner on during SwRI testing of Woodward burner system Final Report NTRD Program N-16 Woodward Page 39 4.2.6.2.10. Effect of Burner on NO:NO2 Ratio During Testing at SwRI Increasing the ratio of NO2 to NO increases the activity of some catalysts at lower temperatures [4]. Figure 4 shows this trend. An alternative perspective on Figure 4 is that a percentage of NO2 to NOx approaching 50% aids in lower temperature NOx conversion. Figure 30 shows the percentage of NO2 to NOx for the Detroit Diesel engine both with and without the burner operating. Figure 30: Ratio of NO2 to NOx at SCR inlet with the burner off (left) and on (right) during SwRI testing of Woodward burner system. With burner operation the ratio of NO2 to NOx is close to 50%, which should allow improved catalyst function at lower temperatures. 4.2.6.2.11. Ammonia Slip from SCR with Woodward Burner During Testing at SwRI The availability of ammonia slip measurement during SwRI testing allowed more optimal urea calibrations of the ElimNOx system compared to testing at Woodward. Ammonia slip levels were set at 10 ppm for testing, corresponding to the level set by the California Energy Commission in a modification made to conditions for certification AQ-48 made on August 8, 2007 [5]. Ammonia slip during testing is shown in Figure 31. Final Report NTRD Program N-16 Woodward Page 40 Figure 31: Ammonia slip from SCR with burner on during SwRI testing of Woodward burner system. Actual test data shown in white squares The labels in Figure 31 show that five of twenty-one test points had ammonia levels above 10 ppm, the highest being 20.9 ppm. (Recalibration of the SCR system was undertaken to reduce these levels, but during this process there was contamination of the SCR with diesel fuel as a result of a power supply failure to the air pump for the burner. There was insufficient time left at the end of testing to resolve the issue, so the recalibration and retesting were not carried out in this program. See the Discussion section below.) Final Report NTRD Program N-16 Woodward Page 41 5. Finance and Schedule The monthly expenditures for project N-16 are shown in Figure 32. N-16 Monthly Project Costs $140,000 $120,000 $100,000 $80,000 $60,000 $40,000 $20,000 $0 Monthly NTRD Monthly Cost Share Monthly Project Cost Figure 32: Monthly project costs for N-16 The cumulative costs are shown in Figure 33. Final Report NTRD Program N-16 Woodward Page 42 N-16 Cumulative Project Costs $900,000 $800,000 $700,000 $600,000 $500,000 $400,000 $300,000 $200,000 $100,000 $0 Monthly NTRD Monthly Cost Share Monthly Project Cost Figure 33: Cumulative project costs for N-16 The initial contract period for project N-16 was from 11/28/2006 to 8/31/2007. Several extensions were granted. They were: Grant Amendment #1: Extension: to 5/31/2008 – due to burner development process Grant Amendment #2: Extension: to 12/31/2008 – due to project progress and third party testing schedule There were several revisions to the budget. These included: June 2008 o Budgeted items under Equipment were transferred to Supplies and Materials and Personnel Costs o Adjustments made within Supplies and Materials no changes to the bottom line December 2008 o Remaining budgeted balances transferred to Personnel Costs Explanatory notes for budget changes: January 2008: activity increase in burner development work May – June 2008: activity increase due to supplies and materials purchases Final Report NTRD Program N-16 Woodward Page 43 July 2008 – NTRD Personnel Costs budgeted amount depleted, and costs were absorbed by cost share October 2008: increase due to Cost Share and first SwRI testing payment November: increase due to travel and testing at SwRI – second testing payment December: approval to portion remaining funds to Personnel Costs. Cost share from July and August Personnel Costs removed, recalculated and added back in for final invoicing Final Report NTRD Program N-16 Woodward Page 44 6. Discussion/Observations 6.1.Objectives vs. Results The objective of this project was to demonstrate the combination of a diesel burner and controller capable of elevating the temperature of sub-225°C diesel exhaust to 300°C within a small margin. This goal was met completely (see Figure 16 and Figure 27.) A follow-on metric of the success of the burner performance was the level of NOx reduction with the elevated exhaust temperatures. These levels differed between testing at Woodward and at SwRI based on the ability to measure ammonia slip, which may become more important in the calibration phase of the SCR dosing system. Testing at Woodward was conducted without the ability to differentiate between NO and NO2, nor to measure ammonia slip. However measurements were taken of the effect on fuel economy to raise exhaust temperatures to 300°C at the SCR inlet. With overall NOx reduction levels of 55% the fuel economy penalty ranged from 3% to 47%, depending on speed and load, and with the level of exhaust cooling applied during lab testing. These figures are difficult to interpret without integrating the effect over a realistic operating cycle to determine the effect on fuel economy. However it is realistic to point out that reductions in thermal losses off the exhaust system would reduce the fuel consumption penalty by 50% or more (see Figure 23 and Figure 24.) Initial sizing of the SCR system was made for a 2004-calibration 12.6 L engine at Woodward, with engine-out NOx levels some 25% lower than the NOx levels on the Detroit Diesel engine used for testing at SwRI. Based on observations from both Tenneco and SwRI engineers the recommended SCR volume on the Detroit Diesel should be approximately twice that of the current system. For the range of speeds and loads tested (due to the sub-225°C exhaust temperature requirement, and the use of an exhaust heat exchanger) this was not considered to be an issue. The exhaust flow over the range tested was below half that of peak output, mitigating the effect of the undersized SCR. Having said that though, the higher ammonia slip numbers occurred at higher speed/load points (see Figure 31), indicating that a larger SCR volume, and thus more reaction sites in the catalyst, would aid in meeting the 10 ppm target. The ammonia slip measurements were made on a system that has not been optimized. There were five of twenty-one test points with ammonia slip above the self-imposed 10 ppm limit. The highest value was 21 ppm, at a speed and load where the SCR system was thought to be near its capacity for efficient NOx reduction. Had the SCR system been sized correctly this issue may not have occurred. These points were to be retested, but during this process there was a failure of the power supply to the air pump for the burner. Normal overrides were not in place with the burner due to the experimental nature of the testing, the recalibrations to the ELIM-NOx controller, and the need to make minor modifications to air/fuel ratios with the cooled exhaust. As a consequence of the power supply failure to the air pump raw fuel was injected into the burner can before the pump failure was detected. When the air pump was operational again the process of relighting the burner resulted in combustion that sprayed raw diesel fuel downstream into the SCR. Subsequent attempts to heat the SCR system to a high enough temperature to Final Report NTRD Program N-16 Woodward Page 45 drive out the diesel were unsuccessful. (The exhaust cooler was operated during the process to avoid potential cracking of the cooler with high temperature gradients.) The major goals of the program had been achieved to that point, and the test cell was needed for other programs, so the testing was halted. 6.2.Critical Issues The primary approximation made for this project was to design and build an air-to-air heat exchanger to reduce exhaust temperatures, to demonstrate the capabilities of the burner and controller. It is difficult to determine whether the steady-state temperatures resulting from the heat exchanger are representative of the exhaust temperatures that would be seen in real-world testing. It is uncertain whether the effect on fuel economy was realistic, and fuel economy is an important operating characteristic. Future testing should be done on an application where the actual field conditions can be replicated. Heat loss between the engine and the SCR should be minimized in a vehicle setup that represents field conditions. 6.3.Technical and Commercial Viability of the Proposed Approach There is little doubt that Woodward’s burner and controller system is capable of providing the required heat addition and thermal regulation to enable low-temperature duty cycle engines to work effectively with SCR systems for NOx reduction. Validation of the ability of the burner and controller to provide robust performance under transient operation in conjunction with an SCR system still remains to be proven. (See the next section regarding transient performance.) The commercial viability of the technology depends on a number of factors, not the least of which is the cost of verification. It is unclear how the EPA would want to verify the performance of the burner, as it does not reduce emissions by itself, but rather it allows adjunct systems (DPF, SCR) to perform more effectively. If several different sizes of burner could be tested independent of these other systems, then the path to commercialization is relatively straightforward. However if specific combinations of these systems are required to undergo verification the economic opportunity may be very limited. 6.4.Scope for Future Work There are several steps that are required moving forward. The first is to validate performance of the burner and controller under transient load conditions. Final Report NTRD Program N-16 Woodward Page 46 Testing of the burner system for the SCR was conducted at steady-state conditions only. The Woodward burner system has been tested over transient cycles in other applications, and has been shown to hold a target temperature with close tolerances. Figure 34 shows a plot of a transient performance test on a different burner system at Woodward performed outside of this program. The burner was operated over a 20-minute transient cycle, then switched off. (Details of the plot have been suppressed for confidentiality.) Figure 34: Transient performance of a burner system during Woodward testing (different system than reported here.) Similarly the ELIM-NOx system has been designed for transient operation on diesel engines. Transient operation may result in slightly lower NOx reduction percentages to avoid ammonia slip. As suggested above, testing should be carried out on an appropriate transient duty cycle application, where exhaust temperatures are representative of real-world driving conditions. Identification of suppliers for components should be carried out, and the resulting system should be prepared for verification testing. Final Report NTRD Program N-16 Woodward Page 47 7. Intellectual Properties/Publications/Presentations There are no intellectual property developments as a result of this project. Woodward is planning to prepare a paper for publication in a suitable refereed forum in the next six months. The forum has not been selected at this stage. Woodward made a presentation at a HARC workshop in Houston in February of 2008. Final Report NTRD Program N-16 Woodward Page 48 8. Summary/Conclusions The following conclusions may be drawn from the data presented: 1. With exhaust temperatures at or below 225°C the burner system has shown its capability to maintain temperatures into the SCR inlet of 300°C with a tight tolerance. 2. The burner system is capable of heating the exhaust flow at idle to 300°C. 3. NOx reductions of 75% or more appear achievable over most of the speed/load range with burner inlet temperatures below 225°C. 4. The fuel penalty measured is almost certainly higher than will be experienced in real world applications. Exhaust temperatures entering the burner during these tests are felt to be unrealistically low with the high-heat rejection heat exchanger in the exhaust system. Therefore the energy input to raise exhaust temperatures back to 300°C for the SCR inlet is unrealistically high. 5. Minimization of thermal losses off the exhaust system is critical. At most speeds and loads these losses account for a third or more of the burner fuel requirement. 6. The fuel economy impact is high for such low exhaust temperatures. Operation of the SCR at lower temperatures would improve this penalty, but the NOx conversion efficiency may suffer. 7. Ammonia slip levels below 10 ppm appear feasible over the operating range tested. Results from testing show this burner-controller combination to be a viable solution for the problems of low-temperature duty cycle engine applications. There are commercially available burners used for active regeneration, but mainly used for diesel particulate filters, and mainly developed in-house for the OEM’s own use. The technology is becoming more mature and more sales and marketing information is available, but it is difficult to benchmark other technologies at this point. Based on literature searches, Woodward believes that there are no other fuel-based burner systems for supplemental heat for SCR systems in production. Woodward’s application is unique because it uses ion sensing in closed loop control to detect combustion. Other technologies sense temperature and seem to have difficulty differentiating a transient exhaust temperature from actual flame light-off or blow-out. Woodward is working with Tenneco to release a product for Tier 4 emission regulations. In first- fit applications, the OEM will certify the system with the EPA. For retrofit, the manufacturer of record would bring this to the EPA. Woodward has not selected a delivery partner for retrofit and the timeline for the EPA verification has not been defined. Woodward has tested the burner design on many applications, including trucks, with minimal changes to the design. Final Report NTRD Program N-16 Woodward Page 49 9. Acknowledgements The preparation of this report is based on work funded in part by the State of Texas through a grant from the Texas Environmental Research Consortium with funding provided by the Texas Commission on Environmental Quality. The SCR system was procured through Tenneco, whose personnel assisted with their experience and knowledge in the commissioning and calibration of the SCR system. The advice, efforts and experience of the personnel at SwRI under Dr. Magdi Khair were greatly appreciated. Dr. Qilong Lu at SwRI worked tirelessly to ensure consistent and complete results from testing at SwRI. Final Report NTRD Program N-16 Woodward Page 50 10. References 1. http://www.ci.austin.tx.us/airquality/ozone.htm, All About Ozone 2. Engine Design for Low Emissions, DieselNet 2003 3. DSNY and Cummins Inc.: A Collaboration Towards Cleaner Air. A Demonstration of Diesel Particulate Filter Emission Control Technologies on Refuse Collection Trucks and Deployment of Natural Gas Powered Street Sweepers. Project Summary Report, October 2005. www.nescaum.org/documents/cummins_dsny_report_final.pdf/ 4. W. Addy Majewski, “Selective Catalyst Reduction,” DieselNet.com 5. Letter from California Energy Commission, “Midway Sunset Cogeneration Project (85-AFC-3C), Staff Analysis of Request to Increase Ammonia Slip”, August 2007, http://www.energy.ca.gov/sitingcases_pre-1999/midway_sunset/2007-0810_STAFF_ANALYSIS_OF_REQUEST_MIDWAY.PDF Final Report NTRD Program N-16 Woodward Page 51 11. Appendices 11.1. Appendix 1: Comparison of NOx reduction technologies, report from project N-12 Final Report NTRD Program N-16 Woodward Page 52 Funding Opportunity RFGA-03 Area of Interest: Development and Testing of Engine Upgrade/Retrofit Kit for Existing Engines Applicant: Motive Engineering Co. 19 Old Town Square Suite 238 Fort Collins, CO 80524 Point of contact: Michael B. Riley, President Telephone: (970) 221-9600 / (970) 218-0141 Fax: (970) 221-3863 Email: [email protected] Project Title: A Novel Method of Mechanical Variable Injection Timing to Reduce NOx Emissions Date: January 11, 2007 Phase 1: Benefits of Variable Injection Timing Phase 1 Report Grant N-12 Page 1/15 Benefits of Variable Injection Timing When emissions standards for heavy-duty diesel engine manufacturers tightened in 1991 the industry made the transition from mechanical, fixed injection timing, meaning fixed start of injection (SOI), to more expensive electronically varied SOI. This report seeks to summarize research work conducted both before and after that time to quantify the benefits of variable injection timing (VIT.) There are numerous studies that report the effects of variable SOI [1, 2, 3, 4, 5.] The studies cited from 1981 to 2002, and generally measure the effect of SOI change on fuel consumption and NOx emissions. Locomotive Application In [1] the authors studied the emissions and fuel economy effects on locomotive engines. Of particular interest is the GE 7FDL locomotive engine whose unit pump injection system is a good candidate for MEC’s eccentric sleeve phasing (ESPi™) system for variable SOI. These engines are normally tested over an eight-point duty cycle, but to reduce total testing time their timing sweeps for determining the effects on fuel economy and emissions were conducted at three points. The points chosen were at idle, notch 5 and notch 8. Results quoted are weighted with 50% at the idle condition, and 25% each to the other two points. Extrapolating from the data in the paper they indicate that a reduction of 25% in NOx would require the SOI to be retarded by just over 6° crank, with corresponding drop in fuel economy of just over 3%. Midrange The engine tested in [2] was a 9.5 L truck engine certified to Euro 2 emissions. The aim of the study was to determine the emissions from different diesel fuel formulations, however by testing at the stock, fixed timing, and one other setting with constant NOx output, useful extrapolations could be made on their reference fuel. Testing was conducted over a 13-mode European cycle, again averaging the results. One of the fuels used represented a low-sulfur European fuel, and results using this fuel are referenced. The engine used a fixed SOI of 10° BTDC for the baseline tests. SOI was then altered to produce a fixed NOx level of 6.3 g/kW-hr, or a reduction of 7%. While extrapolating these results to a 25% reduction in NOx may not be linear it points to fuel consumption worsening by approximately 4%, with retarding the SOI by some 5° crank. Initially it appears that it is possible to reduce NOx by 25%, simply by retarding SOI by an average of 5° to 6° crank, but the penalty is paid in fuel economy. In most references [1, 2, 4, 5] data reported are averaged over some sort of representative cycle, disguising the effects of SOI change at different speeds and loads. In [3] however, specific examples are given of these effects, as shown in Figure 1 below. Phase 1 Report Grant N-12 Page 2/15 Figure 1: Test results reported in [3] for BSFC vs. SOI at different speeds and loads Heavy Duty Testing was performed on a single-cylinder test engine, representing a heavy duty truck application. Data for 25%, 50% and 100% load were taken at 1130 and 1420 rpm. Like all other studies reported they show that advancing SOI at all speeds and loads results in increasing NOx output as shown in Figure 2 below. The effect on fuel economy is more varied. In this case it is obvious from Figure 1 that the location of optimal timing for fuel consumption shifts significantly with load, and somewhat with speed. Further, at some load conditions the effect on fuel consumption appears flat over a wide range of timing, allowing timing selection to be made to minimize NOx emissions. Figure 2: Test results reported in [3] for BSNOx vs. SOI at different speeds and loads Assuming that static SOI would occur at 16° BTDC it is possible to estimate the changes in BSFC, BSNOx and, to a certain extent, particulates. (The scale chosen for the particulate plots made it difficult to determine changes in emissions with any degree of accuracy.) Phase 1 Report Grant N-12 Page 3/15 For the case of full load at 1130 rpm, the NOx level was 12 g/kW-hr. Reducing the NOx level to 9 g/kW-hr required a 7.5° timing retard, and fuel consumption worsened by 1.5%. However at 25% load the initial NOx level was 31 g/kW-hr. When this was reduced by 25% to 23 g/kW-hr the timing retard was 4°, and fuel consumption improved by 1.6%. In this case it was more beneficial to retard the timing further, by 10°, which gave an improvement in fuel consumption of almost 4%. With different SOI values feasible at different speeds and loads it may be possible to reduce overall NOx emissions by the 25% target required while having little impact, if any, on fuel consumption. As an example the 1420 rpm data could be considered at full load. In Figure 1 it is apparent that the fuel consumption varies very little between 14° BTDC and 11° BTDC. (There is no data at the 16° BTDC point.) However the NOx level falls off by 12%. Depending on the duty cycle of the engine concerned this may be a suitable trade-off between NOx emissions and fuel economy over the entire cycle while the overall target of 25% is achieved. From all the data found so far in the literature it appears that preserving fuel economy is not feasible with a fixed SOI retard. Mechanical Injector Design Considerations Dual and Single Helix Pumps The data in Figure 2 show that NOx increases significantly as load decreases with fixed SOI timing. This is due to the excess air in unthrottled diesel engines at part load. To counteract this tendency, as NOx emissions regulation began, many non-electronic (or mechanical-only) fuel systems changed to modified designs known as “dual helix” plungers to retard SOI timing as fueling decreases. Mechanical-only systems control SOI and how much fuel is injected by machined cuts in the outer cylindrical surface of the injection plunger. As the injection plunger begins to move upward, fuel flows through the cut plunger passages into a “spill port” in the pump barrel until the lower edge of the cut is reached, which closes the port, and traps fuel in the pumping volume. This trapped volume is then pressurized by the plunger upward motion for injection. End of injection (EOI) occurs when another cut in the plunger connected to the pressurized injection volume reaches the spill port and releases the fuel pressure. A “single helix” plunger has a horizontal edge cut for (fixed timing) SOI, and regulates the amount of fuel injected by rotating the plunger so that a helical cut ends injection, with the amount injected a function of the distance between the SOI horizontal cut and the EOI helical cut at the spill port position. A “dual helix” plunger has a second helical edge cut (instead of horizontal) for SOI so that as the plunger is rotated to regulate fuel quantity, the SOI timing is also modified. SOI Lag Due to Line Length Although dual helix plunger systems have much less variation in NOx versus engine load, the SOI timing is still a direct function of the amount of fuel injected and does not change with engine speed. With pump/line/nozzle (PLN) systems, using either a single multicylinder inline pump assembly, or several separated single cylinder unit pumps, there is still a significant delay between the beginning of an injection pulse at the pump Phase 1 Report Grant N-12 Page 4/15 and the resulting pulse reaching the injector tip, due to the speed of sound in the fuel and the distance along the length of the injection line and through the injector. These delays in each line and nozzle are nearly constant in absolute time (seconds), meaning that the delay in engine crank angle (degrees) varies with engine speed. Thus SOI timing retards as speed is increased. For example, for a 720 mm line length, the delay can increase from 2.6 deg at 800 RPM to 7.2 deg at 2200 RPM, causing a 5.6 deg retard in SOI at 2200 vs. 800. This runs opposite to the desired trend in SOI versus speed, where for constant BSNOx, SOI timing is usually advanced as engine speed increases. Resulting Compromises in SOI Timing Thus even with a dual helix system, the phasing of the injection pump and resulting SOI timings are usually limited by one or only a few speed/load regions at which the highest NOx is produced, usually at the lower speed and high load ranges. With a single helix system, the phasing is often limited by the very high NOx lower speed and lower load ranges. All other points then are not optimized in SOI timing for the best BSNOx vs. BSFC tradeoff. This results in higher overall fuel consumption throughout the full speed/load range, which is magnified if the application duty cycle requires significant amounts of time in the higher speed range. With VIT, the SOI timings can be independently tailored so that in the highest NOx regions, SOI timing is retarded, and in the lower NOx regions, SOI timing is advanced. Thus overall NOx can be reduced without a significant penalty in fuel consumption, and even sometimes an improvement, depending on application duty cycle. Summary statement Fixed retard of SOI for NOx reduction of 25% results in a fuel economy penalty of 3 – 4%. VIT can achieve the same level of NOx reduction with a fuel economy penalty that is much lower, and may sometimes even be an improvement, depending on the duty cycle. EFI Conversion Cost Estimates Finding suitable cost information for comparison purposes has been difficult. Some information has been found on the difference in cost between mechanical injection systems, and their subsequent model electronic versions, and will be summarized here. Some of this information has been provided through personal contacts, and should be regarded as approximate. Other numbers are for retail systems that may be purchased through distributors. However there are no readily available cost numbers that allow direct costing of converting existing mechanical injection systems to electronically controlled, fully variable SOI timing systems. The initial cost information is for replacing a mechanical in-line pump for 6-cylinder heavy-duty diesel engines with an electronically controlled pump. This comparison is made difficult by the difference in architecture between this style of pump, and the MEC ESPi™ system which is intended for applications using unit pumps. Phase 1 Report Grant N-12 Page 5/15 The mechanical in-line pump units are estimated to cost $1,000 to $1,200 to the engine manufacturer. A replacement electronically controlled pump (for varying SOI) is estimated to cost $2,200. (Note that this cost comparison assumes that a direct replacement pump is available for the particular engine under consideration. If a generic electronic pump replaces an existing tailored unit the costs are certain to be considerably higher.) The estimated OEM cost of the appropriate engine control module (ECM) is $400 to $450. If the markup for retail sale is in the range of 50 – 100%, then the additional cost of variable SOI to the end customer is in the range of $2,100 to $3,300 for the components alone for a six-cylinder, in-line diesel engine. The cost of labor for removal of the old system and installation of the new system must be added to these numbers, and the cost of replacement nozzles should be added as well. In comparison, the cost of hardware for the MEC ESPi™ system for this engine type to vary SOI timing only is estimated to be $3,400 (including modified unit pumps) from the information given in the proposal application. As above, labor is additional, but should be comparable. Timing maps for different speed/load conditions for a 25% NOx reduction will have to be generated during the verification stage of the MEC ESPi™ system. These costs have not been included here. They are difficult to estimate due to uncertainty in the numbers of possible candidate engines. However they should be comparable to conversion costs to electronic systems if they were not tailored to the candidate engine. Current retail prices for heavy duty unit injectors (with wiring) for electronically (spill valve) controlled systems are in the range of $400 per injector or $2,400 for a 6-cylinder engine. The ECM for these systems is estimated to cost $1,500. Sensors ($300) and a gear pump for pressurizing the fuel ($300) would bring the hardware cost estimate for this type of system up to $4,500. It is not clear whether EFI conversions require different cam profiles, necessitating either replacing or modifying the existing camshaft. If so this cost would be additional, and is not included here. If suitable solenoid controlled injectors are not available for older, candidate engines then the conversion cost to the MEC ESPi™ system should be considerably lower than electronically controlled SOI injection systems. In the case where such injectors are available, the hardware cost estimates for replacement hardware to convert existing mechanical injection systems to electronically controlled SOI timing appear to be in the same range, or slightly more expensive, than the proposed MEC system. NOx Reduction Approaches NOx is formed in-cylinder as a consequence of the combustion process. There are two general areas to reducing NOx, and techniques in these areas may be used in tandem. The first is in-cylinder, where the conditions that lead to the formation of NOx are modified so that there is less NOx produced. VIT is one of the techniques that can achieve this, but there are others, as described below. Phase 1 Report Grant N-12 Page 6/15 The second approach is to accept the levels of NOx produced in-cylinder and then chemically reduce it in the exhaust. Such aftertreatment approaches may be used in conjunction with in-cylinder techniques to lower the overall NOx output. Their combined use is more a matter of economics than practicality. Available Technologies – In-Cylinder The previous section described the effects of variable SOI on NOx emissions, fuel economy and particulates. The use of higher injection pressures can assist in reducing NOx if later SOI is used with the resulting smaller fuel particles [6]. The following plot [7] contains a concise summary of the different technologies for dealing with NOx and particulates. For in-cylinder technologies the plot demonstrates the effect of SOI on NOx and particulates (more advanced timing leads to higher NOx and lower particulates), and the effects of EGR (more EGR leads to higher particulates and lower NOx.) Meanwhile a combination of aftertreatment approaches helps engine manufacturers in achieving the 2007 emissions standards (shown in the lower left hand corner of the plot.) Figure 3: Summary of in-cylinder and aftertreatment technologies from [7] in reducing emissions Besides new combustion system approaches like HCCI (homogeneous charge compression ignition) and PCC (partial HCCI) the primary technique used to reduce NOx in-cylinder is exhaust gas recirculation (EGR), which, to be most effective, requires cooling. This approach requires external valving and piping, and a cooler for the exhaust gas. (HCCI and PCCI will not be addressed here. For older engines where retrofit Phase 1 Report Grant N-12 Page 7/15 technologies are being considered it is highly likely that these new combustion systems would require greater changes to the engine than would be economic.) EGR works by displacing oxygen in the intake charge with relatively inert gases. With less oxygen available the combustion process will be somewhat slower, leading to lower temperatures. In addition the added CO2 and water vapor in the exhaust stream affects the rate of temperature rise due to their high thermal capacitance relative to other gases. It is also the lower oxygen levels of the intake charge that reduces the oxidation of soot particles, leading to higher PM emissions. The following diagram [8] show the effect of cooled vs. uncooled EGR on NOx, particulates and intake manifold temperature. While the effect of cooling the EGR has little effect on NOx, the effect is substantial on particulates. Figure 4: Effect of EGR temperature on NOx, PM and intake manifold temperature from [8] EGR approaches usually increase the load on the engine cooling system, and impose a fuel economy and particulates penalty [9, 10], although the latter may be mitigated if combined with a diesel particulate filter (DPF.) A further constraint that will apply to retrofit applications is whether the engine is turbocharged or not, and whether a highpressure or low-pressure loop is selected for returning the EGR to the cylinder, as shown in the following diagram. Phase 1 Report Grant N-12 Page 8/15 Figure 5: High pressure EGR loop (left) and low pressure EGR (right) from [8] EGR has certain drawbacks though. With higher particulates the gas stream diverted back to the engine will increase wear. (If used with a DPF this is not as much of an issue, although the low pressure loop must be used, incurring a fuel economy penalty to recompress the EGR, and adversely affecting transient response. Also the combination would be expensive for retrofitting older engines.) During transients the volume of EGR in the piping and heat exchanger will cause additional particulates due to the rate of fueling exceeding the available air even more than a non-EGR engine. Piping, heat exchanger and valving for EGR can be cumbersome and expensive. Available Technologies – Aftertreatment There are a number of aftertreatment technologies available for reduction of both NOx and particulates. These technologies are: • SCR – selective catalyst reduction • LNT – lean NOx trap • DPF – diesel particulate filter • DOC – diesel oxidation catalyst Technologies that reduce particulates are included in this study because both VIT and EGR impact particulates. If particulate levels are worse due to reduced NOx (and possibly improved fuel economy) there will be a trade-off at some point to maintain air quality. SCR Technology This approach introduces a reducing agent into the exhaust stream, either by the addition of urea or ammonia directly, or the addition of extra fuel to provide the reducing reagent [9, 11, 12, 13.] The resulting chemical reaction reduces NOx to oxygen and nitrogen. This approach has been used in stationary power plants for some time. Efficiencies are very high for engines that operate under constant conditions, but are lower for operation under transient conditions. (Model-based algorithms are under development to allow more accurate prediction of the amount of ammonia required when the anticipated quantity of NOx changes with load and speed.) Phase 1 Report Grant N-12 Page 9/15 Of potential concern is ammonia slip, where some of the reducing agent escapes the exhaust system into the atmosphere. The major logistical problems are that an additional storage tank is required on each vehicle, and a refilling infrastructure is required. The promise of significant reductions in NOx means that SOI can be advanced again for improved efficiency, resulting in better fuel economy than other approaches. Particulates are also improved with this approach. However, in certain applications the temperature of the exhaust stream may be too low for effective operation of the catalytic reaction. In those cases an additional heat source may be required, either a burner or an electric heating element. Either of these options will result in a reduction of fuel economy of the engine. There is potentially a 6% improvement in fuel economy, although this is offset by the cost of urea. One study [13] found that urea must cost less that $1.50 per gallon for there to be an equivalent fuel economy benefit using an SCR. A schematic of a system developed by Bosch is shown below. Figure 6: A commercial SCR system with a DOC as shown in [14] LNTs LNTs adsorb NOx and oxygen during lean operation modes, then during occasional rich operation the NOx is catalyzed to nitrogen. Sulfur in the exhaust causes performance degradation over time [12] so that periodic desulfation is required. There are some operational issues with these NOx adsorbers for the regeneration phase. Either a dual-leg layout is needed where one of the two legs may be regenerated while the other continues to adsorb NOx, or a single-leg layout requires periodic injection of diesel fuel into the exhaust to facilitate the reduction process. Using fuel as a reductant has a substantial fuel economy penalty. Schematics of the two approaches are shown below. Phase 1 Report Grant N-12 Page 10/15 Figure 7: Single and double leg LNT systems from [10] DPF Technology This consists of a closed filter that physically traps particulates then oxidizes them. The oxidation process requires a particular temperature range, which is often controlled by a burner, impacting fuel economy. Some filters are catalytic, reducing the fuel economy impact. They also trap ash from combustion of engine oil, which cannot be oxidized. Consequently they require periodic cleaning. DOC Technology This approach is similar to the use of catalyst in automotive applications, except that it does not reduce NOx emissions due to the oxygen-rich environment. These oxidize unburned hydrocarbons and carbon monoxide as well as some particulates (although not as effectively as DPFs for the latter.) They are passive devices with no maintenance required. The following table shows a summary of the effectiveness of both in-cylinder and aftertreatment approaches on emissions, including a range of costs for retrofit situations, based on the references given at the end of this report. Phase 1 Report Grant N-12 Page 11/15 Table 1: NOx reduction alternatives at a glance Technology NOx Reduction PM Reduction HC Reduction CO Reduction Effect on Fuel Economy Estimated Cost 1 VIT Up to 50% - - Less than fixed retard, may even be neutral $7,400 EGR (cooled) 40 – 60% Increased Increased 1 – 4% worse $13,000 – 15,000 SCR 60 – 90% Could increase 50% Could increase 300% 20 – 30% 99% 76% $10,500 - $50,000 LNT >80% - - - Possibly up to 6% improved, but have reductant costs/consumption 3 – 7% worse DOC - 10 – 50% 50% 40% - $500 - $2,000 DPF - 80 – 90% 85% 85% Depending on heat source for $5,000 - $10,000 2 activation 1 2 Estimates based on 10 – 15 L heavy duty diesel engine Requires ULS diesel Phase 1 Report Grant N-12 Page 12/15 $5,000 - $10,000 The following diagram from [7] gives a good comparison of EGR, SCR and NOx adsorber approaches on other performance issues. As noted above, the advantage that SCRs have with fuel economy is somewhat negated by the need to recharge the reductant tank periodically. The alternative approach of on-board reforming to provide the reductant reduces this advantage somewhat. Figure 8: Performance effects of different NOx reducing technologies from [7] Another potential NOx reducing technology is that of the lean NOx catalyst. Unfortunately to date there have been no successful, durable lean NOx catalysts that can reduce NOx under the typical oxygen-rich environment of a diesel engine exhaust. Even if one is found, there is expected to be a fuel economy penalty of 3% or more due to the addition of a suitable reductant [10, 12]. Phase 1 Report Grant N-12 Page 13/15 Summary of Retrofits Each of the technologies listed above has a number of advantages and disadvantages. The table below is intended to offer a summary of the pros and cons of applying these systems as retrofits to older diesel engines for the purposes of NOx reduction. Table 2: Pros and cons of different NOx reduction alternatives Technology Advantages Mechanical VIT Cooled EGR Transparent to user Constant over engine life Little impact on fuel economy Effective NOx reduction No user intervention required SCR NOx reduction high Potentially best fuel economy LNT Potentially high NOx reduction DOC Low cost control of HC, CO, PM Reduces PM with timing retard DPF Disadvantages May be invasive in engine May require higher injection pressures PM, HC, CO worse Additional engine wear Higher PM during transients Hardware packaging Additional cooling system demands Requires reductant User intervention required Hardware packaging Expensive High fuel economy penalty Hardware packaging Does nothing for NOx Does nothing for NOx Requires heat source Hardware packaging Summary A low-cost VIT solution may be a very attractive approach for older diesel engines to achieve a 25% reduction in NOx emissions. While there are other approaches that reduce NOx further they appear to be substantially more expensive, and in some cases require user intervention. Further VIT appears to offer very good fuel economy results for the cost, an issue that is sure to be of concern to users of older engines who will see no economic benefit to lower NOx emissions. Phase 1 Report Grant N-12 Page 14/15 References 1) 2) 3) 4) 5) 6) 7) 8) 9) 10) 11) 12) 13) 14) V. O. Markworth, S. G. Fritz, G. R. Cataldi, “The Effect of Injection Timing Enhanced Aftercooling, and Low-Sulfur, Low-Aromatic Diesel Fuel on Locomotive Exhaust Emissions,” Transactions of the ASME, pp. 488 – 495, Vol. 114, July 1992 R. Stradling, P. Gadd, M. Signer, C. Operti, “The Influence of Fuel Properties and Injection Timing on the Exhaust Emissions and Fuel Consumption of an Iveco Heavy-Duty Diesel Engine,” SAE Paper 971635, 1997. D. A. Kouremenos, D. T. Hountalas, K. B. Binder, A. Raab, M. H. Schnabel, “Using Advanced Injection Timing and EGR to Improve DI Diesel Engine Efficiency at Acceptable NO and Soot Levels,” SAE Paper 2001-01-0199, 1999. P. Lauvin, A. Loffler, A. Schmitt, W. Zimmermann, W. Fuchs, “Electronically Controlled High Pressure Unit Injector System for Diesel Engines,” SAE Paper 911819, 1991. R. C. Yu, S. M. Shahed, “Effects of Injection Timing and Exhaust Gas Recirculation on Emissions from a D.I. Diesel Engine,” SAE Paper 811234, 1981. J. M. Desantes, J. V. Pastor, J. Arregle, S. A. Molina, “Analysis of the Combustion Process in a EURO III Heavy-Duty Direct Injection Diesel Engine,” ASME J. Eng. Gas Turbines Power, 124, pp. 636-644 M. Schittler, “State-of-the-Art and Emerging Technologies,” 9th Diesel Engine Emissions Reductions Conference, August 2003 “Exhaust Gas Recirculation,” DieselNet Technology Guide, Engine Design for Low Emissions, 2005 “Overview of Clean Diesel Requirements and Retrofit Technology Options,” F. J. Acevedo, Michigan Clean Fleet Conference, March 2006 G. Weller, “EPA Engine Implementation Workshop – 6/7 August 2003, 2007 Technology Primer,” Presentation by Ricardo “Diesel Powered Machines and Equipment: Essential Uses, Economic Importance and Environmental Importance,” Diesel Technology Forum, June 2003 H. Hu, J. Reuter, J. Yan, J. McCarthy Jr., “Advanced NOx Aftertreatment System and Controls for On-Highway Heavy Duty Diesels,” SAE Paper 200601-3553, 2006 R. Krishnan, T. J. Tarabulski, “Economics of Emission Reduction for HeavyDuty Trucks,” DieselNet Technical Report, January 2005 W. Addy Majewski, “SCR Systems for Mobile Engines,” DieselNet Technical Report, 2006 Phase 1 Report Grant N-12 Page 15/15 11.2. Appendix 2: Poisoning in SCR Systems Final Report NTRD Program N-16 Woodward Page 68 ENGINE SYSTEMS, AFTERTREATMENT SYSTEMS GROUP Phase 1: Literature Study Contract# N-16 Project# 89016 March 11, 2008 authored by Dan Mastbergen Poisoning in SCR Systems 1 ABSTRACT In this study, a review of SCR degradation mechanisms has been performed to assess longterm SCR system efficiency. This study has also focused on the specific issue of hydrocarbon poisoning which plays a larger role in a fuel-fired heater-SCR system. There have been a number of papers published in the past few years regarding SCR performance degradation as more long-term field/lab experience comes in. Reductions in conversion efficiency can come from thermal aging, poisoning, and hydrocarbon adsorption/coking. Typical causes of poisoning in after-treatment systems come from minerals in the fuel or oil such as sulfur, potassium, calcium, zinc [2], and urea related by-products [3][4]. 2 BACKGROUND In recent years, the ground level ozone concentrations in a number of US cities have exceeded EPA limits. This results in negative health effects for the residents, and severe fines for the city governments. In the state of Texas, four cities have exceeded the ozone levels several times. The key contributors to ozone formation are NOx, hydrocarbons, and sunlight. Emissions levels for new engines being produced over the next decade will have to reduce NOx levels by roughly an order of magnitude (depending on engine size). However, many engines in fleet vehicles (delivery trucks, trash haulers, etc) will not be replaced by these newer engines for some time. Because these vehicles are significant contributors to NOx within the city, a retrofit technology is required to bring these cities into compliance. Currently the most efficient and cost effective means for lowering NOx is Selective Catalytic Reduction (SCR). SCR systems have been implemented commercially in Europe now for two years, with positive results. For a successful retrofit, the SCR system must maintain a high conversion efficiency long enough to make a contribution to NOx reduction within that city. Typically SCR systems are very efficient at reducing NOx, however, the conversion efficiency is very temperature dependant. In order to exceed 80% conversion efficiency, the exhaust temperature must be above 300-400 C (depending on the catalyst material). For inner city vehicles following stop-and-go driving cycles, the exhaust temperature may rarely, if ever, exceed these temperatures. Therefore, for these applications it is also necessary to have an auxiliary exhaust heater in-line to increase the exhaust temperatures. Currently Woodward Governor is developing an exhaust heater capable of heating exhaust temperatures at idle up to 650 C. The inclusion of a heater into SCR systems is a newer development, since most systems to date have been installed on on-highway vehicles where exhaust temperatures are typically high. As a part of this study the issue of hydrocarbon poisoning has received focused attention since additional hydrocarbon emissions can be emitted from the fuel-fired heater. 3 THERMAL AGING Thermal aging of the catalyst can have a significant effect on conversion efficiency, special high temperature cycles. The main cause of thermal deactivation is metal sintering and 1/5 ENGINE SYSTEMS, AFTERTREATMENT SYSTEMS GROUP Phase 1: Literature Study Contract# N-16 Project# 89016 March 11, 2008 authored by Dan Mastbergen dealumination [6]. The effect of thermal aging on catalyst performance is very complex and hard to predict since it depends on the time-temperature history of the substrate. It also depends largely on the substrate material. High temperature Zeolite catalysts have much higher temperature capability than Vanadium, however, they also require higher temperature operation to be efficient. Cavataio et al. performed an extensive study of thermal aging on different catalyst materials at varying temperatures[5]. The majority of the work was on Cu-zeolites and Fe-zeolites. The Cu-zeolite showed an approximately 5% reduced (peak) efficiency at 120k miles, while the Fezeolite showed almost no drop in performance at 120k miles (120k miles simulated as 64 hours at 670 C). The same test was performed after aging at a lower temperature (550C) for 2000 hours. In this test the Cu-zeolite showed a roughly 15% reduction in peak efficiency while the Fe-zeolite again showed negligible reductions in peak efficiency. An additional study was performed by exposing the catalyst to high temperatures for one hour. The reductions in maximum efficiency for the Cu-zeolite were around 10% at 800C, 60% at 900 C, and 80% at 950 C. For the Fe-zeolite the reduction in maximum efficiency was 1% at 800 C, 5% at 900 C, and 6% at 950 C. Houel et al. performed a comparison of Cu-Zeolite and Ag/Alumina. The two substrates were aged at 700 C for 72 hours. The peak conversion efficiency in the Ag/alumina system shifted from 400 C to 300c, and was reduced from 90% to 60%. The Cu-zeolite peak efficiency was reduced from 80% to 30%. Although these results are specific to the catalyst material used for the test, it serves as a good example of the time/temperature sensitivity on SCR catalyst aging. 4 POISONING 4.1 SULFUR POISONING Unlike other after-treatment devices, SCR systems are fairly insensitive to sulfur poisoning. Sulfur in the fuel can result in ammonium sulfate that can foul the SCR catalyst. This reduces the low temperature (< 300 C) conversion efficiency. Fortunately, after bringing the substrate up to high temperatures (650 C) the sulfur poisoning is purged and the performance is returned to normal[1][5]. In general, the effects of sulfur poisoning are less detrimental than thermal aging, especially on the Cu-zeolite system[6]. However, Houel et al. found that the effect of sulfur poisoning is very detrimental on the Ag/Alumina system. No data was shown as to whether this damage could be reversed by a thermal regeneration. 4.2 OIL DERIVED POISONING Poisoning can also be caused by minerals contained in the motor oil that make it into the catalyst such as Potassium, Calcium, and Zinc[2]. Trace amounts of these substances were observed on the catalyst after 120k miles of service. However, the contribution of these poisons to the overall deactivation could not be separated from the thermal aging effect. 4.3 UREA BYPRODUCT POISONING It is also possible for deposits of urea to build up on the catalyst and impact conversion efficiency. This can occur if the SCR system is run at low temperatures and the urea dosing system does not sufficiently atomize the urea solution. The result is a build up of crystallized 2/5 ENGINE SYSTEMS, AFTERTREATMENT SYSTEMS GROUP Phase 1: Literature Study Contract# N-16 Project# 89016 March 11, 2008 authored by Dan Mastbergen urea on the face of the catalyst that will plug the channels, resulting in reduced efficiency. At temperatures less than 250 C large deposits of urea were formed (when dropping aqueous urea directly on the substrate). It was also found that once the substrate was heated above 350 C the deposits would be vaporized[4]. 5 HYDROCARBON EFFECTS The issue of hydrocarbon poisoning is very important in a fuel-fired heater-SCR system since there is the possibility of much higher hydrocarbon emissions entering the SCR system than with a stand alone SCR. The effects hydrocarbons can be broken into three regimes: instantaneous effects, short-term effects, and long-term effects. During times when the SCR is in operation (dosing urea), the presence of hydrocarbons can reduce the efficiency of the SCR system. It should be noted that hydrocarbons can act as the reducing agent in place of urea/NH3, however, the efficiency of hydrocarbon reduction is lower than for urea/NH3 [5][6]. In fact, Hoeul et al. experimented with using diesel fuel as the reducing agent and showed conversion efficiencies up to 60% (above 450 C). However, at lower temperatures (<300) the conversion efficiency using diesel fuel is less than 10 %[6]. When hydrocarbons are present in an SCR system made to operate on urea/NH3, the hydrocarbons directly interfere with the reaction of NH3, reducing the overall conversion efficiency. Cavatio et al. showed that the conversion efficiency of a Cu-zeolite catalyst at 300 C dropped from 95% to 85% with 225 ppm Benzene and to 50% with 50 ppm n-Decane. At 200 C the efficiency dropped from 80% to 75% with 225 ppm Benzene and to 30% with 50 ppm n-Decane[5]. This reduced efficiency can also lead to increased ammonia slip since the hydrocarbons are blocking the reaction of the ammonia. Gieshoff et al showed the conversion efficiency on a Vanadia based catalyst with varying concentrations of n-decane. Above 400 C there is negligible effect of 30 ppm n-Decane. Below 300 C the conversion efficiency is roughly cut in half for 30 ppm n-Decane. Hydrocarbons can also lead to medium-term deactivation if they are adsorbed to the substrate, or if coking occurs. This would cause the catalyst to continue to operate at a reduced efficiency until the exhaust temperature got high enough to free and burn the hydrocarbons. The temperature required for regeneration is around 400 C[5]. At this temperature the recovery was nearly instantaneous. Houel et al also saw a recovery from coking at 500 C[6]. Within the sources reviewed here, there has been no mention of long term poisoning effects of hydrocarbons, assuming they can be periodically purged completely from the system. Any mineral left behind (such as sulfur) would be present in the exhaust stream regardless of what form the hydrocarbons are in. 6 SUMMARY There are many potential causes for reduced efficiency in SCR systems including thermal aging, sulfur poisoning, oil-derived compound poisoning, urea crystallization, and hydrocarbon poisoning. The most severe and most permanent is thermal aging, however, this can be 3/5 ENGINE SYSTEMS, AFTERTREATMENT SYSTEMS GROUP Phase 1: Literature Study Contract# N-16 Project# 89016 March 11, 2008 authored by Dan Mastbergen minimized by selecting the appropriate material for the application and by not exceeding “maximum” thresholds. Reductions in efficiency from thermal aging should be less than 15% per 120k miles for a well designed system. The effect of sulfur poisoning is significant for nonzeolite catalysts. However, poisoning due to sulfur can be reversed by regenerating the catalyst. Poisoning by oil-derived minerals has also been observed, but its effects are not well quantified. Poisoning by crystallized urea is possible at low temperatures, but is quickly vaporized once the temperature exceeds 350 C. Hydrocarbons can reduce the instantaneous efficiency by inhibiting the reaction with ammonia. This could lead to increased ammonia slip from the catalyst. The substrate can also temporarily absorb hydrocarbons for continued lower efficiency. Once again, this type of poisoning can be reversed by increasing the temperature above 400 C. Hydrocarbons do not appear to contribute to any long-term degradation. 7 REFERENCES [1] Majewski a, “Selective Catalytic Reduction” on www.dieselnet.com 2005 [2] Cheng Y, Xu L, Hanngas J, Jagner M, Lambert C, “Laboratory Postmortem Analysis of 120k mi Engine Aged Urea SCR Catalyst” SAE Publication 2007-01-1579 [3] Kim J, Cheng Y, Patterson J, Laing P, Lambert C, “Modeling Study of Urea SCR Catalyst Aging Characteristics” SAE Publication 2007-01-1580 [4] Xu L, Watkins W, Snow R, Graham G, McCabe, Lambert C, Carter R, “Laboratory and Engine Study of Urea-Related Deposits in Diesel Urea-SCR After-Treatment Systems” SAE Publication 2007-01-1582 [5] Cavatio G, Girard J, Patterson J, Montreuil C, Cheng Y, Lambert C, “Lab Testing of Urea-SCR Formulations to Meet Tier 2 Bin 5 Emissions” SAE Publication 2007-01-1575 [6] Houel V, James D, “A Comparison of the Activity and Deactivation of Ag/Al2O3 and Cu/ZSM-5 for HC-SCR Under Simulated Diesel Exhaust Emission Conditions” Journal of Catalysis, Feb 2005 Vol 230(1), p. 150-157 [7] Pieterse J, Top H, “Selective Catalytic Reduction of NOx in Real Exhaust Gas of Gas Engines Using Unburned Gas: Catalyst Deactivation and Advances Toward Long Term Stability” Chemical Engineering Journal, July 2006 Vol 120, issue 1-2, p. 17-23 [8] Block M, Clark N, Wayne S, Nine R, Miller W, “An Investigation into the Emissions Reduction Performance of an SCR System Over Two Years IN-Use Heavy-Duty Vehicle Operation” SAE Publication 2005-01-1861 [9] Gieshoff J, et al “ Improved SCR Systems for Heavy Duty Applications” SAE Publication 2000-01-0189 4/5 ENGINE SYSTEMS, AFTERTREATMENT SYSTEMS GROUP Phase 1: Literature Study Contract# N-16 Project# 89016 March 11, 2008 authored by Dan Mastbergen 5/5 11.3. Appendix 3: SwRI Testing Report of Woodward’s Burner System Final Report NTRD Program N-16 Woodward Page 74 IMPROVING DIESEL SCR LOW TEMPERATURE PERFORMANCE USING A BURNER SYSTEM ― PROOF-OF-CONCEPT EVALUATION FINAL REPORT SwRI® Project No. 03.14560 Prepared for: Woodward Governor Company 3800 North Wilson Avenue Loveland, CO 80538 Prepared by: Qilong Lu Senior Research Engineer December 16, 2008 S A N A N T O N I O , HOUSTON, TEXAS ! T E X A S WASHINGTON, DC TABLE OF CONTENTS Page 1.0 INTRODUCTION .............................................................................................................. 1 2.0 EXPERIMENTAL DETAILS AND TEST PROCESS...................................................... 2 2.1 Test Engine ..................................................................................................................... 2 2.2 Test Fuel and Lube Oil ................................................................................................... 3 2.3 Test Procedures............................................................................................................... 3 2.4 Installation of Woodward’s Aftertreatment System ....................................................... 6 2.5 Test Engine Instrumentation ........................................................................................... 7 3.0 EMISSION TEST RESULTS AND ANALYSIS .............................................................. 8 iii TABLE OF FIGURES Page Figure 1. Photograph of DDC Series-60, 12.7L Engine Installed in Test Cell.............................. 3 Figure 2. FTIR System Setup......................................................................................................... 5 Figure 3. Schematic of CVS Emissions Sampling System............................................................ 5 Figure 4. Test Parameter Denotation of Special Measurement Required by Woodward.............. 6 Figure 5. Installation of the Woodward Aftertreatment System.................................................... 7 Figure 6. SCR Inlet Temperature Comparison ............................................................................ 13 Figure 7. NO2/NOx Ratio Comparison ....................................................................................... 14 Figure 8. SCR NOx Reduction Efficiency and NH3 Slip............................................................ 15 iv LIST OF TABLES Page Table 1. DDC Series-60, 12.7L Engine Specifications ................................................................. 2 Table 2. Final Test Points .............................................................................................................. 8 Table 3. Diluted Tailpipe Measurement Without Burner Operation ............................................. 9 Table 4. FTIR Measurement Before and After SCR Catalyst Without Burner Operation .......... 10 Table 5. Diluted Tailpipe Measurement With Burner Operation ................................................ 11 Table 6. FTIR Measurement Before and After SCR Catalyst With Burner Operation ............... 12 v 1.0 INTRODUCTION The project was conducted at Southwest Research Institute (SwRI) on behalf of Woodward Governor Company (Woodward). The objective of this program was to evaluate the effectiveness of the Woodward burner to improve an SCR system performance measured through its NOx reduction efficiency, especially at low exhaust temperatures. SwRI conducted this project on a 1998 model year, Detroit Diesel Series-60, 12.7L, diesel engine. ULSD fuel was used for all the emissions tests. NO, NO2 and NH3 upstream and downstream of the SCR catalyst were measured by a FTIR analyzer. Regulated emissions of HC, CO, NOx, and PM were also measured for each test by a dilute constant volume sampling (CVS) system. This work was performed under SwRI Project No. 03-14560. The project leaders were Dr. Magdi Khair and Dr. Qilong Lu. This final report contains experimental details, test procedures, installation of test engine and Woodward’s aftertreatment system, and emission test results and analysis. 1 2.0 EXPERIMENTAL DETAILS AND TEST PROCESS This section of the report provides an overview of the equipment, fuel, and test procedures used during the project. 2.1 Test Engine The test engine was a 1998 model year, Detroit Diesel Series-60, 12.7L, diesel engine. The engine’s specifications are given in Table 1. A side view of the engine installed in the test cell is given in Figure 1. Table 1. DDC Series-60, 12.7L Engine Specifications Item Description/Specification Engine Type In-line, 6-Cylinder Engine Model DDC Series-60, 12.7 L Model Year 1998 Serial Number 06R0422316 Engine Displacement 12.7 L/775 CID Rated Speed 1800 rpm Rated Power 405 hp Peak Torque Speed 1200 rpm Peak Torque 1625 lb-ft Aspiration Turbocharged - Aftercooled Fuel Injection System EUI System 2 Figure 1. Photograph of DDC Series-60, 12.7L Engine Installed in Test Cell 2.2 Test Fuel and Lube Oil Emission tests in this project were conducted using USLD fuel. The fuel was coded as EM-6406-F at SwRI. The lube oil used was Shell Rotella T Multi-Grade Triple Protection SAE 15W-40 API CJ-4 diesel engine oil. 2.3 Test Procedures The project objective was to evaluate the effectiveness of the Woodward burner to improve a SCR system performance at low exhaust temperatures. The test procedures to achieve the project goal were described as follows: 1, SwRI installed the test engine and Woodward’s aftertreatment system in a test cell equipped with a dilution tunnel. Preliminary verification of engine performance was carried out. 2, Experiments were conducted to determine final test points by changing engine speed from idle to 1800rpm in 200 rpm increments and load from 0 to rated in 200 lb-ft increments. The temperature downstream of Woodward heat exchanger was set as the selection criterion. 3 3, SwRI provided emission test benches. NOx emissions such as NO and NO2 and ammonia (NH3) before and after the SCR catalyst were measured by a Fourier transform infrared (FTIR) system as shown in Figure 2. Regulated emissions of HC, CO, NOx, and PM were measured using a CVS system. Figure 3 shows a schematic diagram of the CVS system. In the system, the exhaust gases are diluted with conditioned air to maintain a constant total flow rate under all engine operating conditions. A portion of the diluted exhaust gases is taken for emissions measurement. HC was measured using a heated flame ionization detector (FID). CO and CO2 were determined by a non-dispersive infrared analyzer (NDIR). NOx was measured via chemiluminescence instruments (CLD). PM levels were determined by collecting particulate matter on 90 mm Pallflex filters which were weighed before and after each test mode after conditioning in a temperature and humidity controlled environmental chamber. 4, Test parameters denoted in Figure 4 were documented for all the final test points. 5, Woodward burner system and Tenneco Elim-NOx SCR system were calibrated by Woodward and Tenneco personnel for operation with the test engine. 6, Initially, the Woodward burner system was not operated. SCR dosing system was controlled by Tenneco Elim-NOx controller. Emissions were measured when the engine and aftertreatment system reached thermal equilibrium for all the final test points. 7, Subsequently, the Woodward burner system was operated. SCR inlet temperature was increased to 300 °C and maintained during emissions measurement for each test point. SCR dosing system was controlled by its controller. Emissions were measured when the engine and aftertreatment system reached thermal equilibrium for all the final test points. 4 Heated Sampling Lines FTIR Console Switch Valve Figure 2. FTIR System Setup Aftertreatment System Note: NO Analyzer was not used in this project. Figure 3. Schematic of CVS Emissions Sampling System 5 10 8 1 2 3 4 5 6 9 7 1, Turbo Outlet Temp. 2, Heat Exchanger Inlet Temp. 3, Heat Exchanger Outlet Temp. /Burner Inlet Temp. 4, Burner Outlet Temp. /DPF Inlet Temp. 5, DPF Outlet Temp. 6, SCR Inlet Temp. 7, SCR Outlet Temp. 8, SCR Inlet FTIR Measurement 9, SCR Outlet FTIR Measurement 10, Diluted Tailpipe Emission Measurement Figure 4. Test Parameter Denotation of Special Measurement Required by Woodward 2.4 Installation of Woodward’s Aftertreatment System SwRI received the Woodward’s aftertreatment system which consisted of an exhaust heat exchanger, a 10" Woodward burner, a DPF, and a SCR system as shown in Figure 4. Figure 5 shows the aftertreatment system installation at SwRI. 6 Airless Urea Injector SCR FTIR Sampling Probes Exhaust Pipe to CVS System DPF Burner Heat Exchanger Figure 5. Installation of the Woodward Aftertreatment System 2.5 Test Engine Instrumentation For each test engine used for emissions measurement, SwRI provides the engine with an extensive list of instrumentation to monitor test engine performance. In this project, the test cell was equipped with thermocouples and pressure transducers for monitoring coolant inlet and outlet temperatures, oil temperature, intake air temperature, fuel temperature, exhaust temperature, intercooler inlet and outlet temperatures, inlet air restriction, exhaust back pressure, boost pressure, intercooler restriction, oil pressure, etc. 7 3.0 EMISSION TEST RESULTS AND ANALYSIS After the installation of the test engine, its performance at rated as well as peak torque was validated. The rated power was 420 bhp at 1800rpm and the peak torque was 1612 lb-ft at 1200rpm. Both observed rated power and peak torque agreed well with the engine performance specifications. By changing engine speed from idle to 1800rpm in 200 rpm increments and load from 0 to rated in 200 lb-ft increments, sweep experiments were conducted in order to determine final test points for the SCR system performance evaluation. By considering lower exhaust temperature into the SCR catalyst and wider engine operating range, Woodward engineers determined the 21 modes listed in Table 2 as the final speed and load points for the test matrix. Table 2. Final Test Points Mode No. Speed (rpm) Load (lb-ft) 1 1800 20 109 2 1600 20 99 3 1400 20 89 4 1200 20 78 5 1000 20 69 6 700 20 59 7 1800 200 188 8 1600 200 167 9 1400 200 148 10 1200 200 135 11 1000 200 117 12 1800 400 250 13 1600 400 235 14 1400 400 216 15 1200 400 195 16 1000 400 172 17 1600 600 295 18 1600 500 268 19 1400 600 270 20 1200 600 258 21 1000 800 280 Temp. after Heat Exchanger (°C) Following the determination of the test matrix and the calibrations of the burner system and the SCR system, SwRI conducted emissions measurement for all those 21 test points. Tests were firstly performed when the burner system was not operated while the SCR dosing system was controlled by its own controller. Tables 3 and 4 summarize the test results of diluted tailpipe 8 measurement and FTIR measurement before and after SCR catalyst. And then, tests were conducted when the burner system was triggered and SCR inlet temperature was increased to 300 °C. Emission test results are tabulated in Tables 5 and 6. Table 3. Diluted Tailpipe Measurement Without Burner Operation Temperature Distribution (°C) Mode No. Speed (rpm) Load (lb-ft) Diluted Tailpipe Measurement (g/hp-hr) Turbo Outlet HX Inlet HX Outlet Burner Outlet DPF Outlet SCR Inlet SCR Outlet HC CO NOx PM CO2 1 1800 20 162 156 109 NA 100 100 99 5.04 84.45 40.61 0.113 3965 2 1600 20 149 144 99 NA 91 90 90 4.56 59.38 27.51 0.365 2765 3 1400 20 139 134 89 NA 82 82 81 4.63 48.79 24.15 0.015 2285 4 1200 20 125 120 78 NA 73 74 72 6.31 55.54 25.25 0.092 2321 5 1000 20 114 109 69 NA 63 64 63 4.23 39.75 34.60 0.165 2144 6 700 20 109 103 59 55 52 55 54 0.71 14.51 21.34 0.027 1240 7 1800 200 279 268 188 NA 168 163 163 0.22 1.71 7.36 0.035 598 8 1600 200 258 246 167 NA 149 145 145 0.14 2.02 7.13 0.004 584 9 1400 200 239 228 148 NA 132 130 128 0.15 2.17 8.48 0.006 569 10 1200 200 234 221 135 NA 118 115 114 0.15 2.00 8.82 0.009 548 11 1000 200 216 203 117 NA 102 102 100 0.15 1.70 12.05 0.013 546 12 1800 400 360 344 250 NA 223 216 215 0.07 0.15 6.08 0.008 512 13 1600 400 354 336 235 NA 209 202 201 0.03 0.05 5.42 0.005 496 14 1400 400 342 324 216 NA 191 185 184 0.02 0.06 6.14 0.001 484 15 1200 400 329 309 195 NA 172 168 166 0.06 0.34 6.59 0.002 478 16 1000 400 319 296 172 NA 149 146 144 0.04 0.31 10.10 0.004 466 17 1600 600 432 410 295 NA 261 251 251 0.02 0.10 5.68 0.002 470 18 1600 500 396 377 268 NA 239 233 232 0.01 0.01 5.59 0.001 479 19 1400 600 420 395 270 NA 235 226 226 0.01 0.01 6.30 0.000 459 20 1200 600 423 395 258 NA 223 215 215 0.01 0.00 6.17 0.000 457 21 1000 800 495 454 280 NA 236 222 224 0.01 0.01 7.77 0.000 453 9 Table 4. FTIR Measurement Before and After SCR Catalyst Without Burner Operation SCR Inlet (ppm) Mode No. Speed (rpm) SCR Outlet (ppm) Load (lb-ft) NO NO2 NOx NO2/NOx(%) NH3 NO NO2 NOx NO2/NOx (%) NH3 1 1800 20 150 60 210 28.6 0 153 38 191 19.9 0 2 1600 20 144 59 202 29.2 0 137 42 179 23.5 0 3 1400 20 134 60 194 30.9 0 136 45 181 24.9 0 4 1200 20 129 54 183 29.5 0 131 40 171 23.4 0 5 1000 20 191 52 243 21.4 0 191 39 230 17.0 0 6 700 20 235 41 276 14.9 4.9 211 16 227 7.0 4.7 7 1800 200 479 31 511 6.1 0 500 1.6 502 0.3 0 8 1600 200 435 48 483 9.9 0 448 30 478 6.3 0 9 1400 200 498 59 557 10.6 0 505 45 549 8.2 0 10 1200 200 559 59 618 9.5 0 562 48 610 7.9 0 11 1000 200 749 63 812 7.8 0 752 55 807 6.8 0 12 1800 400 652 33 685 4.8 1 671 0 671 0.0 0 13 1600 400 600 20 620 3.2 0 613 1 614 0.2 0 14 1400 400 702 9 711 1.3 0 711 1 712 0.1 0 15 1200 400 754 17 771 2.2 0 747 16 763 2.1 0 16 1000 400 1202 46 1248 3.7 0 1210 38 1248 3.0 0 17 1600 600 791 45 836 5.4 2 815 1 816 0.1 0 18 1600 500 687 28 715 3.9 0 698 15 713 2.1 0 19 1400 600 903 32 935 3.4 0 917 22 939 2.3 0 20 1200 600 933 23 956 2.4 0 940 16 956 1.7 0 21 1000 800 1489 38 1528 2.5 0 1491 29 1520 1.9 0 10 Table 5. Diluted Tailpipe Measurement With Burner Operation Temperature Distribution (°C) Mode No. Speed (rpm) Load (lb-ft) Diluted Tailpipe Measurement (g/hp-hr) Turbo Outlet HX Inlet HX Outlet Burner Outlet DPF Outlet SCR Inlet SCR Outlet HC CO NOx PM CO2 1 1800 20 168 162 115 315 321 307 308 0.17 1.17 40.12 0.096 6927 2 1600 20 159 153 107 313 319 306 305 0.04 0.29 2.77 0.059 3401 3 1400 20 143 137 93 315 320 304 303 0.08 0.33 2.72 0.092 4556 4 1200 20 132 126 83 313 320 301 300 0.01 0.38 1.31 0.098 3593 5 1000 20 114 109 70 315 319 297 296 0.00 0.49 1.93 0.344 5785 6 700 20 104 98 59 321 320 291 290 0.00 0.53 0.13 0.273 4660 7 1800 200 279 267 189 318 318 309 305 0.00 0.04 0.22 0.010 770 8 1600 200 262 251 172 317 318 308 304 0.00 0.04 0.54 0.021 761 9 1400 200 241 228 150 317 318 305 301 0.00 0.06 0.91 0.003 779 10 1200 200 230 217 134 317 318 303 300 0.00 0.06 1.04 0.003 770 11 1000 200 220 207 120 319 319 301 297 0.00 0.05 3.77 0.005 766 12 1800 400 360 344 245 319 318 310 304 0.00 0.02 0.44 0.007 583 13 1600 400 357 340 235 319 318 308 304 0.00 0.02 0.25 0.004 572 14 1400 400 347 328 215 318 318 306 301 0.00 0.02 1.11 0.001 569 15 1200 400 334 313 193 319 318 304 299 0.00 0.03 1.27 0.002 575 16 1000 400 316 294 168 321 319 302 299 0.00 0.01 4.39 0.146 576 17 1600 600 428 407 294 319 318 309 304 0.00 0.01 1.27 0.000 506 18 1600 500 398 378 267 319 318 309 303 0.00 0.01 0.47 0.001 532 19 1400 600 425 400 275 319 318 308 302 0.01 0.09 1.43 0.007 506 20 1200 600 419 392 252 319 319 305 301 0.00 0.00 2.01 0.000 511 21 1000 800 409 377 223 319 319 303 297 0.00 0.03 2.96 0.004 494 11 Table 6. FTIR Measurement Before and After SCR Catalyst With Burner Operation SCR Inlet (ppm) Mode No. Speed (rpm) SCR Outlet (ppm) NO NO2 NOx NO2/NOx (%) NH3 NO NO2 NOx NO2/NOx (%) NH3 NOx Conv. Efficiency (%) Torque (lb-ft) 1 1800 20 90 127 217 58.5 59 15 36 57 63.2 2.4 74 2 1600 20 91 127 218 58.3 68 11 37 48 77.1 2.6 78 3 1400 20 82 124 206 60.2 81 7 13 20 65.0 2.0 90 4 1200 20 79 131 210 62.4 97 6 6 12 50.0 2.6 94 5 1000 20 70 136 206 66.0 129 7 2 9 22.2 2.9 96 6 700 20 62 153 215 71.2 165 7 1 8 12.5 6.8 96 7 1800 200 199 239 438 54.6 196 8 38 46 82.6 3.5 89 8 1600 200 184 229 413 55.4 179 8 38 46 82.6 6.0 89 9 1400 200 213 273 486 56.2 188 9 63 72 87.5 6.0 85 10 1200 200 220 289 509 56.8 194 8 72 80 90.0 5.5 84 11 1000 200 291 358 649 55.2 183 53 168 221 76.0 1.7 66 12 1800 400 352 278 630 44.1 252 28 3 30 10.0 10.6 95 13 1600 400 291 268 559 47.9 283 17 8 25 32.0 6.3 96 14 1400 400 325 278 603 46.1 220 66 65 131 49.6 8.2 78 15 1200 400 347 332 679 48.9 299 45 64 109 58.7 6.4 84 16 1000 400 582 446 1028 43.4 254 235 176 411 42.8 6.6 60 17 1600 600 469 266 735 36.2 158 163 13 176 7.4 14.3 76 18 1600 500 381 279 660 42.3 309 220 51 271 18.8 9.8 59 19 1400 600 440 419 860 48.7 321 118 103 221 46.6 20.7 74 20 1200 600 830 465 1295 35.9 361 435 143 578 24.7 13.1 55 21 1000 800 758 613 1371 44.7 496 305 164 469 35.0 20.9 66 12 The weight factor of each test mode was considered as the same for this emission analysis. When the SCR inlet temperature was not regulated by the burner, the total NOx emission results of the 21 modes was considered as a baseline. The NOx baseline emission was 283.14 g/hp-hr, which was the sum of all modal NOx contribution listed in Table 3. When the burner was operated to maintain the SCR inlet temperature at the level of 300 °C, the total NOx emission was reduced to 71.05 g/hp-hr, which was the sum of all modal NOx contribution listed in Table 5. Thus, the overall SCR NOx reduction efficiency was 74.9 % with the aid of the burner. SCR inlet temperature of each test mode was summarized and plotted in the Figure 6. With the exception of Mode 17, all other SCR inlet temperatures were below 250 °C and 18 modes were below 225 °C. When the burner was operated, the SCR inlet temperatures of all the 21 modes were well controlled at 300 °C within ±3.5% steady-state errors. SCR Inlet Temperature 400 Temp. Not Regulated By Burner Temp. Regulated by Burner T [degC] 300 200 100 0 1 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 Engine Mode Points Figure 6. SCR Inlet Temperature Comparison 13 17 18 19 20 21 Upstream of the SCR catalyst, a significant difference of NO2/NOx ratios was observed for the two comparison conditions as shown in Figure 7. The greatest NO2/NOx ratio was 31% at Mode 3 and most other modes had much lower NO2/NOx ratios when the burner was not used. When the burner was operated, the NO2/NOx ratios were for all modes higher than 40% with the exception of Modes 17 and 20. NO2/NOx Upstream of SCR Catalyst 80 Temp. Not Regulated by Burner Temp. Regulated by Burner NO2/NOx [%] 60 40 20 0 1 2 3 4 5 6 7 8 9 10 11 12 13 14 15 Engine Mode Points Figure 7. NO2/NOx Ratio Comparison 14 16 17 18 19 20 21 When the burner was operated to raise the exhaust gas temperature, an overall 74.9% NOx reduction efficiency was achieved based on the diluted tailpipe emission results. Figure 8 further shows the reduction rate for each test mode based on FTIR NOx measurement before and after the SCR catalyst. The reduction rates varied in the range of 55% to 96%. The NH3 slip concentrations are also plotted in Figure 8 for all the 21 modes. The NH3 slip for all modes was below 25ppm. In Modes 12, 17, 19, 20, and 21 the NH3 slip was above 10ppm. All other modes had NH3 slip below 10ppm. Modes with high NH3 slip had relatively higher exhaust flow than other modes due to higher speed, higher load or both. This might indicate that the SCR catalyst used in the tests was undersized so that NH3 could not get enough storage space and became susceptible to slip when exhaust space velocity increased. It is worth noting that there exists an opportunity to further optimize the urea dosing calibration. SCR NOx Reduction Efficiency and NH3 Slip NOx Reduction [%] 100 80 60 40 20 30 0 NH3 Slip [ppm] 25 20 15 10 5 0 1 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 17 Engine Mode Points Figure 8. SCR NOx Reduction Efficiency and NH3 Slip 15 18 19 20 21