b767 engineering continuation training
Transcription
b767 engineering continuation training
FOR REFERENCE ONLY B767 ENGINEERING CONTINUATION TRAINING Q1 & Q2 2013 FOR REFERENCE ONLY FOR REFERENCE ONLY Contents 1 DHL Air Procedures Review 2 Star Air Procedures Review 3 767 Maintenance Tips 4 767 Technical Notes & AENs (DHL Air) 5 767 Airworthiness Directives 6 767 UK Maintenance Related MOR FOR REFERENCE ONLY FOR REFERENCE ONLY 1 DHL Air Procedures Review For clear and precise instructions on how DHL Air require their Technical Logs to be completed, refer to the following! See DHL Air DAEP CD for DAEP No 67. Tech log completion See DHL Air DAEP CD for DAEP No 8 (General Section) Deferred Defect See DHL Air DAEP CD for DAEP No.70 and 67 and the DHL Air ETOPS manual for information relating to ETOPS Operations See DHL Air DAEP CD for DAEP No. 84 for AWOPS operations See DHL Air DAEP CD for DAEP No. 85 for RVSM operations. AEN 58E has been issued to give some useful flow charts providing guidance to all engineering staff on the ETOPS downgrading and upgrading process following a defect or maintenance action. There are relevant TRs to the DHL Air ETOPS manual. DAEP’s: ETOPS Manual: B767 Maint Tips: Available on CD Hard copy See TechCom 2 Star Air Procedures Review For clear and precise instructions on how Star Air require their Technical Logs to be completed, refer to the following! FOR REFERENCE ONLY FOR REFERENCE ONLY See Star Air CAME CD Part 1, Chapter 1.1.1 Aircraft Technical Log, Chapter 1.1.1.2 Instruction for Use See Star Air CAME CD Part 1, Chapter 1.1.4 Deferred Items, General. Defect reports (Deferred Defect Policy) Part 1, Chapter 1.8.3 ETOPS Operations – not applicable All Weather Operations – If there is ice or snow, do the cold weather maintenance service. Please refer to Boeing AMM ref. AMM 12-3301/301. RVSM – Refer to Boeing AMM TASK 51-10-00-206-001 (Examine the Airplane Skin) for instructions on Inspection/Check ALL OF THESE DOCUMENTS ARE AVAILABLE IN THE ALT LINE STATION OFFICE or ALT Technical Library: 3 B767 Maintenance Tips Please see ALT TechCom for full details using the following link or the full MTIP can be found in the “useful files” attachment to this module. https://intranet.altitudeglobal.aero/techlib/techserv/Maintenance%20Tips/Forms/AllIte ms.aspx Please note that non-relevant maintenance tips and those subject to correction of typographical errors or subject to minor non-relevant amendments have not been included in this listing. All complete MTIPS are in the useful file. There were no relevant Maintenance Tips for this period. FOR REFERENCE ONLY FOR REFERENCE ONLY 4 B767 Technical Notes & AENs (DHL Air) Below is a summary of all Technical Notes & AENs recently issued by DHL Air for the B767. TN / AENs Number: 48E Subject CF6-80C2 Information FOR REFERENCE ONLY TN Number: 68E FOR REFERENCE ONLY Subject Pegasus FMC 2009 Issues FOR REFERENCE ONLY TN Number: 69E FOR REFERENCE ONLY Subject Forward Equipment Cooling Fan Part Numbers FOR REFERENCE ONLY TN Number: 67E FOR REFERENCE ONLY Subject B767-300F Fleet Differences FOR REFERENCE ONLY FOR REFERENCE ONLY 5 B767 Airworthiness Directives Below is a listing of Airworthiness Directives issued over the last period: AD Reference: 2013-05-07 Subject Stiff Operation – Elevator Pitch Control AD Reference: 2013-07-09 Subject O2 Mask Stowage Box Units FOR REFERENCE ONLY AD Reference: 2013-08-20 6 FOR REFERENCE ONLY Subject Fuel Tube Replacement B767 Maintenance Related MOR The following are maintenance related extracts from the UK CAA MOR data base related to the B767 family. The information is protected by the UK CAA and the monthly digest are now strictly controlled by them. It is respectfully requested that with this in mind, the content of the following is not copied or distributed in any way. British Airways Bolt found in LH engine tail pipe during walk around. Bolt found laying on the green section of the acoustic lining. Engineer determined the bolt came from the inboard side of the pylon between the core and outer engine lining. Bolt replaced with proper torque setting. Checks revealed none of the bolts were at the correct torque setting, this was rectified. CAA Closure: Investigations confirmed that a bolt had been found in the LH engine tail pipe lying on the green section of the acoustic lining. The engineer determined that it came from the inboard side of the pylon, between the core and outer engine lining. He replaced the bolt with the proper torque setting. On checking other bolts in the area he found none were at the proper torque setting so retightened them all. The panel was the hoop plate fairing on the left engine and the a/c had recently had a 4C Check where the hoop plate fairing bolts are required to be torque checked in accordance with maintenance instructions. The engineering staff who had worked the engine overnight stated that the hoop plate inspection and check of bolts was carried out, with none found missing and the plate in good condition. The bolts in question are small and prone to vibrating loose. The instructions call for tightening of bolts which is considered as a satisfactory requirement. FOR REFERENCE ONLY British Airways FOR REFERENCE ONLY Unreported damage: Sheared and drilled bolt found inside engine thrust ring. The jacking bolt (used to remove the thrust ring) was found sheared off and still in place in the ring. The bolt appeared to have been drilled flush, indicating that it was known to be in place on re-fitting. It is likely that this would have been the cause of the reported high vibration, which was the reason for this engineering investigation. CAA Closure: The organisation has concluded its investigation. The subject a/c was last at contracted maintenance organisation for a 4 C check from the 27 Apr 2011 until 2 Jun 2011. During this check the right hand engine fan blades were removed, cleaned, lubricated and installed. This is the last recorded work performed on the subject engine relating to the damaged thrust ring. The investigation concentrated on two task cards from the pack. Detailed investigation could not establish that the rework occurred at this input, noting vibration was not reported post input and the witness marks appeared more recent. Further investigation failed to identify where the faulty work took place. It has therefore not been possible to identify the root cause in this instance and the evidence to date indicates that there may have been some unrecorded work activities but this cannot be confirmed. ThomsonFly A/c returned following multiple electrical and display failures. During taxi 'L GEN OFF' EICAS message appeared, checklists followed and generator reset. The same problem occurred on rotation along with the failure of captain's flight director, command airspeed bug and LH FMC CDU. Control was handed to FO whose display was functioning normally. Subsequently multiple failures occurred including failure of auto throttle, speed window frozen and MCP displays all frozen. Fuel jettisoned and a/c was flown back using RH autopilot and manual thrust. Engineers could find no faults once a/c was back on the ground. CAA Closure: BPCU BITE carried out which provided a ‘MPU/wiring’ 'LH generator' message. Fault diagnosis carried out and LH and RH generator GCU and IDG replaced due to failure. Operator's Reliability Department confirms that IDGs are now subject to a 16000hr soft life campaign. Furthermore, the minimum company requirement of received IDGs is set at OEM overhaul status. These actions are designed to increase in-service reliability. Data on GCUs shows no component reliability trends and no further relevant defects recorded to date with no autoflight system reoccurrences. ThomsonFly Flight crew oxygen found partially closed and wire locked. First Officer checked his oxygen and noticed a significant drop in pressure when tested. Pressure resumed after testing. Engineer checked oxygen tap and found it partially closed and wire locked. Wire lock broken and tap opened fully to allow normal oxygen supply. CAA Closure: The a/c had undergone a C Check at a third party maintenance organisation. A task was carried out which resulted in crew oxygen bottle being removed and refilled. After witnessing the installation of the bottle by the mechanic, the engineer ensured that the valve was fully open and performed a leak test before going to the flight deck to check EICAS. Meanwhile the mechanic installed the locking wire. The AMM procedure requires the installer to turn the valve to fully open then close the valve ‘one quarter of a turn’ before applying locking wire. The engineer inspected the safety wire and certified installation. During the event when the flight crew reported the drop in pressure, the oxygen bottle was inspected and was found to be partially closed and wire locked. Engineering staff involved were interviewed and it was found that both the engineer and mechanic had worked in excess of 50 hours in the 5 days prior to the error and the engineer had been responsible for certifying the majority of over 200 cabin interior defects. The operator has recorded seven similar events of the crew O2 cylinder being either closed or partially closed. The only common theme appears to be human error. Of the seven, only two are linked to a hangar location and these happened in 2008/9. The other six, including this event, were traced either to 3rd party maintenance organisations or line stations. FOR REFERENCE ONLY FOR REFERENCE ONLY During this period, there have been a five company Technical Notices issued to reinforce the need to follow AMM procedures and cautioning against partially closing the valve to the point of preventing oxygen flow. These have been available to third party MROs. The MRO has confirmed that the investigation report will be distributed to all engineers to ensure that all task requirements are strictly followed. They will actively demonstrate both the availability of qualified staff per project and the manhour-limitation for those staff. As a process improvement, review whether associated tasks should be linked together in a single process stream to ensure that tasks on the same system are completed at the same time. British Airways On removing nose wheel it was discovered that there was no axle washer or spacer fitted. Further reports reveal that missing items had been returned to the workshop attached to a wheel. ThomsonFly At 700ft on approach EICAS message 'trailing edge disagree'. Flap gauge checked both indicating flap 25. A/c manually flown and handled normally with uneventful landing completed. Flaps retracted normally. CAA Closure: EICAS message 'TE FLAP DISAGREE' appeared after selection of F25 on approach. During go-around, F20 selected and message disappeared. A/c then reconfigured early and after F25 was selected no EICAS message appeared. The landing checks were completed and at this point the 'TE FLAP DISAGREE' message flashed on and off for the rest of the second approach. It was concluded that it must be a spurious message and normal landing was completed. Similar messages have intermittently appeared on the B767 fleet, both in flight and during rollout and can go more than a year with no reports. Flap/Slat Electronic Unit (FSEU) BITE checks show no faults on the ground. All operators use an FSEU P/N 285T0049-53 or 285T0049-63 configuration. Boeing developed the -63 with an improved BITE and troubleshooting capability. Many operators with older 767 fleets maintain a few -63 units expressly for this purpose. The -63 also has greater tolerance when exposed to nuisance or intermittent fault indications. Boeing Fleet Team Digest 767-FTD-27-11003 refers. Experience has shown that while there could be multiple causes for the 'TE FLAP DISAGREE' message, operators benefit by focusing on certain higher probability components which is aided by using a -63 FSEU. The FSEU was replaced with a -63 part number to aid fault finding and reduce nuisance messages. No further occurrences to date. ThomsonFly LH engine ran down and stopped approx 1min after start. Run down associated with 'L eng spar valve' message. A/c returned to stand. CAA Closure: Circuit breaker P6- 1 E1 cycled and valve actuator exercised several times iaw FIM. Valve operation verified as satisfactory and engine started normally. The next day the symptoms occurred again and engineers transposed the LH engine spar valve V25 with LH wing defuel valve. The defuel valve was locked out in a closed position and the a/c despatched iaw MEL. On landing, spares were positioned, the defuel valve was replaced and a/c restored to flight conditions. The spar valve had failed due to normal wear and operator's reliability data indicates no trends with the item. FOR REFERENCE ONLY British Airways FOR REFERENCE ONLY 'Brake Temp' indication received at 110kts on take-off roll. After seeing brake unit 6 with a temperature of 9 units in white, indication was considered spurious and gear retracted. After 45secs there was no change to temperature indication and decided to stop at flap 1 and gear dropped. After 20secs indication dropped to 8 units. Gear left down for approx 4mins until temperature indication reached 4 units. Temperature slowly dropped to 1 unit after 40mins with gear retracted. Tyre pressure at 245psi initially dropping to 233psi. After consultation with Maintrol it was deemed the best option was to continue to destination. Brake temperature rose to 4 units on arrival at destination. Upon wheel removal, entire inner bearing assembly was missing and inner bearing housing was melted and fused. DHL Air Limited Oxygen cylinders in closed position and safety wired. During pre-flight check the contents of oxygen fell from 1700 to 950psi. On investigation both oxygen cylinders had been left in the closed position and safety wired. Both cylinders were safety wired in the open position and oxygen pressure tested to be within limits. British Airways First Officer rudder pedal locking mechanism failed during landing. No rudder input from P2 position. A/c on final approach in slight crosswind when application of rudder was applied to align a/c with runway centreline. P2 rudder pedals were not locked and therefore travelled as if they were being adjusted. A/c landed firmly but not in line with runway centreline. Control handed over to other pilot who aligned a/c with runway and controlled deceleration. Taxi to stand uneventful but P2 rudder pedals did not operate. Pre-flight checks had not highlighted this fault. Investigation showed that the spring loaded pin was not engaging with the lock plate. The pin had either worn away or had sheared and worn. British Airways Nr1 slat intermediate sensor and attachments found to be missing. On pushback, EICAS "LE SLAT ASYMM" warning occurred. On investigation the sensor target along with the auxiliary slat track roller bearing, bolt, washers and castellated nut were all missing. No evidence of the missing parts or of any damage sustained to the area. CAA Closure: Sensor 282 is located on the nr1 slat outboard auxiliary track and the intermediate target was found to be missing. The sensor provides position information and is also used to detect an asymmetry condition with the slats on the opposite wing. Each slat has two sensors for this purpose. The target installation also incorporates a roller for the auxiliary track an all these parts were found missing. As no asymmetry condition had been noted on the previous flight, the parts must have departed the a/c when the slats were deployed to the extended position. As the parts were unavailable for inspection, no determination of failure mode can be made. The bolt is secured by a nut and split pin, so it is reasonable to assume that the bolt sheared rather than the nut unwinding. There is no record of recent maintenance to the track. FOR REFERENCE ONLY ThomsonFly FOR REFERENCE ONLY During scheduled maintenance it was discovered that an electrical loom was resting on flight control cables. Whilst accessing crown skin station 544 it was observed that the electrical loom terminating at M749 (lighting ballast) was resting on the two sets of control cables for the rudder and elevator in the upper cabin area. Work order raised to inspect for damage, rectify and prevent continued loss of clearance. CAA Closure: No damage to the flight control cables was found and a fleet check was carried out without any other findings. Details of the occurrence was sent to the external maintenance organisation's Quality department for investigation of work carried out prior to the event. The response indicated that the previous tasks in 2009 were carried out correctly, evidenced by other non-related findings in that area and no evidence of loom movement. The root cause was an unpredicted gradual loom droop, potentially caused by disturbance away from the immediate area over the last three years. Cable fastenings in this area were considered to be of a satisfactory standard. The loom was repaired and cleaned and additional cable clamping was applied to the wire bundle to ensure clearance. A Quality Information Bulletin was published to internal and external maintenance personnel and for inclusion in technical training to alert staff to the safety issues. British Airways A/c flown not iaw MEL for RH thrust reverser fault. The MEL procedure had not been followed insofar as the circuit breakers, for locking out the inoperative thrust reverser, had not been tripped and collared as required. The a/c had flown for two days in this condition. CAA Closure: The investigation could not determine when the circuit breakers had been reset. A Quality Alert Bulletin is to be raised to reinforce the importance of recording all work carried out on a/c systems. FOR REFERENCE ONLY