Lube Free Die Casting
Transcription
Lube Free Die Casting
Lube Free Die Casting Steve Midson - Colorado School of Mines David Schwam – Case Western Reserve University Al Miller – Ohio State University Castings Solutions for Readiness AMC Technology Review June 16-17, 2016 Chicago, IL Die Castings for Military Applications • • • • • High volume manufacturing Lightweight and thin wall Low cost Excellent surface finish Close dimensional tolerances Die casters supply customers who sell to: • United States Army • United States Navy • United States Air Force • Defense Logistics Agency • United States Transportation Command • Missile Defense Agency • Defense Finance and Accounting Service • Defense Commissary Agency www.kineticdiecasting.com/military_parts.html 2 Problem • Die casting requires that a liquid organic-based lubricant be applied to the die cast die before each shot – Otherwise liquid metal will stick to steel die • Reduces quality of castings – Die lubricants are a major source of defects (porosity) • Adds cost to process – Purchase price of lubricants is high (up to 2.5% of the casting cost) – Life of die casting dies is compromised by thermal fluctuations caused by use of die lubricants (die life can be doubled without spray) • Creates expensive housekeeping issues – Effluents in air, on machine and on floor must continuously be cleaned 3 Spraying Die Lubricant 4 Needs and Benefits • DoD/DLA – Cost savings: reduced cycle time, increased die life, reduced costs from purchasing lubricants, and enhanced energy efficiency – Higher quality / performing parts: reduced porosity, increased production reliability – Sustainment: increased die life and durability • Foundry / Casting Supplier / Industry – Cost savings: reduced cycle time, increased die life, eliminate the costs associated with buying lubricants – Improved quality / performance: reduced porosity, better surface finish of the products, improved production reliability – Energy savings: reduced cycle time and energy consumption – Reliability: increased die life and durability – Environmental improvement: minimize effluents 5 Objectives • Without lubricant: The molten aluminum will solder to uncoated dies • With a suitable coating: Soldering of the aluminum can be minimized/avoided Soldering on uncoated core pin Project Objectives • Identify and apply permanent and semi-permanent coatings to steel dies so they do not require lubrication • Maintain high production rates without lubrication • Improve casting quality, reduce cycle times, decrease process costs and extend die life 6 Technical Approach Colorado School of Mines: • Utilize advanced physical vapor deposition (PVD) methods to develop non-sticking and self-lubricating coatings for metal molds • Develop coating architecture to ensure coating adheres to steel dies Case Western Reserve University • Design and benchmark an improved pull-out test for die lube release load testing • Use the pull-out test to evaluate Boron Nitride-based dry / semipermanent lubricants Ohio State University • Heat transfer modelling to assess the relative importance of spray for die cooling • Quantify heat balance, cycle time, and die temperature relationship 7 Previous Work in this Project • Developed a simple laboratory test that is representative of the die casting process • Evaluated both in-house and commercial coatings • Generated a quantitative measurement of the “sticking” behavior of molten aluminum on substrates and coatings Ceramic tube Molten A380 aluminum alloy Tensile test Procedures 1. 2. 3. 4. Heat substrate & tube in a furnace and pour the liquid A380 alloy into tube Keep the filled tube at temperature for 15 minutes Cool the assembly in furnace, to allow the A380 aluminum alloy to solidify Test the strength of the interface 8 Results – Adhesion Strength Material Supplier Method Adhesive Strength [MPa] AlCrN Supplier 1 Cathodic arc 0 AlTiN Supplier 1 Cathodic arc 0 CrWN Supplier 2 Thermal diffusion 0 AlTiN Supplier 3 Cathodic arc 0* TiAlN Supplier 3 Cathodic arc 0.01 CrN Supplier 4 Cathodic arc 0.07 Cr CSM Sputtering 0.12 CrN/AlN CSM Sputtering 0.19 CrWN Supplier 4 Cathodic arc 0.26 CrN Supplier 5 Cathodic arc 0.78 TiN CSM Sputtering 0.84 AlCrN TiB2 Supplier 5 Supplier 6 Cathodic arc Sputtering 1.30 2.54 *Stuck, but no load required to separate cast aluminum from coating 9 Results – Adhesion Strength Material Supplier Method Adhesive Strength [MPa] AlCrN Supplier 1 Cathodic arc 0 AlTiN Supplier 1 Cathodic arc 0 CrWN Supplier 2 Thermal diffusion 0 AlTiN Supplier 3 Cathodic arc 0* TiAlN Supplier 3 Cathodic arc 0.01 CrN Supplier 4 Cathodic arc 0.07 Cr CSM Sputtering 0.12 CrN/AlN CSM Sputtering 0.19 CrWN Supplier 4 Cathodic arc 0.26 CrN Supplier 5 Cathodic arc 0.78 TiN CSM Sputtering 0.84 AlCrN TiB2 Supplier 5 Supplier 6 Cathodic arc Sputtering 1.30 2.54 *Stuck, but no load required to separate cast aluminum from coating Exceeded project target of 0.05 MPa adhesive strength 10 Results – Adhesion Strength Material Supplier Method Adhesive Strength [MPa] AlCrN Supplier 1 Cathodic arc 0 AlTiN Supplier 1 Cathodic arc 0 CrWN Supplier 2 Thermal diffusion 0 AlTiN Supplier 3 Cathodic arc 0* TiAlN Supplier 3 Cathodic arc 0.01 CrN Supplier 4 Cathodic arc 0.07 Cr CSM Sputtering 0.12 CrN/AlN CSM Sputtering 0.19 CrWN Supplier 4 Cathodic arc 0.26 CrN Supplier 5 Cathodic arc 0.78 TiN CSM Sputtering 0.84 AlCrN TiB2 Supplier 5 Supplier 6 Cathodic arc Sputtering 1.30 2.54 *Stuck, but no load required to separate cast aluminum from coating AlCrN has best high temperature oxidation resistance – so research has focused on this coating 11 In-Plant Trials Colorado School of Mines 12 In-Plant Trials • Two plants trials of the AlCrN coating from Supplier 1 have been performed – Mercury Castings, Fond-du-Lac, WI • First trial – Coated single steel cavity insert in a larger die • Mercury Castings wanted to: – Test the durability of the coatings – Ensure that the coating would not cause problems • Second trial – Coated a complete die 13 1st Plant Trial 14 1st Plant Trial • Casting is a 350 HP Verado Gearcase • Coated insert is shown in red • Fabricated from H13 tool steel (46-48 RC) 15 1st Plant Trial • Trial was performed at Mercury Castings – December, 2015 • Alex Monroe (Mercury) & Jie Song (CSM) • Casting is produced with two loose steel inserts • Inserts are ejected from die with the casting • Several loose inserts are used in rotation • Inserts are normally lubricated 16 1st Plant Trial • Loose piece coated with AlCrN 17 1st Plant Trial Day 1 • First 5 shots with lube • Sprayed onto insert • Next 20 shots made with no lube • No evidence of sticking or soldering Day 2 • Another 20 shots produced with no lube • Again no evidence of sticking or soldering • Mercury personnel indicated that the uncoated loose piece sticks after 3 shots 18 1st Plant Trial • Photographs of inserts after trial No evidence of sticking was observed on the insert 19 1st Plant Trial Summary 1. This first plant trial appeared to be very successful 2. Castings would be expected to stick to a nonlubricated insert after 3 shots or so 3. AlCrN coated insert ran 40 shots without lubricant 4. No apparent sticking/soldering of aluminum to the coating’s surface 5. Based on the success of this initial trial • A decision was made to run a second plant trial • Coating a complete die casting die 20 2nd Plant Trial 21 2nd Plant Trial • Casting is a balance shaft housing 6.64 in • Weighs 1.75-lbs • Produced in a single cavity die – Using a 700-ton die casting machine 22 2nd Plant Trial • Trial again performed at Mercury Castings – May 2016 – PPAP (Pre-Production Approval Process) run • Prove to customer that castings meet requirements • Alex Monroe (Mercury) and Bo Wang (CSM) • Uncoated version of die had been run previously at Mercury – About 90,000 shots • Necessary to spray lube on uncoated die for 12 secs 23 2nd Plant Trial • Entire die coated with AlCrN by Supplier 1 Moving side of die – Moving side • Cavity, runner block, vent block and core pins – Fixed side • Cavity and vent block Fixed side of die 24 2nd Plant Trial Day 1 • 70 castings produced using 2 seconds lube spray – 83% reduction in spray – No evidence of sticking • 30 castings produced using 1 second lube spray – 92% reduction in spray – No evidence of sticking • One casting attempted with no spray – Stuck 25 2nd Plant Trial • Stuck casting bent on ejection Stuck casting bent on ejection – Red area of casting stuck • Heavy section near gate • During removal of stuck casting – Core pin was bent • Had to remove die – Replace all core pins – With new, coated core pins Bent core pin Area shaded in red stuck 26 2nd Plant Trial Day 2 • Die was replaced on machine • 96 castings were produced using 1 second lube spray – 92% reduction in spray – No evidence of sticking 27 2nd Plant Trial 28 2nd Plant Trial Summary 1. Second plant trial was also very successful Lube Free 2. Entire die was coated with AlCrN • From Supplier 1 3. Coating allowed a reduction in spray time from 12 seconds to 1 second • Spray zone 92% reduction in spray 4. Casting produced with no lube did stick in the die 29 Mechanism Controlling Sticking / Non-Sticking Behavior 30 Sticking / Non-Sticking Mechanism • Continuing to perform laboratory research to determine the mechanisms that control the observed sticking and non-sticking behaviors • Possible cause of the different behavior for AlCrN 1. Differences in chemical composition of the coating (Al:Cr ratio) 2. Roughness of the coating 3. Presence of an oxide layer on the surface of the AlCrN coating 31 Summary and Conclusions Colorado School of Mines 32 Summary and Conclusions 1. Based on a simple aluminum adhesion test developed at CSM • An AlCrN permanent die coating has been identified that exhibits non-sticking behavior with aluminum A380 die casting alloy 2. Plant trials using the AlCrN coating have demonstrated excellent results • Successfully ran lube free with a single cavity insert • Reduced lubricant spraying by 92% on a fully coated die 3. Still working to understand the mechanism controlling the observed sticking/non-sticking behavior 33 Future Work 1. Perform laboratory studies to determine the mechanism controlling the sticking/non-sticking behavior of aluminum alloy against various coatings 2. Continue the plant trial of both the insert and the fully coated die i. Run the insert until the coating fails • Determine the mechanism of failure ii. Continue to run the fully coated die • Determine if the 1 second spray time can be maintained 34 Case Western Reserve University 35 Technical Progress Case Western Reserve • Design and benchmarking of a new pullout test for die lube testing • Laboratory testing of BN-based die lubes in collaboration with Momentive, a producer of BN • Evaluation of BN-based die lubricants in production at Mercury Castings and PHB Inc. (planned) • Use of the release tester to develop and implement a high performance dry lubricant system 36 Technical Progress Case Western Reserve Schematic of the Pull-out Experimental Set-up 37 Technical Progress Case Western Reserve Experimental set-up for Pull-out Test 38 Technical Progress Case Western Reserve Experimental set-up for Pull-out Test 39 Technical Progress Case Western Reserve Evaluated BN Coating Before Before BN FPC 50:50 BN LPC 50:50 After After 40 Technical Progress Case Western Reserve Typical BN Coatings Before BN GPC 50:50 After Before BN ZYP 50:50 After 41 Technical Progress Case Western Reserve 42 Technical Progress Case Western Reserve 3000 Release Load (lbs) - Commercial Die Lubes 2500 2000 1500 1000 500 0 HMA 1:40 HMA 1:80 Moresco Moresco SL 1:40 SL 1:80 1: 40 1:80 HNA 1:40 HNA 1:80 43 Technical Progress Case Western Reserve Summary • The test provides good sensitivity to measure release load, differentiate among die lubricants and determine the effect of dilution ratios. • BN formulations released at very low loads. • Commercial die lubricants evaluated at higher dilution ratios (1:40, 1:80) required much higher release loads. 44 Project Plans Case Western Reserve • Next 12 months – Benchmark more commercial die lubricants – Compare release load of die lubricants with in-plant performance at PHB Inc. – Measure increase in release load when the BN-based die lubricant is applied once every 10, 25, 50 pull-out cycles – Evaluate and implement BN-based dry lubricants (with Momentive) in production 45 Ohio State University 46 Technical Progress Modeling • Impact of elimination of spray on thermal control • Post injection heat transfer modeling issues • Cooling design tradeoffs 47 Addressed Today Modeling • Compensating for lack of spray by – Letting the die run hot – Adjusting the internal cooling • Sensitivity of the die thermal balance • Do we understand thermal quasiequilibrium? 48 Model Modeling To cooling line Casting Closed Open • Cycle: • Assumptions: – – – – Die Spray Open Conduction from casting to die when closed (post fill) Conduction to platen at face opposite casting Convection to air at cavity side when open Spray approximated by convection • Simple enough for easy sensitivity analysis • Complete enough for understanding trends 49 Questions Modeling • Spray, or lack of spray, affects die heat load and thermal balance – How much? • Spray is intermittent, internal cooling is continuous (usually). – Does that matter? • Spray is at the surface. Cooling lines are internal. – Does that matter? 50 Basic Cycle with Spray Modeling • Die temperature over one cycle – Part rapidly dumps heat then heat transfer slows – How much heat depends on both part and die Why not shorten cycle by 10 or 15 seconds? Is this die thermally stable? 51 Equilibrium Modeling • With or without spray, die temperature equilibrium depends on – How rapidly die temperature can change when temp difference exists – Heat fluxes in and out • Fluxes depend on both die and sink or source temperatures • Die temperature transient has to play out – Depends on how far to go and how fast you can go 52 Is This Die Stable? Modeling Temperature still rising, and not slowing, after 200 cycles without spray Same Curve 53 Die and Part Surface Modeling 1.5oC (0.5%) ∆ at cycle 20 0.3oC (0.07%) ∆ at cycle 100 Eject Temp: 370oC cycle 20 465oC cycle 100 475oC cycle 200 Acceptable? 54 Improved Internal Cooling Modeling • Locked in by cycle 20 • 250oC initial condition close to long term average Ejection Temp @ cycle 20: 318oC 55 Both Dynamics and Die Heat Content Matter Modeling • Blue curve - initial surface temp history from previous slides • Orange curve has exact same cooling • No equilibrium until enough heat to balance flux in and out 56 Summary Modeling • Letting a die run hotter, i.e. no change in internal cooling or cycle time, may or may not work – How much heat did spray remove? – Will affect other variables, e.g. part ejection temp – Initial conditions matter – How long do you run before interruptions 57 Project Plans Modeling • Compete and use 2-D version of model for more complete internal cooling pattern studies • Review practices used in Mercury Castings experiments • Guidelines / recommendations for NADCA 58 Project Metrics Description Baseline Threshold Objective Non-wetting/ Nonsticking (Sticking strength) 0.5 MPa 0.1 MPa 0.05 MPa Thermal stability 675oC 800oC 1,000oC Mechanical properties (Hardness) 25 GPa 30 GPA 35 GPa Wear resistance (Wear rate) 5x10-5 mm3N-1m-1 1x10-5 mm3N-m-1 2x10-6 mm3N-1m-1 In-plant testing of coatings (Die life) 5,000 shots 10,000 shots 30,000 shots 59 JDMTP Criteria - Summary Jointness B – Benefit to more than one service, but not jointly funded Needs: Non-sticking and self-lubricating coatings for metal molds to reduce cycle time / production costs, and improve die life and part quality Needs and Benefits Transition Leveraging MRL Benefits: –Cost savings: reduced cycle time, increased die life, and energy savings –Higher quality / performing parts: production reliability improves quality –Sustainment: increased die life and durability –Environmental improvement: lubricant-free process • Commercial suppliers such as Tribologix, Dayton & Phygen will reproduce the optimized self-lubricating coatings on die components in their industrial sized coaters. • In-plant trial testing at Mercury Castings and others • Computer Modeling Guidelines for lube free die casting through NADCA • Presentations at committee & chapter meetings and annual NADCA Congress • Webinars, Die Casting Engineer articles • DOE E-SMARRT “Smart Die Coatings” • CSM’s ACSEL and CANSFA consortia • NADCA-funded project on ultra-sonic coatings evaluation 4 – Manufacturing capability to produce the system in a laboratory environment 60 Lube Free Die Casting DLA - POC: Dean Hutchins ([email protected], 804-279-5033) Problem – Applying die lubricant: – – – – Partners: • Colorado School of Mines, Case Western Reserve, Ohio State University, NADCA, Phygen, Mercury Marine, Twin City Die Casting, Premier Tool and Die Source of porosity Reduces die life Adds time to the casting cycle, increases costs Produces effluent with associated waste issues Objective – Develop non-sticking and self-lubricating coatings for metal molds to improve part quality, decrease cycle time and reduce process costs. Benefits – Higher quality / performing parts – Cost savings from reduced cycle times and increased die life – Supply chain reliability from increased die life – Environmental improvement (lubricant-free process) Milestones / Deliverables – Coating properties measured and characterized – Computer modeling method for die and process design – In-plant trails on coating system 61