Flexible risers at Kristin, StatoilHydro
Transcription
Flexible risers at Kristin, StatoilHydro
Classification: Internal Flexible risers at Kristin Flexible Pipelines and Risers PSA Norway 12.12. 2007 Nils Terje Nordsve, StatoilHydro 2 Drift Nord Hammerfest Harstad Alve Urd Idun Norne Skarv Heidrun Sandnessjøen Åsgard Kris tin * * Brønnøysund Mikk el Njord Draugen Stjørdal Tjeldbergodden Trondheim Ormen Lange Kristiansund Nyhamna Kårstø SLP/UK 3 Key data for Kristin • Water depth: 320 m • Reservoir pressure: 911 barg • Reservoir temperature: 170 °C • Production capacity – Gas: 18.3 MSm3/sd – Condensate: 20000 Sm3/sd • Number of risers: 9 • Number of umbilicals: 5 Photo: Trond Sigvaldsen 4 Kristin field layout Possible sidetrack to existing N-3H well N Åsgard C N-102/N-201 N101 P ”S-4 target” FORE Template and well slot ID’s: AF S3T S4 ST S2 S B 1 FOR E Grid North P-102/P201 POR T P101 Kristi n Semi To Åsgard FOC-1/B-401 l le Oi cab 11 t 2 cal i P or t p p ex re o Fib P-212 N P-212 S P-212 Gas export loop Åsgard Transp ort P-121 Permanent P&A Not accessible Pig direc tion S-103/S201 S R-103/R-201 Toft e S101 S102 R FORE R101 R-102 10" ID prod (13% Cr.) w/ DEH 12" oil export (CS) 18" gas export (CS) Umbilical w/ 2" ID centre line 3.5“ ID service line (CS) Fibre optical cable (FOC) Direct el. heating (DEH) risers Future tie-in hub SSIV ROV operated ball valve Check valve Diverless hot tap tee Temporary pig launcher 16 ” Completed well Completion ongoing Drilled and capped well Drilling commenced Planned well Spare well slot Not available well slot 5 Kristin risers – historical account until early November 2006 • The export risers were parked on seabed in October 2004 • The flexible risers were tied back to the platform in April to June 2005 • Annulus vacuum testing performed in May/June 2005 confirmed that all risers were intact after installation • First production took place 3rd November 2005 (through S-101) • Problem with one riser detected early November 2006 (S-101) Leakage detected early November 2006 End fitting by annulus vent monitoring system Gas diffusion or leakage through polymer liner Valve opens automatically to release gas when pressure gauge measures 0.5 barg Water spray Air pressure 1.7 barg Normal gas permeation Rapid pressure build up 6 7 Kristin riser S-101 – early work done to identify damage • The pressure in the riser was increased to 80 bar; the riser remaining out of service • The pressure in the Riser Guide Tube was reduced to ambient pressure – Frequent pressure relief of annulus ended => The phenomenon was due to leakage in the outer sheath 20.5 m 1.7 barg (P &GE risers) Cast insert 20.5 m – Frequent pressure relief of annulus continued after ambient pressure was achieved RGTs pressurised to ~ 17 m Riser S-101 was depressurized down to ambient pressure (prod. risers only) RGT water level • Water spraying 1.0 m Supposed reason was leakage of hydrocarbons from riser bore through the pressure sheath into annulus 7.5 m • 8 S-101 – Test to determine location of damage 20.5 m Cast insert RGT water level location 7.5 m Damage 1.0 m 17 m 20.5 m Testing was carried out 20th to 21st November 2006 9 Kristin risers – damages detected • Scheduled vacuum tests in November 2006 showed that all export risers were intact • Vacuum tests in December 2006 – Damage to four risers confirmed: S-101, R-101, R-102 and P-211A – Damage to riser S-102 detected May 2007 10 Consequences of damage • Tensile armours are exposed – Possible wear against RGT inner surface – Corrosion fatigue in aerated sea water • Riser calculated fatigue lives in aerated sea water – Production risers: Five to eight years – Condensate export riser: 2.5 years – Gas export risers: Six months 11 Potential causes – as evaluated at an early stage • Possible material problem? – TP-Flex™ is a new material – Brittle behaviour? – Bad wear resistance? • Mechanical damage – due to inadequate Riser Guide Tubes? – Surface roughness? – Misalignment? 12 Material testing performed • Fatigue of tensile armours • Tensile testing of outer sheath • Wear testing of outer sheath Fracture 13 Preliminary wear test results of outer sheath materials •Testing carried out for 0.13 to 2.0 MPa contact pressure Riser RGT •Wear rate varies linearly with contact pressure •TP-Flex wears faster than Rilsan (dry and wet) •Both materials wear faster wet than dry Contact pressure •Largest difference between Wet TP-Flex and dry Rilsan Wear depth 14 Roughness typically measured with profile print-outs at three points for all bellmouths 15 Kristin vs. Åsgard B guide tube solution Hang-off at Riser balcony ÅSG B Contact force difference: ∆ load=sin 5°x50 tonnes=4.5 tonnes Kristin, vertical + 5° bend Åsgard, straight 5° inclined KRI 16 Wear protection collars at Værnes 17 Installation of wear protection collars A 1 2 3 28/42 29/43 30/44 B 1. Mount clamp anti-sliding clamp (A) on riser 2. Install collars consecutively; neck down 3. Mount extra locking clamp (B) on neck of lowermost collar 4. Hang clump weight on lowermost collar 5. Release and remove anti-sliding clamp (A) 6. Release collars from clump weight 7. Collars will then slide into the RGT driven by buoyancy Locking mechanism ROV handles 18 Wear protection collars on R-101 entering RGT 19 Experiences from installation of wear protection • Practice makes perfect: – From more than one hour per collar to typically four collars per hour • Due to friction against the RGT the collars may stop on their way upwards: – Will eventually move during rougher seas – Tilting the platform and/or adding buoyancy would help • One some collars the locking mechanism opened 20 Examples of wear protection collars that have opened P-211A P-212S 21 16 collars missing on riser P-212N 22 Lost collar - Picture taken after recovery 23 Wear protection collar – locking mechanism 24 Dry riser repair • Project with Aker Reinertsen – Kick-off 28th March 2007 Cheap – First riser repaired 20th August 2007 • Complex project with short execution time • Close co-operation between the parties involved was required Safe Fast 25 Damage to riser P-211A before cut-out for welding 26 Damage to the R risers before cut-out for welding R-101 R-102 27 Damage to the S risers before cut-out for welding S-101 S-102 28 Connection of patch to outer sheath By Sikaflex R-102 By welding 29 Application of heat shrink R-102 30 Temporary offloading of condensate during repair of P-211A 31 Summary of damages and repairs • Damages were detected as follows: – S-101: 5th November 2006 – R-101: 19th November 2006 – R-102: 25th November 2006 – P-211A: 16th December 2006 (vacuum test – OK in November) – S-102: 11th May 2007 • Repair carried out: – R-102 repaired 20th August 2007; second time 5th October 2007 – S-101 repaired 28th August 2007 – P-211A repaired 10th September 2007 – R-101 repaired 18th September 2007 – S-102 repaired 25th September 2007 32 New risers • Contract with Technip: – Delivery 01.09.2008 – 6 new risers (1 x condensate export, 1 x gas export, 4 x production) • Outer sheath material: – Rilsan for all risers – Rilsan protective sheath in RGT area – Cooling of production risers required for flow temperatures exceeding 92°C • Wear protection collars most likely to be used for new risers 33 Lessons learned so far • Damage is due to wear rather than fracture • Rilsan has better wear resistance than TP-Flex • Wear resistance is better dry than wet • Riser Guide Tubes are important – Geometry – Inner surface condition • Riser configuration is important • Locking mechanism of Wear Protection Collars is crucial 34 Concluding remarks • Wear protection collars installed on all risers • Problems with the locking mechanisms encountered – Design changed • Fast track repair project – All suppliers have met schedule – No HES incidents • Work ongoing to clarify cause of damages – Wear of outer sheath against inner surface of RGTs – RGT geometry? – Riser configurations?